CESSNA 182Q
Gardner, KS — April 7, 2023
Event Information
| Date | April 7, 2023 |
| Event Type | ACC |
| NTSB Number | CEN23LA149 |
| Event ID | 20230411107037 |
| Location | Gardner, KS |
| Country | USA |
| Coordinates | 38.80685, -94.95675 |
| Highest Injury | NONE |
Aircraft
| Make | CESSNA |
| Model | 182Q |
| Category | AIR |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 0 |
| None | 2 |
| Total Injured | 0 |
Probable Cause
A total loss of engine power due to failure of the No. 6 connecting rod as a result of detonation.
Full Narrative
On April 7, 2023, about 1648 central daylight time, a Cessna 182Q airplane, N982NC, was substantially damaged when it was involved in an accident near Gardner, Kansas. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot reported that the flight departed New Century AirCenter Airport (IXD), Olathe, Kansas, and was enroute to Lloyd Stearman Field Airport (1K1), Benton, Kansas. About 30 minutes into the flight, he noticed a subtle, abnormal vibration and elected to return to IXD. He stated that the engine gauges all indicated normally, and the only indication of an issue was the subtle vibration. As the airplane approached IXD, he noticed a high cylinder head temperature (CHT) on one cylinder, but he could not recall which cylinder. He adjusted the fuel mixture and was able to lower the CHT. As the airplane was descending, the engine went from full power to a partial loss of engine power and ultimately to total failure over a period of about 30 seconds. The pilot reported that, except for the one high CHT indication, all of the engine indications were normal until the engine lost power.
During the subsequent forced landing, the airplane impacted a culvert and nosed over. The airplane sustained substantial damage to the fuselage. A postaccident examination revealed that the engine could not be rotated by hand. In addition, there was a hole in the top of the engine case above the No. 6 connecting rod, and the No. 6 connecting rod was separated from the crankshaft. Removal of the cylinders and pistons revealed varying damage consistent with detonation. The No. 5 piston was melted on the intake side and displayed evidence of severe detonation. Damage to the skirt of cylinder No. 6 prevented removal of the piston. All the intake and exhaust valves and associated pushrods were intact with no damage noted.
An interview of the mechanic who had performed recent maintenance revealed that all six cylinders were recently replaced with new or repaired units 90.7 flight hours before the accident. All work was performed in accordance with the Continental Overhaul Manual. There was no mention of work performed on the pistons or rings being repaired. The mechanic stated in the interview that he had not performed a cold valve clearance check when the cylinders were installed.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.