ENBRIDGE STORAGE (CUSHING) L.L.C.

hazardous_liquid Incident — — February 27, 2015

Incident Information

Incident DateFebruary 27, 2015
OperatorENBRIDGE STORAGE (CUSHING) L.L.C.
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates35.93444, -96.75213

Cause

CauseINCORRECT OPERATION
SubcauseOTHER INCORRECT OPERATION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$4,000
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

ON FEBRUARY 27 AT 11:46 AM, CUSHING CONTROL CENTER RECEIVED 2 SEAL FAIL ALARMS ON MANIFOLD 259 (BOOSTERS 01 AND 02) AND THE SUMP TANK BEGAN TO RUN; BOOSTERS WERE ISOLATED AND TECHNICIANS WERE NOTIFIED. THE CAUSE OF THIS RELEASE WAS A RESULT OF ENTERPRISE (SEAWAY LINE 15) SHUTTING DOWN THE LINE ACCIDENTALLY WHILE IN THE PROCESS OF SWITCHING UNITS. THE DRAIN LINES WERE NOT ABLE TO DRAIN FAST ENOUGH TO ACCOMMODATE THE FLOW RATE FROM THE PSV'S, WHICH IN TURN CAUSE THE GRAVITY FEED LINES FROM THE BOOSTER SEAL DRAINS TO BACK UP. THE GRAVITY FED DRAIN LINES ARE ISOLATED AND CONTINUE TO BE ISOLATED UNTIL A PERMANENT ENGINEERING SOLUTION CAN BE APPLIED. ESTIMATED VOLUME RELEASED IS 8 GALLONS. CONTAMINATED SOIL WAS REMOVED AND DISPOSED OF AT AN APPROVED DISPOSAL FACILITY

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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