PLAINS PIPELINE, L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorPLAINS PIPELINE, L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates35.46695, -119.70443

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

APPROXIMATELY 12.7 BBLS OF CRUDE OIL WERE RELEASED FROM A 10-INCH, BELOW-GROUND SECTION OF PIPE, AS A RESULT OF INTERNAL CORROSION. THE SEGMENT OF PIPE WAS REPLACED, AND HAS BEEN SENT FOR A THIRD PARTY EVALUATION TO CONFIRM THE CAUSE OF THE CORROSION. A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE THE RESULTS ARE RECEIVED. THE NATIONAL RESPONSE CENTER (NRC) WAS NOTIFIED AND ASSIGNED REPORT NUMBER 1118360. SUPPLEMENTAL NARRATIVE: THE THIRD PARTY EVALUATION HAS CONFIRMED THE ROOT CAUSE OF THE FAILURE TO BE CO-COLONY MICROBIOLOGICAL INFLUENCED CORROSION (MIC), CAUSED PREDOMINANTLY BY SULFATE REDUCING BACTERIA (SRB).

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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