PIPER PA32R

Loogootee, IN — April 30, 2022

Event Information

DateApril 30, 2022
Event TypeACC
NTSB NumberCEN22LA186
Event ID20220502105024
LocationLoogootee, IN
CountryUSA
Coordinates38.71570, -86.91282
Highest InjuryNONE

Aircraft

MakePIPER
ModelPA32R
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Probable Cause

The inadequate maintenance and subsequent failure of an internal component in the fuel servo that prevented adequate fuel flow to the engine, which resulted in a partial loss of engine power.

Full Narrative

On April 30, 2022, about 0810 eastern daylight time, a Piper PA-32R-301 airplane, N4303P, was substantially damaged when it was involved in an accident near Loogootee, Indiana. The pilot and passenger were not injured. The airplane was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.
The pilot reported that he and a passenger departed Huntingburg Airport (HNB), Huntingburg, Indiana, and were en route to Putnam County Regional Airport (GPC), Greencastle, Indiana. About 10 minutes after departure, while in cruise flight at 3,000 ft mean sea level, the engine lost partial power. The pilot performed a forced landing to a gravel road. During the landing, the airplane’s left wing contacted a tree resulting in substantial damage.
The airplane was transported to a recovery facility for further examination. After the airplane was recovered, a Federal Aviation Administration (FAA) inspector examined the engine and could not find any anomalies with the engine. An engine functional test run was conducted, and full engine rpm could not be achieved. The fuel servo and fuel flow divider were removed and sent for further examination.
Testing of the fuel servo found that it could not deliver more than 22 pounds per hour of fuel, which was less than the rated specifications. Disassembly discovered that the self-locking nut (p/n 2539449) was stuck inside the top section of the plug. This resulted in the head idle spring not properly allowing fuel to flow through the ball valve.
The FAA inspector was informed by the mechanic that the fuel servo was overhauled at the same time as the engine, in March 2002, at a total time of 2,011.1 hours. At the time of the accident, the airplane had accrued 4,383.3 hours. Precision Airmotive Service Bulletin PRS-97 revision 2, dated November 22, 2013, established the time between overhaul for all designated fuel system components to be the same as the engine manufacturer or 12 years, whichever occurred first. Lycoming established a time between overhaul of 1,800 hours.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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