"ONEOK NGL PIPELINE, LLC"

hazardous_liquid Incident — — February 9, 2018

Incident Information

Incident DateFebruary 9, 2018
Operator"ONEOK NGL PIPELINE, LLC"
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates35.78150, -97.23780

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$410
Emergency Response$150
Other Costs$0

Location Map

Incident Narrative

"ON 2/9/18 A LAND OWNER NEAR THE ONEOK GOAT JUNCTION CALLED ONEOK PERSONNEL TO INFORM THEM SHE COULD SEE A SMALL VAPOR CLOUD INSIDE THE ONEOK FACILITY. UPON ARRIVAL, THE LOCAL AREA REPRESENTATIVE DISCOVERED PRODUCT VAPORS COMING FROM THE VALVE BODY OF A DRAIN VALVE INSTALLED ON THE SCRAPER TRAP BARREL. THE SCRAPER TRAP BARREL WAS ISOLATED AND DE-PRESSURED. THE 2"" BALON DRAIN VALVE WAS REMOVED FROM THE SCRAPER TRAP AND A BLIND FLANGE INSTALLED. THE SCRAPER TRAP WAS THEN RETURNED TO NORMAL OPERATIONS. ONEOK'S INVESTIGATION DETERMINED THE O-RING IN THE VALVE BODY HAD FAILED CAUSING THE RELEASE. THE O-RING HAS BEEN SENT TO A LAB TO DETERMINE THE CAUSE OF FAILURE. 3/16/2018 - UPDATED TIME OF ACCIDENT (A-4), VERIFIED LAT./LONG. PER REQUEST OF OCC. 7/05/2018 - UPDATED INVESTIGATION OF O-RING DETERMINED O-RING TO BE COMPATIBLE WITH PRODUCT IN PIPELINE. CAUSE OF FAILURE OF O-RING WAS INCONCLUSIVE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in