COLONIAL PIPELINE CO
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | COLONIAL PIPELINE CO |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 30.71393, -91.27505 |
Cause
| Cause | EXCAVATION DAMAGE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 8/6/17, A CONTRACTOR CREW WAS PREFORMING SOIL REMEDIATION RELATED TO A SPILL THAT OCCURRED ON 8/4/17. AT APPROXIMATELY 10:45 CST, THEIR EXCAVATOR STRUCK A BURIED TUBING LINE NEAR THE LINE 01 CONTROL VALVE INSIDE BATON ROUGE STATION. STRIKING OF THE TUBING LINE BROKE THE NIPPLE BELOW THE SHUT-OFF VALVE ON THE TUBING VALVE-TREE AND RESULTED IN A RELEASE OF APPROXIMATELY 12.3 BBLS OF GASOLINE INSIDE THE ACCESS WELL. THE INSPECTOR IMMEDIATELY NOTIFIED OPERATIONS WHICH CONTACTED THE CONTROL CENTER AND ISOLATED AND BYPASSED THE STATION AT APPROXIMATELY 10:56. OPERATORS LOCKED-OUT AND DRAINED THE STATION PIPING WHICH STOPPED THE LEAK AT APPROXIMATELY 11:30. ALL RELEASED PRODUCT WAS CONTAINED ON COMPANY PROPERTY WITHIN THE ACCESS WELL. A VACUUM TRUCK THAT WAS STAGED NEARBY WAS IMMEDIATELY DEPLOYED TO THE ACCESS WELL WHERE THE PRODUCT WAS CONTAINED. THE PARISH LEPC AND STATE OF LA WERE EACH NOTIFIED. A TECHNICIAN WAS MOBILIZED WHO REPLACED THE DAMAGED TUBING SECTION AT APPROXIMATELY 14:15 AND BATON ROUGE STATION LN01 WAS RESTARTED AT APPROXIMATELY 14:35. PRODUCT RECOVERY AND CLEANUP ACTIVITIES WERE COMPLETED ON 8/6/17 BY 11:30. INITIAL INVESTIGATION INDICATED TUBING WAS STRUCK DUE TO FAILURE TO FOLLOW COLONIAL'S EXCAVATION PROCEDURE; DID NOT PROPERLY LOCATE/VERIFY DEPTH OF TUBING PRIOR TO EXCAVATION. EXCAVATOR OPERATOR, SPOTTER AND INSPECTOR OQS WERE SUSPENDED AS A RESULT. FINAL REPORT UPDATE: INCIDENT ANALYSIS WAS COMPLETED ON 1/24/18, CONFIRMING THE APPARENT CAUSE AND PROVIDED RECOMMENDATIONS RELATED TO LOCATING BURIED TUBING. REGARDING ZERO COMMODITY COSTS, THE RELEASED PRODUCT WAS RECOVERED FROM A PARTIALLY WATER FILLED ACCESS WELL, WAS NOT CONTAMINATED, AND THEREFORE RETURNED TO THE PIPELINE SYSTEM VIA TRANSMIX INJECTION.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.