SUNOCO PIPELINE L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorSUNOCO PIPELINE L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.61843, -94.96992

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

DURING A ROUTINE STATION CHECK ON 10/15/2015 EMPLOYEE DISCOVERED A RELEASE OF CRUDE OIL AT GOODRICH STATION. THE SOURCE OF THE RELEASE WAS DETERMINED TO BE INTERNAL CORROSION IN A THERMAL RELIEF LINE ON THE SUCTION SIDE OF THE PUMP MANIFOLD AREA WHICH WAS IMMEDIATELY ISOLATED. RESPONSE PERSONNEL WERE DISPATCHED TO THE AREA FOR CLEANUP ACTIVITIES. APPROXIMATELY TEN BARRELS WAS RELEASED IN THE MANIFOLD AREA. ON 10/19/2015 IT WAS DETERMINED THAT TOTAL COSTS WOULD EXCEED $50K AND AN NRC REPORT (1131203) WAS MADE. THE AFFECTED PIPING/FITTING WAS REMOVED AND REPLACED WITH NEW PIPING AND FITTINGS. TO AID IN PREVENTING A RECURRENCE OF THIS TYPE OF FAILURE ON THE THERMAL RELIEF PIPING THE PIPING NOW REMAINS EMPTY AND ISOLATED FROM STATION PRESSURE UNTIL ITS USE IS REQUIRED FOR MAINTENANCE ACTIVITIES. AFTER MAINTENANCE ACTIVITIES ARE COMPLETED THE THERMAL PIPING WILL BE EMPTIED AND ISOLATED FROM STATION PRESSURE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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