COLONIAL PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorCOLONIAL PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.30467, -92.82545

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

AT APPROXIMATELY 11:00 ON 8/25/14, A TECHNICIAN ARRIVED AT WELSH STATION TO RESPOND TO A COMMUNICATIONS FAILURE. THE TECHNICIAN OBSERVED A STAIN ON THE GROUND ABOVE THE LINE 2 UNIT 2 CHECK VALVE. INTERNAL NOTIFICATIONS WERE MADE AND A CONTRACT CREW WAS CALLED IN TO EXCAVATE THE AREA FOR THE SUSPECTED LEAK. THE CONTRACTOR ARRIVED ON SITE AT 11:45 AND THE STATION WAS SHUT DOWN AND ISOLATED BY 12:10. THE LEAK WAS DETERMINED TO BE ORIGINATING FROM A FLANGE ASSOCIATED WITH THE UNIT CHECK VALVE SPRING CAN. THE LEAK SOURCE WAS POSITIVELY IDENTIFIED AND STOPPED BY 13:30. REPAIRS WERE COMPLETED ON THE CHECK VALVE AND THE STATION WAS RESTARTED AT 19:37. THE CAUSE OF THE RELEASE WAS A FAILED GASKET AT THE FLANGE LOCATION ON THE CHECK VALVE SPRING CAN. THE SOFT GOODS ON THE OTHER SIDE OF THE CHECK VALVE WERE REPLACED ON 8/26/14. ALL RELEASED PRODUCT WAS CONTAINED ON COMPANY PROPERTY IN THE IMMEDIATE AREA. CONTAMINATED SOIL EXCAVATION WAS COMPLETED ON 8/27/14. AN ELECTRONIC NOTIFICATION WAS MADE TO THE LOUISIANA DEQ/SPOC WITHIN 24 HOURS OF THE INCIDENT AND A WRITTEN FOLLOW UP REPORT WAS FILED WITHIN 7 DAYS PER APPLICABLE STATE REGULATIONS.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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