BUCKEYE PARTNERS, LP
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | BUCKEYE PARTNERS, LP |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 40.62252, -80.41810 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON MARCH 20TH 2011 AT APPROXIMATELY 14:02, BUCKEYE WAS NOTIFIED BY EMERGENCY RESPONDERS OF A POSSIBLE LEAK ON THE BUCKEYE LINE IN SHIPPINGPORT, PA. BUCKEYE IMMEDIATELY DISPATCHED LOCAL FIELD PERSONNEL AND BEGAN A CONTROLLED SHUTDOWN AND ISOLATION OF THE LINE CONTAINING ULTRA LOW SULFUR DIESEL (ULSD). THE APPROPRIATE INTERNAL AND EXTERNAL NOTIFICATIONS WERE MADE TO REPORT THE RELEASE AND DISPATCH TEAMS OF RESPONDERS TO CONTAIN THE PRODUCT AND REPAIR THE DEFECT IN THE LINE. THE DAMAGED PIPE WAS CUT OUT AND REPLACED WITH CERTIFIED PIPE ON 3/23/11. THE PIPE SEGMENT CONTAINING THE DEFECT WAS SENT TO A LABORATORY FOR METALLURGICAL ANALYSIS TO DETERMINE THE EXACT CAUSE OF THE RELEASE. ONCE THE PERMANENT REPAIR WAS COMPLETED ON MARCH 23RD, THE LINE WAS RESTARTED AT A TEMPORARILY REDUCED MOP. AS AN EXTRA PRECAUTION, THE LINE IS OPERATING AT THE REDUCED MOP UNTIL THE ANALYSIS OF THE PIPELINE IS COMPLETED. MOST OF THE PRODUCT HAS BEEN RECOVERED AS REMEDIATION EFFORTS CONTINUE. A PROFESSIONAL METALLURGICAL ANALYSIS CLAIMS IT IS LIKELY THAT THE CORROSIVE LOW PH WATER DIRECTLY CONTACTING THE EXPOSED SEGMENT OF PIPELINE CAUSED THE LOCALIZED EXTERNAL PITTING CORROSION LEADING TO THE THROUGH WALL DEFECT AND THE SURROUNDING METAL LOSS.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.