NUSTAR PIPELINE OPERATING PARTNERSHIP L.P.

hazardous_liquid Incident — — March 5, 2018

Incident Information

Incident DateMarch 5, 2018
OperatorNUSTAR PIPELINE OPERATING PARTNERSHIP L.P.
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates39.18809, -89.46314

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

WHILE ATTEMPTING TO BLOW DOWN THE STOPPLE TOWER, THE TDW TECHNICIAN OPENED THE 2 INCH BLOW DOWN VALVE. THE TECHNICIAN HEARD A LOUD POP AND AMMONIA WAS RELEASED FROM THE 2 INCH VALVE. AMMONIA VAPORS WERE RELEASED FOR APPROXIMATELY 25 MINUTES CREATING A LARGE VAPOR CLOUD. PIPELINE WAS SHUT DOWN AND MAINLINE VALVES WERE CLOSED AND PRESSURE WAS REDUCED AT THE STOPPLE SITE SO THE 2 INCH VALVE COULD BE CLOSED TO STOP THE RELEASE. APPROXIMATELY 248 LBS. OF AMMONIA WAS RELEASED. TDW'S INVESTIGATION DETERMINED THE WRONG O-RING WAS USED WHEN THE STOPPLE WAS INSTALLED CAUSING THE COMPLETION PLUG TO SEIZE UP NOT ALLOWING THE PLUG TO BE REMOVED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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