PLAINS PIPELINE, L.P.
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | PLAINS PIPELINE, L.P. |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 35.93878, -97.99486 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
APPROXIMATELY 740 BBLS OF CRUDE OIL WERE RELEASED AS A RESULT OF INTERNAL CORROSION. THE FAILED SEGMENT OF PIPE HAS BEEN SENT TO A LAB TO UNDERGO METALLURGICAL ANALYSIS; THEREFORE, A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE THE CAUSE IS CONFIRMED. THE NATIONAL RESPONSE CENTER (NRC) WAS NOTIFIED AND ASSIGNED INITIAL REPORT #1182539. A FOLLOW-UP CALL TO THE NRC, ASSIGNED REPORT #1182742. SUPPLEMENTAL NARRATIVE: THE RESULTS OF THE METALLURGICAL ANALYSIS INDICATE THE LEAK OCCURRED DUE TO INTERNAL CORROSION, ASSOCIATED WITH A PIT AND PRIMARILY DUE TO THE PRESENCES OF DISSOLVED CO2. THE MICROBIOLOGICAL DATA OBTAINED DID NOT SUPPORT MIC AS A CONTRIBUTING MECHANISM. THE LINE REMAINS PURGED AT THIS TIME.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.