AMOCO OIL CO

hazardous_liquid Incident — — February 15, 2018

Incident Information

Incident DateFebruary 15, 2018
OperatorAMOCO OIL CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates41.75027, -86.11472

Cause

CauseEQUIPMENT FAILURE
SubcauseDEFECTIVE OR LOOSE TUBING OR FITTING

Casualties

Fatalities0
Injuries0

Costs

Property Damage$2,000
Emergency Response$15,500
Other Costs$0

Location Map

Incident Narrative

ON 2/15/18 AT 09:55 EST A BP TECHNICIAN WAS PERFORMING PUMP VIBRATION CHECKS ON THE SOUTH BEND STATION MAINLINE PUMPS AND DISCOVERED A SPRAY COMING OUT OF THE PUMP BEARING COOLING TUBING LINE ON PUMP #3. THE TECHNICIAN IMMEDIATELY CONTACTED THE TULSA CONTROL CENTER AND THE LINE WAS SHUT DOWN AND ISOLATED. THE SOURCE OF THE RELEASE WAS DETERMINED TO BE A TUBING FAILURE. THE TUBING WAS REMOVED AND SENT TO BE ANALYSED. THE PUMP WAS ISOLATED AND THE STATION WAS RESTARTED ON 2/15/18 AT 16:31 EST. THE RESULTS OF THE METALLURGICAL ANALYSIS INDICATED THAT THE CAUSE OF THE FAILURE WAS FATIGUE. THE CRACK LIKELY INITIATED AT THIS LOCATION BECAUSE THE END OF THE FITTING SERVED AS A STRESS CONCENTRATOR.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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