PLAINS PIPELINE, L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorPLAINS PIPELINE, L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates35.93878, -97.99486

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

APPROXIMATELY 740 BBLS OF CRUDE OIL WERE RELEASED AS A RESULT OF INTERNAL CORROSION. THE FAILED SEGMENT OF PIPE HAS BEEN SENT TO A LAB TO UNDERGO METALLURGICAL ANALYSIS; THEREFORE, A SUPPLEMENTAL REPORT WILL BE SUBMITTED ONCE THE CAUSE IS CONFIRMED. THE NATIONAL RESPONSE CENTER (NRC) WAS NOTIFIED AND ASSIGNED INITIAL REPORT #1182539. A FOLLOW-UP CALL TO THE NRC, ASSIGNED REPORT #1182742. SUPPLEMENTAL NARRATIVE: THE RESULTS OF THE METALLURGICAL ANALYSIS INDICATE THE LEAK OCCURRED DUE TO INTERNAL CORROSION, ASSOCIATED WITH A PIT AND PRIMARILY DUE TO THE PRESENCES OF DISSOLVED CO2. THE MICROBIOLOGICAL DATA OBTAINED DID NOT SUPPORT MIC AS A CONTRIBUTING MECHANISM. THE LINE REMAINS PURGED AT THIS TIME.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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