Brennan RV-8

Idaho Falls, ID — October 1, 2008

Event Information

DateOctober 1, 2008
Event TypeACC
NTSB NumberSEA08LA216
Event ID20081006X60439
LocationIdaho Falls, ID
CountryUSA
Coordinates43.06361, -112.07056
AirportIdaho Falls Regional Airport
Highest InjuryNONE

Aircraft

MakeBrennan
ModelRV-8
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Event Location

Probable Cause

The on-ground fire during taxi due to a loose fuel line "B" nut.

Full Narrative

On September 30, 2008, about 1825 mountain daylight time, an amateur built Brennan RV-8 experimental airplane, N272RS, was substantially damaged by an on-ground fire while taxiing for departure at the Idaho Falls Regional Airport (IDA), Idaho Falls, Idaho. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 with no flight plan filed. Visual meteorological conditions prevailed. The commercial pilot and his passenger were not injured. The cross-country personal flight was originating at the time of the accident with a planned destination of Heber, Utah.

The pilot reported that while taxiing to the runway for departure, he noticed flames entering the cockpit below his feet. He immediately stopped the airplane and shut the engine down as he and his passenger exited the airplane. The airport's Aircraft Rescue Fire Fighting (ARFF) team responded and extinguished the fire, which was originating from the engine compartment. A few minutes later, the fire reportedly ignited a second time and was immediately extinguished by ARFF personnel.

Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that the firewall was severely fire damaged and buckled. The engine compartment and forward portion of the fuselage were thermally damaged.

Examination of the airplane by a local mechanic revealed that a "B" nut attaching the firewall end of the fuel line from the firewall to the engine driven fuel pump was found "finger tight." When the airplane was placed in a tail high attitude, fuel was observed leaking from this fitting. The mechanic stated that after the ARFF team extinguished the fire, he disconnected the battery. Prior to disconnecting the battery, he noted that the electric fuel boost pump was on. The reason for the loose "B" nut was undetermined.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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