COLONIAL PIPELINE CO

hazardous_liquid Incident — — June 2, 2015

Incident Information

Incident DateJune 2, 2015
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates33.59888, -85.82550

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$100
Emergency Response$3,000
Other Costs$0

Location Map

Incident Narrative

"AT 07:30 CST 6/3/15 WHILE AT OXFORD STATION TO PERFORM MAINTENANCE ACTIVITIES A COLONIAL TECHNICIAN OBSERVED PRODUCT DRIPPING FROM THE THERMAL WELL BUSHING ON A LINE 2 RISER. THE TECHNICIAN IMMEDIATELY PLACED A BUCKET UNDER THE DRIP AND NOTIFIED THE LINE 2 CONTROLLER, OPERATIONS MANAGER AND ENVIRONMENTAL SPECIALIST. SINCE THERE WERE NO IMPACTS TO GROUNDWATER NO ADDITIONAL NOTIFICATIONS WERE REQUIRED. THE CONTROLLER BYPASSED AND SHUT DOWN THE STATION AT 09:55 CST. THE REPAIR WAS COMPLETED AND STATION RESTARTED AT 10:20 CST. THE CLEAN UP BEGAN AS SOON AS REPAIR WAS COMPLETE. 5.5 YARDS OF CONTAMINATED SOIL WAS REMOVED. RELEASE VOLUME WAS CALCULATED TO BE 11 GALLONS - 9.5 GALLONS OF LIQUID RECOVERED AND SOIL ANALYSIS (SEE ATTACHED) INDICATED 1.5 GALLONS OF PRODUCT IN EXCAVATED SOIL. CLEAN UP WAS COMPLETE ON 6/4/15. SOIL WILL BE DISPOSED OF AT PINE RIDGE LANDFILL."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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