DOUGLAS BRIAN G BA-100

Killeen, TX — August 10, 2013

Event Information

DateAugust 10, 2013
Event TypeACC
LocationKilleen, TX
CountryUSA
Coordinates31.08583, -97.68639
AirportKilleen Skylark Field Airport
Highest InjuryNONE
NTSB NumberCEN13LA478
Event ID20130812X25533

Aircraft

MakeDOUGLAS BRIAN G
ModelBA-100
Registration #N27BD
OperatorDOUGLAS BRIAN G
OwnerDOUGLAS BRIAN G
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

The pilot’s improper management of the fuel mixture, which resulted in an over-rich fuel mixture condition and a subsequent partial loss of engine power.

Full Narrative

On August 10, 2013, about 0927 central daylight time, a Brian Douglas BA-100 airplane, N27BD, was substantially damaged during a forced landing near Killeen, Texas. The pilot, who was the sole occupant, was not injured. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which departed without a flight plan. The local flight originated from Skylark Field Airport (KILE), near Killeen, Texas, about 0925.

According to the pilot's statement, the airplane departed Runway 01 at KILE and the engine lost partial power while in the crosswind turn. The pilot considered turning back toward the runway, but elected not to because he was concerned that the airplane might enter into a spin. The pilot maneuvered the airplane and made a forced landing, during which both wings were structurally damaged during impact with trees.

Following the accident, the engine and fuel system were examined by an airframe and powerplant mechanic. Both fuel tanks were about ¾ full, with no evidence of fuel contamination. The magnetos and ignition leads were operable. Both spark plugs for the #1 cylinder were completely carbon fouled and the spark plugs for #2-#4 cylinders were significantly sooted. The pilot stated that he had set the engine mixture control to the full rich position during taxi and takeoff for the accident flight.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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