HILLER UH-12E
Powder River, WY — October 30, 2008
Event Information
| Date | October 30, 2008 |
| Event Type | ACC |
| NTSB Number | WPR09LA028 |
| Event ID | 20081030X14507 |
| Location | Powder River, WY |
| Country | USA |
| Coordinates | 43.03556, -107.08111 |
| Highest Injury | MINR |
Aircraft
| Make | HILLER |
| Model | UH-12E |
| Category | HELI |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 1 |
| None | 1 |
| Total Injured | 1 |
Event Location
Probable Cause
A flight control system malfunction while the helicopter was maneuvering at low altitude due to the failure/separation of the rotor blade control tube.
Full Narrative
October 30, 2008, about 0840 mountain daylight time, a Hiller UH-12E, N61436, experienced a flight control system malfunction while maneuvering about 5 miles west-southwest of Powder River, Wyoming. Unable to maintain control of the helicopter, the pilot made a hard forced landing on the slope of a hillside. Upon touchdown, the helicopter rolled over and was substantially damaged. The commercial certificated pilot received a minor injury, and the passenger was not injured. The helicopter was owned and operated by Wyoming Air Corporation, Casper, Wyoming. Visual meteorological conditions prevailed at the time of the aerial observation (predator control) flight, and no flight plan was filed. The flight was performed under the provisions of 14 Code of Federal Regulations Part 91, and it originated from a refueling vehicle near Powder River, about 0830.
The pilot reported to the National Transportation Safety Board investigator that the accident occurred while he was maneuvering about 50 feet above ground level and looking for coyotes. Suddenly, one blade associated with the control rotor assembly separated from the helicopter and a violent vibration started. The pilot reported that the vibration precluded him from being able to read the airspeed indicator, and he only had "minimal control" of the helicopter.
During the subsequent examination of the helicopter, one of the two control rotor blade assemblies (Hiller part number 36209-3) was found separated from the rotor head. The rotor control blade assembly tube was observed cracked and broken off outboard of the two bolts attaching it to the cuff assembly. The helicopter had been operated about 21 hours since receiving its last annual inspection.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.