PIPER PA 44-180

Gaithersburg, MD — June 9, 2017

Event Information

DateJune 9, 2017
Event TypeACC
NTSB NumberERA17LA204
Event ID20170609X91950
LocationGaithersburg, MD
CountryUSA
Coordinates39.16833, -77.16611
AirportMONTGOMERY COUNTY AIRPARK
Highest InjuryNONE

Aircraft

MakePIPER
ModelPA 44-180
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionNITE
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None4
Total Injured0

Probable Cause

The failure of the right main landing gear trunnion bracket due to an undetermined overstress event.

Full Narrative

On June 8, 2017, about 2110 eastern daylight time, a Piper PA-44-180 airplane, N3020M, was substantially damaged during landing rollout at Montgomery County Airpark (GAI), Gaithersburg, Maryland. The flight instructor and two student pilots were not injured. The instructional flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the local flight.According to the flight instructor, he was returning to home base after a training flight that consisted of basic maneuvers, as well as two takeoffs and landings to a full stop. During the final approach the flight instructor configured the airplane for landing and briefed the student pilot. The touchdown was uneventful and during the landing roll the airplane began veering to the right of centerline. The airplane came to a full stop and the instructor performed an engine shutdown before exiting the airplane. On inspection of the airplane the flight instructor noted that the right main landing gear was collapsed and bent backwards towards the aft of the airplane.

Examination of the airplane by a Federal Aviation Administration inspector revealed that the aft right wing spar web was damaged during the landing sequence. Further examination of the landing gear revealed that the right aft main landing gear trunnion bracket failed. A visual examination of the fracture surfaces by the NTSB Materials laboratory revealed that there were no signs of fatigued failure within the trunnion, and the bracket failed during an overstress event. A review of the logbooks did not reveal any recent maintenance to the landing gear assembly.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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