DCP MIDSTREAM

hazardous_liquid Incident — — May 7, 2018

Incident Information

Incident DateMay 7, 2018
OperatorDCP MIDSTREAM
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates31.22761, -101.62323

Cause

CauseEQUIPMENT FAILURE
SubcausePUMP OR PUMP-RELATED EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"BENEDUM STATION PUMP P310 3/4 INCH MANUAL BLOW DOWN GATE VALVE WAS DISCOVERED TO BE LEAKING BY TO VENT. THE VALVE WAS NOT SEATING PROPERLY, ALLOWING NGL TO LEAK BY THROUGH THE SYSTEM VENT, AS DESIGNED. THE 3/4 INCH VALVE IS LOCATED ON THE PUMP SKID AND IS USED FOR MANUAL BLOW DOWN OF STATION PUMP P310. THE TECHNICIAN WHO DISCOVERED THE LEAKING VALVE WAS ABLE TO GET THE VALVE TO HOLD BY WORKING THE VALVE AND EVENTUALLY GETTING IT TO SEAL OFF. THE CAUSE IS UNKNOWN, HOWEVER IT IS BELIEVED TO BE CAUSED BY TRASH FROM PREVIOUS MAINTENANCE ACTIVITY WHICH MAY HAVE LODGED IN THE GATE CAUSING THE VALVE NOT TO SEAL OFF COMPLETELY. DCP NGL TECH'S WILL ADD STATION VENT CHECK AFTER RETURN TO SERVICE FROM MAINTENANCE ACTIVITY HAS BEEN COMPLETED IN THE FUTURE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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