CESSNA 150M

Toledo, OR — September 3, 2012

Event Information

DateSeptember 3, 2012
Event TypeACC
NTSB NumberWPR12LA391
Event ID20120903X94646
LocationToledo, OR
CountryUSA
Coordinates44.61666, -123.93333
AirportToledo State Airport
Highest InjurySERS

Aircraft

MakeCESSNA
Model150M
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious1
Minor0
None0
Total Injured1

Event Location

Probable Cause

The pilot’s failure to maintain directional control of the airplane after landing.

Full Narrative

On September 3, 2012, about 0945 Pacific daylight time, a Cessna 150M, N3700V, sustained substantial damage during landing at the Toledo State Airport (5S4), Toledo, Oregon. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91. The commercial pilot, the sole occupant of the airplane, sustained serious injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight. The local flight originated from Newport, Oregon, at 0930 with an intended destination of 5S4.

The 94-year old pilot reported to a Federal Aviation Administration (FAA) inspector that following normal approach and landing on runway 31, a 1,750-foot long and 40-foot wide asphalt runway, the airplane veered to the right. The pilot said that he attempted to apply left rudder, however, the rudder pedal would not move. Subsequently, the airplane exited the right side of the runway and struck a hangar. The pilot further reported to the inspector that he reduced the throttle before landing, and did not advance the throttle prior to impact with the hangar.

Witnesses located adjacent to the accident site reported observing the accident airplane enter a normal final approach for runway 31. One witness stated that the airplane “landed hard and fast” about 100 feet from the runway threshold, and started going to the right. Another witness stated that the airplane touched down fast near the approach end of the runway, bounced 5 to 8 feet in the air, begin to wobble, and touch back down. The witness said that the airplane traveled about 100 feet along the runway when it violently veered to the right. The witness added that the engine noise got louder just before the airplane exited the runway, and did not decrease until the airplane came to rest in a ditch.

Examination of the airplane by an FAA inspector and a representative from Cessna Aircraft Company revealed that both wings and the fuselage were structurally damaged. Examination of the airplanes flight controls, brake system, nose wheel steering system, and engine throttle control revealed no evidence of any preexisting mechanical malfunction or failure that would have precluded normal operation.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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