CESSNA 172E

Mammoth Lakes, CA — August 22, 2010

Event Information

DateAugust 22, 2010
Event TypeACC
NTSB NumberWPR10LA417
Event ID20100822X41843
LocationMammoth Lakes, CA
CountryUSA
Coordinates37.62389, -118.83861
AirportMammoth Yosemite Airport
Highest InjurySERS

Aircraft

MakeCESSNA
Model172E
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious4
Minor0
None0
Total Injured4

Event Location

Probable Cause

The pilot’s failure to maintain adequate airspeed and airplane control during takeoff in high density altitude conditions, which resulted in an aerodynamic stall.

Full Narrative

On August 22, 2010, about 0833 Pacific daylight time, a Cessna 172E airplane, N7807U, sustained substantial damage following an in-flight collision with terrain at the Mammoth Yosemite Airport, Mammoth Lakes, California. The private pilot and three adult passengers sustained serious injuries. The airplane sustained structural damage to the forward fuselage and wings. The airplane was being operated by the pilot as a personal cross-country flight under the provisions of 14 Code of Federal Regulations (CFR) Part 91, when the accident occurred. Visual meteorological conditions prevailed, and no flight plan was filed. The flight originated from Mammoth Lakes.

In a written statement to the National Transportation Safety Board (NTSB), the pilot reported that shortly after takeoff the airplane encountered turbulence and a downdraft, and began to lose altitude rapidly. The pilot stated he tried to control the airplane; however, it impacted terrain in a nose-low attitude.

During a telephone conversation with the NTSB investigator-in-charge, the front seat passenger stated that the takeoff roll was long and they "had a little time taking off, gradually going up with the buzzer going off." He reported that shortly after liftoff, the airplane encountered an updraft followed by a downdraft. He stated the pilot initiated a turn to the left which was followed by a "stall."

The four-seat, high-wing, fixed-gear airplane was manufactured in 1964, and powered by a Continental O-300, 145-hp engine. The airplane was equipped with a fixed-pitch propeller. The published maximum gross takeoff weight for the airplane was 2,300 pounds. The pilot did not report the actual takeoff weight of the airplane.

A review of recorded weather data from the automated weather observation station at the airport revealed at 0829 conditions in part were: wind from 220 degrees at 5 knots, visibility of 10 statute miles, temperature 18 degrees Celsius, and altimeter 30.18 inches of mercury.

The airport elevation was 7,135 feet. Using the reported temperature and altimeter setting, the calculated density altitude during the time of the accident was approximately 8,900 feet.

A post impact examination of the airframe and engine did not reveal any anomalies with the airframe or engine that would have precluded normal operation.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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