PLAINS PIPELINE, L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorPLAINS PIPELINE, L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.01142, -102.01289

Cause

CauseEXCAVATION DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

APPROXIMATELY 500 BBLS OF CRUDE OIL WERE RELEASED FROM A TANK-TO-TANK TRANSFER LINE, WHICH RUNS FROM PLAINS MIDLAND MESA TERMINAL TO THE ADJOINING PLAINS MIDLAND BASIN TERMINAL. THE RELEASE FROM THIS TERMINAL PIPING WAS A RESULT OF EXCAVATION DAMAGE BY A SECOND PARTY. THE ROOT CAUSE IS STILL UNDER INVESTIGATION. THE PIPE HAS BEEN SENT TO THE LAB TO UNDERGO METALLURGICAL ANALYSIS; THEREFORE, A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE THE ROOT CAUSE AND LAB ANALYSIS IS RECEIVED. THE NATIONAL RESPONSE CENTER (NRC) WAS NOTIFIED AND ASSIGNED REPORT NUMBER 1104686. SUPPLEMENTAL NARRATIVE: BASED ON THE EXAMINATIONS AND ANALYSIS, IT WAS DETERMINED THAT THE FAILURE WAS THE RESULT OF THIRD-PARTY DAMAGE THAT CREATED A RELATIVELY LARGE DENT AT THE LF-ERW SEAM IN THE LINE. BECAUSE THE PIPELINE WAS IDENTIFIED AND ASSIGNED INCORRECTLY IN THE ONE-CALL SYSTEM, THE LINE WAS INADEQUATELY MARKED. SUBSEQUENTLY, THE LINE WAS STRUCK DURING AN EXCAVATION PROJECT. ADDITIONALLY, NO EVIDENCE OF CORROSION, FATIGUE, OR OTHER TIME-DEPENDENT FLAW-GROWTH MECHANISMS WERE OBSERVED AND NO EVIDENCE OF FLAWS IN THE LF-ERW SEAM OR IN EITHER OF THE ADJACENT GIRTH WELDS WERE IDENTIFIED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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