PETROLOGISTICS OLEFINS, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorPETROLOGISTICS OLEFINS, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates29.43130, -95.65000

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

4/30/2014 8:30 A.M. HOUSTON AMMONIA/T & L LEASE SERVICES BEGAN ANOMALY DIG ON AN AMMONIA PIPELINE. JUSTIN KELLY WAS PRESENT TO WITNESS EXPOSING OF THE 4' PGP PIPELINE. JUSTIN PERFORMED LEL TEST AND NO GAS DETECTED. 10:15 A.M. 4 INCH PGP PIPELINE EXPOSED. AT THAT TIME PIPELINE WAS NOT IN CONTACT WITH CASING. 12:45 P.M. T&L CREW MEMBER NOTICED LEAK AND TOLD BLM TECHNICIAN JUSTIN KELLY ABOUT LEAK. JUSTIN IMMEDIATELY NOTIFIED CONTROL ROOM TO SHUT DOWN THE 4 INCH PGP LINE. CONTROL ROOM CLOSED RSD AT THE PL PROPYLENE FACILITY, AND BEGAN DRAW DOWN OF PIPELINE VIA TOTAL. CONDITIONS ARE CLEAR; VAPOR CLOUD FORMED FOR LESS THAN 3 MINUTES AND BEGAN TO DISSIPATE. BLM TECH CURTIS BLACK REMAINS ON SITE TO KEEP SITE CLEAR AND INSURE TO PUBLIC IMPACT. 12:50 P.M. JUSTIN NOTIFIES VAUGHN TROSCLAIR AND PAT BARDWELL OF LEAK, 1:10 P.M. BLM CONTROL ROOM COMPLETES DRAW DOWN OF 4' PGP LINE AND SHUTS TOTAL RSD 1:15 P.M. JUSTIN CLOSES 4' VALVE AT GEORGIA GULF ROAD, AND DOW MAINLINE PGP. 1:30 P.M. JUSTIN CLOSES 4' VALVE AT AND DOW MAINLINE PGP. 1:38 P.M. PAT BARDWELL NOTIFIES NATIONAL RESPONSE CENTER OF LEAK. REPORTING 7 BARRELS RELEASED AND LINE ISOLATED. NRC NUMBER IS 1081325. 1:44 P.M. TEXAS HOME LAND AND EMERGENCY SERVICES NOTIFIED OF LEAK 1:49 PM. TEXAS RAIL ROAD COMMISSION NOTIFIED OF LEAK. LEAK REPORT WILL BE REFERRED TO AREA INSPECTOR FOR REVIEW 2:30 P.M. DAVID WARD (HARRIS COUNTY EMERGENCY SERVICES) INSPECTS LEAK AREA 3:45 P.M. CLAMP INSTALLED OVER GIRTH WELD TO CONTAIN PROPYLENE. 4:26 P.M. BEGAN FLARING 4' PGP PIPELINE. LINE PRESSURE AT 218 6:13 P.M VICTOR JIMENEZ (TRRC) ARRIVES ONSITE TO INSPECT LEAK AREA 5/01/2014 12:00 A.M. END FLARING ON 4 INCH PGP. LINE PRESSURE 2 PSIG 1:30 A.M. INSTALLED SPECTACLE BLIND AT 6/4 JUNCTION 2:30 A.M. INSTALLED SPECTACLE BLIND AT DOW 7:30 A.M. RESUME FLARING OF RESIDUAL PROPYLENE AND PURGING LINE WITH NITROGEN. 9:15 A.M. 4 INCH PGP LINE PURGE COMPLETED 9:30 A.M. DUSTIN HARRIS (BLM SYSTEM INTEGRITY TECH) ARRIVES TAKES SOIL POTENTIALS AND IDENTIFIES 4' PGP AS SHORTED TO CASING BELOW. PIPE HAS SAGGED OVERNIGHT AS THE PIPE SETTLED OVERNIGHT. 10:00 SPRINT WELDER BEGINS TEST FOR QUALIFYING 12:00 P.M. TEXAS RAILROAD COMMISSION PIPELINE SAFETY INSPECTOR VICTOR JIMENEZ ARRIVES ON SITE FOR FIELD FOLLOW UP 1:00 P.M. SPRINT PIPELINE ARRIVES WELDER ONSITE TO TAKE MEASUREMENTS FOR SPOOL FABRICATION 2:00 P.M. TRRC PIPELINE INSPECTOR LEAVES SITE, BLM TO PROVIDE FOLLOW UP ON INVESTIGATION AND REPORT. 3:00 P.M. SPRINT PIPELINE BEGINS FABRICATION OF SPOOL PIECE 9:00 P.M. HYDROSTATIC TEST BEGINS, 11:00 A.M. WELDER WELDS WELDOLET ON CUTOUT PIECE 5/02/2014 12:00 A.M. HYDROSTATIC TEST PRESSURE LOCKED IN. AMBIENT TEMPERATURE IS DROPPING. 4:00 A.M. HYDROSTATIC TEST COMPLETE 8:00 A.M. BEGIN REMOVAL OF CUT OUT SECTION 2:30 P.M. TIE IN WELDS COMPLETE 3:30 P.M. X- RAY COMPLETE ALL WELDS ACCEPTABLE 4:00 P.M. BEGIN COMMISSIONING PGP PIPELINE 5:30 P.M. 4 INCH PGP SEGMENT COMMISSIONING COMPLETE. ALL BLINDS HAVE BEEN REMOVED. 12/18/2014: UPDATED BY PHMSA PER THE OPERATOR'S MARK UP SINCE THE OPID IS NO LONGER ACTIVE IN PHMSA'S DATABASE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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