COLONIAL PIPELINE CO
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | COLONIAL PIPELINE CO |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 30.30467, -92.82545 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
AT APPROXIMATELY 11:00 ON 8/25/14, A TECHNICIAN ARRIVED AT WELSH STATION TO RESPOND TO A COMMUNICATIONS FAILURE. THE TECHNICIAN OBSERVED A STAIN ON THE GROUND ABOVE THE LINE 2 UNIT 2 CHECK VALVE. INTERNAL NOTIFICATIONS WERE MADE AND A CONTRACT CREW WAS CALLED IN TO EXCAVATE THE AREA FOR THE SUSPECTED LEAK. THE CONTRACTOR ARRIVED ON SITE AT 11:45 AND THE STATION WAS SHUT DOWN AND ISOLATED BY 12:10. THE LEAK WAS DETERMINED TO BE ORIGINATING FROM A FLANGE ASSOCIATED WITH THE UNIT CHECK VALVE SPRING CAN. THE LEAK SOURCE WAS POSITIVELY IDENTIFIED AND STOPPED BY 13:30. REPAIRS WERE COMPLETED ON THE CHECK VALVE AND THE STATION WAS RESTARTED AT 19:37. THE CAUSE OF THE RELEASE WAS A FAILED GASKET AT THE FLANGE LOCATION ON THE CHECK VALVE SPRING CAN. THE SOFT GOODS ON THE OTHER SIDE OF THE CHECK VALVE WERE REPLACED ON 8/26/14. ALL RELEASED PRODUCT WAS CONTAINED ON COMPANY PROPERTY IN THE IMMEDIATE AREA. CONTAMINATED SOIL EXCAVATION WAS COMPLETED ON 8/27/14. AN ELECTRONIC NOTIFICATION WAS MADE TO THE LOUISIANA DEQ/SPOC WITHIN 24 HOURS OF THE INCIDENT AND A WRITTEN FOLLOW UP REPORT WAS FILED WITHIN 7 DAYS PER APPLICABLE STATE REGULATIONS.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.