ENTERPRISE CRUDE PIPELINE LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENTERPRISE CRUDE PIPELINE LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates35.95325, -96.75886

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

THE STATION OPERATOR OBSERVED OIL IN THE DIKE OF TANKS 21 AND 22 DURING DAILY LOCATION INSPECTION. THE LINES WERE ISOLATED AND FREE STANDING OIL WAS REMOVED PRIOR TO EXCAVATION. LINE WAS HYDRO EXCAVATED AND THE LEAK WAS CLAMPED THE FOLLOWING MORNING. 1500 FEET OF 24 INCH PIPE FROM MANIFOLD A TO TANK #23 WAS REMOVED AND REPLACED. LINE WAS PUT BACK INTO SERVICE ON JUNE 22, 2012. THE REMOVED PIPE WAS SENT TO LAB FOR METALLURGICAL ANALYSIS. METALLURGICAL REPORT ON THE PIPE INDICATED INTERNAL CORROSION WAS THE REASON FOR THE LEAK. ADDITIONAL CORROSION INHIBITOR HAS BEEN ADDED TO THE INJECTION POINT FOR THIS AREA TO ASSIST IN MITIGATING THE INTERNAL CORROSION. REMEDIATION WAS COMPLETED ON THE REMAINING CONTAMINATION.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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