CESSNA 152

Madisonville, TN — February 28, 2022

Event Information

DateFebruary 28, 2022
Event TypeACC
NTSB NumberERA22LA139
Event ID20220301104708
LocationMadisonville, TN
CountryUSA
Coordinates35.54962, -84.34380
AirportMONROE COUNTY
Highest InjuryMINR

Aircraft

MakeCESSNA
Model152
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor2
None0
Total Injured2

Event Location

Probable Cause

A partial loss of engine power for undetermined reasons.

Full Narrative

On February 28, 2022, about 1730 eastern standard time, a Cessna 152, N68218, was substantially damaged when it was involved in an accident near Madisonville, Tennessee. The pilot and passenger received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
According to the pilot, after a normal preflight inspection, he departed with 20 gallons of fuel for a local flight. After a 30-minute flight, about 5 miles from the airport, he initiated a descent from 3,000 ft and slightly reduced engine power. About 10 seconds later, the engine rpm suddenly dropped to 900 to 1,000 rpm. He advanced the throttle and turned on the carburetor heat, with no effect on the engine. He performed a forced landing and touched down on a wet grassy field. During the rollout the main landing gear wheels locked up, the airplane hit a tree stump and came to a stop.
According to the Federal Aviation Administration (FAA) inspector who responded to the site, the left wing was nearly separated at the wing root, and the firewall was bent. A detailed examination of the engine supervised by the FAA inspector confirmed crankshaft continuity. Compression and suction were observed on all four cylinders and a lighted borescope was used to view the interior of the cylinders and no anomalies were noted. The propeller was separated at the crankshaft flange. The carburetor was separated, the throttle cable remained partially attached. The magnetos remained attached to the engine, and spark was observed from all towers when rotated by hand. The oil suction screen and filter were absent of debris.
According to the manufacturer’s maintenance manual, the engine should be overhauled every 12 years. Review of the maintenance logbooks revealed the engine had not been overhauled since 1998. The engine had accumulated 1,598 hours since the overhaul. Between the annual inspection in 2021 and the previous annual in 2017, the airplane accumulated 4 hours of flight time.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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