SUNOCO PIPELINE L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorSUNOCO PIPELINE L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.17974, -82.21559

Cause

CauseEXCAVATION DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

CONTROL CENTER RECEIVED LOW PRESSURE ALARMS AT 22:18 AND INITIATED SYSTEM SHUT DOWN. PIPELINE WAS SHUT DOWN AT 22:22. CAUSE OF LEAK WAS DETERMINED THROUGH METALLURGICAL ANALYSIS TO BE A RUPTURE CAUSED BY A SMALL CRACK AT THE BASE OF AN AREA OF MECHANICAL DAMAGE (E.G., DENT AND LONGITUDINAL GOUGES). IT WAS NOT POSSIBLE TO DETERMINE WHEN THE MECHANICAL DAMAGE OCCURRED. THE LINE SEGMENT WAS RESTARTED PER THE CONDITIONS STIPULATED IN THE CAO (3-2012-5002H) REQUIREMENTS ON 02/23/012.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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