CESSNA 208B

Kipnuk, AK — January 6, 2011

Event Information

DateJanuary 6, 2011
Event TypeACC
NTSB NumberANC11LA009
Event ID20110107X52253
LocationKipnuk, AK
CountryUSA
Coordinates59.93278, -164.03027
AirportKipnuk Airport
Highest InjuryNONE

Aircraft

MakeCESSNA
Model208B
CategoryAIR
FAR Part135
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None6
Total Injured0

Event Location

Probable Cause

The pilot’s decision to land long on the icy snow-covered runway, resulting in a runway excursion and collision with terrain.

Full Narrative

On January 6, 2011, about 1326 Alaska standard time, a Cessna 208B, N715HE, sustained substantial damage during landing on runway 33 at the Kipnuk Airport (PAKI), Kipnuk, Alaska. The airplane was registered to Icecap LLC Trustee, Anchorage, Alaska, and operated by Hageland Aviation, Anchorage, as scheduled commuter Flight 161 under the provisions of Title 14 Code of Federal Regulations Part 135. The commercial certificated captain, first officer, and the four passengers, were not injured. Visual meteorological conditions prevailed, and a company flight plan was active. The flight originated at Bethel, Alaska at 1240, with an intended destination of Kipnuk.

During a telephone conversation with the Safety Board investigator-in-charge, the captain reported that following an uneventful flight, he obtained the current weather conditions at PAKI from the airport's automated surface observation system, noting the wind was from the northeast at 10 knots. He said he flew over the airport, and entered a left downwind for runway 33. The captain stated that following a normal approach, he landed long on the 2120 foot long runway to avoid a bump in the runway. As the airplane touched down on the runway, he applied brakes and moved the propeller into beta. During the landing roll, he realized the airplane was still traveling too fast on the snow and ice covered runway to stop, and he did not have enough area to abort the landing. He said he applied maximum brakes, but the airplane overran the departure end of runway 33, and impacted a ditch. The airplane came to rest right wing and nose low.

Examination of the airplane by the captain revealed that the right wing was bent upwards about 3 to 4 feet inboard from the wingtip. The captain noted that there were no preimpact mechanical problems with the airplane that contributed to the accident.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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