KOCH PIPELINE COMPANY, L.P.

hazardous_liquid Incident — — August 15, 2017

Incident Information

Incident DateAugust 15, 2017
OperatorKOCH PIPELINE COMPANY, L.P.
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates30.05642, -93.84246

Cause

CauseEQUIPMENT FAILURE
SubcauseOTHER EQUIPMENT FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$21,000
Other Costs$0

Location Map

Incident Narrative

ON AUGUST 15, 2017, KOCH PIPELINE COMPANY'S CONTRACTOR, TDW, WAS PERFORMING A HOT TAP ON THE INV-ORANGE 4"" SEGMENT LINE IN ORANGE COUNTY, TEXAS. ONCE THE WELD WAS MADE ON THE TOR, KOCH PIPELINE THEN FOLLOWED THE PROCEDURE TO PRESSURE TEST THE WELD AND THE HOT TAP MACHINE. OPERATIONS PERSONNEL VERIFIED THAT THE PRESSURE HELD. TDW THEN TAPPED THE LINE. FOLLOWING THE TAP AND VERIFICATION OF PRESSURES, OPERATIONS PERSONNEL BLOCKED IN THE VALVE AND DE-PRESSURED THE TAPPING MACHINE. TDW THEN TOOK THE MACHINE OFF OF THE VALVE AND INSERTED THE PLUG TO PLUG TO TOR. ONCE TDW REINSTALLED THE MACHINE BACK TO THE VALVE, PERSONNEL TRIED TO OPEN THE VALVE TO THREAD THE PLUG IN. AT THIS POINT, PRODUCT BEGAN TO LEAK OUT OF THE STEM. THE LINE WAS THEN BLOCKED IN AND ISOLATED. PRESSURED DROPPED SUFFICIENTLY TO SAFELY THREAD THE PLUG IN, WHICH STOPPED THE PRODUCT FROM LEAKING. THE 2-INCH BALL VALVE WAS VISUALLY EXAMINED AND FOUND TO HAVE NO SIGNIFICANT EXTERNAL MECHANICAL OR CORROSION DAMAGE. THE VALVE WAS DISASSEMBLED AND THE INDIVIDUAL PARTS WERE VISUALLY EXAMINED, DOCUMENTED, AND COMPARED TO THE SPECIFIED MATERIALS OF THE MANUFACTURER'S PRODUCT CATALOG. A DISCREPANCY OBSERVED DURING DISASSEMBLY WAS THE ABSENCE OF A PACKING WASHER IN THE PACKING GLAND. ANALYSIS OF THE POLYMERIC COMPONENTS REVEALED DISCREPANCIES IN THE SPECIFIED MATERIALS OF THE STEM PACKING SEALS. AN ANALYSIS REPORT CONCLUDED THAT THE CAUSE OF THE PACKING LEAK WAS MOST LIKELY DUE TO THE COMBINATION OF 1) THE ABSENCE OF A PACKING WASHER IN THE PACKING GLAND, AND 2) THE PTFE MATERIAL USED FOR THE PACKING SEAL CONTAINED NO DETECTABLE REINFORCING MATERIAL VIA FTIR SPECTROSCOPY (FTIR - FOURIER TRANSFORM INFRARED). NO OTHER DISCERNABLE DAMAGE, WEAR, OR UNEVEN LOADING WAS OBSERVED IN THE VALVE COMPONENTS.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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