MOONEY M20R

New Port Richey, FL — June 9, 2025

Event Information

DateJune 9, 2025
Event TypeACC
NTSB NumberERA25LA273
Event ID20250721200582
LocationNew Port Richey, FL
CountryUSA
Coordinates28.28308, -82.64070
AirportHIDDEN LAKE
Highest InjuryNONE

Aircraft

MakeMOONEY
ModelM20R
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Full Narrative

On June 9, 2025, about 0600 eastern daylight time, a Mooney, M20R airplane, N9166Z, was substantially damaged when it was involved in an accident near New Port Richey, Florida. The commercial pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot reported that he departed Inverness Airport (INF), Inverness, Florida and flew for about 15 minutes to Hidden Lake Airport (FA40), New Port Richey, Florida where he intended to land. During the landing flare to runway 5, a 4,425-ft-long runway, the airplane floated; the pilot reported that he was uncomfortable trying to land on the remaining runway, so he executed a go-around, by adding full power and setting the flaps for climb. During the maneuver, at about 50 ft. the engine immediately stopped producing power. There was no hesitation or “engine cough” that preceded the loss of power. Too low to fully troubleshoot, the pilot switched fuel tanks, but it did not restore power and the airplane began to descend.
The airplane descended into the runway overrun area and impacted brush and muddy terrain before coming to rest upright. A Federal Aviation Administration inspector examined the airplane after recovery and confirmed substantial damage to the wings and fuselage. The right wing sustained damage to the wing spar and there were multiple buckles and dents throughout the fuselage.
According to the pilot, he should have had at least 17 gallons remaining in the fuel tanks at the time of the accident, based on his fuel consumption and the airplane’s most recent fueling that occurred on June 1, 2025. In addition, he reported that neither low fuel quantity warning lights illuminated during the flight.
The pilot called to report the accident on July 19, 2025, 40 days after its occurrence. The airplane was retained for further examination.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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