CESSNA 310K

El Monte, CA — July 14, 2010

Event Information

DateJuly 14, 2010
Event TypeACC
NTSB NumberWPR10LA349
Event ID20100714X01135
LocationEl Monte, CA
CountryUSA
Coordinates34.08472, -118.03416
AirportEl Monte Airport
Highest InjuryNONE

Aircraft

MakeCESSNA
Model310K
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

The pilot’s failure to maintain directional control during the takeoff ground roll.

Full Narrative

On July 14, 2010, about 0855 Pacific daylight time (PDT), a Cessna 310K, N6909L, exited the side of the runway during an aborted takeoff at El Monte Airport (EMT), El Monte, California. Lightning Aircraft Corporation was operating the airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The private pilot, the sole occupant, was uninjured. The airplane sustained substantial damage to both wings and the right horizontal stabilizer. The local personal flight departed El Monte about 0845. Visual meteorological conditions prevailed, and no flight plan had been filed.

According to the pilot, he was conducting touch-and-go landings during a post annual maintenance flight. The pilot reported that after touchdown, he retracted the flaps and increased power when the airplane pulled to the right. The pilot applied full left rudder and reduced power to idle; the airplane continued to the right and exited the runway onto the soft ground. Subsequently, the right main landing gear collapsed and the airplane slid to a stop.

A review of Federal Aviation Administration (FAA) records revealed that the pilot holds a private pilot certificate in single-engine land aircraft. The pilot’s flight logbook indicated a multi-engine endorsement for solo flight, which was issued on December 24, 1984. The pilot reported to the FAA inspector-in-charge (IIC) that he had 2,500 total hours of flight time, and about 1,200 hours in the airplane make and model involved in the accident. In the past year, the pilot flew 4 hours in the Cessna 310.

An inspection of the airplane by FAA maintenance inspectors noted no engine or flight control system abnormalities.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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