ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.09048, -88.29830

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

DURING AN INTEGRITY DIG ON FEBRUARY 10, CONTRACTOR CREW SMELLED CRUDE OIL AT APPROXIMATELY 3:15 PM CST. THE PIPELINE WAS SHUTDOWN AT 3:54 PM CST TO INVESTIGATE THE SOURCE OF THE CRUDE ODOR. AFTER FURTHER INVESTIGATION IT WAS CONFIRMED THAT CRUDE OIL WAS SEEPING FROM BEHIND THE COAL TAR PIPELINE COATING. APPROXIMATE VOLUME OUT IS 1 1/2 CUPS. THE INTEGRITY DIG LOCATION WAS BASED UPON THE LINE 62 MAGNETIC FLUX LEAKAGE IN-LINE INSPECTION TOOL RUN WHERE THE TARGET ANOMALY WAS CALLED OUT AS INTERNAL METAL LOSS INDICATION LOCATED AT MP 20.8627. THE ACTUAL SOURCE POINT OF THE LEAK WAS APPROXIMATELY 2 INCHES FROM THE TARGETED ANOMALY. THE FEATURE WAS NOT REMOVED; REPAIRS WERE MADE BY INSTALLING A 2 FOOT LONG TIGHT FITTED SLEEVE. THE THRU-WALL FEATURE WAS IDENTIFIED AS A MANUFACTURING FLAW BASED ON RESULTS OF DIRECT ASSESSMENT OF THE FEATURE IN THE FIELD AND ANALYSIS OF THE CORRESPONDING ILI DATA. THE ORIENTATION OF THE FEATURE WAS NOT ALIGNED WITH PRINCIPLE STRESS ON THE PIPE. VISUALLY THE FEATURE MATCHES DESCRIPTION OF LAP AS DEFINED BY API STANDARD 5T1. LESS THAN 1 CUBIC FOOT OF CONTAMINATED SOIL WAS REMOVED AND DISPOSED OF AT AN APPROVED DISPOSAL FACILITY

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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