Milholland Kelly D
Livingston, TX — October 7, 2016
Event Information
| Date | October 7, 2016 |
| Event Type | ACC |
| Location | Livingston, TX |
| Country | USA |
| Coordinates | 30.67945, -95.01334 |
| Airport | Livingston Municipal Airport |
| Highest Injury | NONE |
| NTSB Number | CEN17LA015 |
| Event ID | 20161012X54219 |
Aircraft
| Make | Milholland |
| Model | Kelly D |
| Registration # | N522LM |
| Category | AIR |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 0 |
| None | 1 |
| Total Injured | 0 |
Event Location
Probable Cause
A total loss of engine power for reasons that could not be determined based on the available information.
Full Narrative
On October 7, 2016, about 1315 central daylight time, a Milholland Kelly D airplane, N522LM, was substantially damaged during a forced landing 1/2 mile north of Livingston Municipal Airport (OOR), Livingston, Texas. The pilot was not injured. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91 without a flight plan. Visual meteorological conditions prevailed. The cross-country flight departed Sport Flyers Airport (27XS), Brookshire, Texas, about 1200, and was en route to OOR.According to the pilot, while approaching OOR for landing, the engine rpms decreased and the engine stopped producing power. He added that there were no indications from the engine or the engine gauges prior to the sudden power loss. During the forced landing to the field, the landing gear collapsed and partially separated from the fuselage. The lower wings, fuselage, and firewall were substantially damaged.
An examination of the engine revealed that the left magneto was not producing spark. Further examination of the engine and related systems revealed no additional mechanical anomalies that would have precluded normal operations.
The left magneto was placed on a test machine and brought to operating speed. Each of the four ignition leads produced spark; however, at times the spark was intermittent. Further examination of the magneto revealed a greyish color on the points, consistent with failure of the capacitor. The technician remarked that a magneto could test within expected parameters but when it got hot during normal engine operations, it could fail.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.