WOLVERINE PIPELINE CO

hazardous_liquid Incident — — March 16, 2014

Incident Information

Incident DateMarch 16, 2014
OperatorWOLVERINE PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates43.01628, -84.65540

Cause

CauseEQUIPMENT FAILURE
SubcauseDEFECTIVE OR LOOSE TUBING OR FITTING

Casualties

Fatalities0
Injuries0

Costs

Property Damage$200
Emergency Response$15,000
Other Costs$0

Location Map

Incident Narrative

WOLVERINE PIPE LINE OPERATION CONTROL CENTER RECEIVED A CALL FROM A LANDOWNER THAT THERE WAS WHAT SMELLED LIKE DIESEL FUEL AROUND A MAINLINE ISOLATION VALVE. THE PIPELINE WAS IMMEDIATELY SHUT IN & COMPANY EMPLOYEES WERE DISPATCHED TO INVESTIGATE. LINE PRESSURE WAS RELIEVED TO A DOWNSTREAM DELIVERY POINT, WHICH STOPPED THE RELEASE OF PRODUCT. COMPANY EMPLOYEES REMOVED THE RELEASED PRODUCT WITH A VAC TRUCK & ABSORBENTS. THE ORIGIN OF THE RELEASE WAS FOUND TO BE AN ABOVE GROUND PIPING CONNECTION. THE PIPING WAS CONNECTED TO A VALVE BODY GREASE/BLOCK & BLEED CONNECTION ON THE ORBIT 6 INCH VALVE BODY. NEW PIPING WAS INSTALLED. THE VALVE BODY & FLANGES WERE EXCAVATED FOR AN INTEGRITY INSPECTION. ALL OTHER SIMILAR INSTALLATIONS WERE ALSO INSPECTED. THE LINE WAS SUBJECTED TO A ONE HOUR STAND UP PRESSURE TEST BEFORE THE LINE WAS RESTARTED. APPROXIMATELY 240 CUBIC YARDS OF SOIL WERE EXCAVATED FOR PROPER DISPOSAL.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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