ROSE ROCK MIDSTREAM L.P.

hazardous_liquid Incident — — December 6, 2018

Incident Information

Incident DateDecember 6, 2018
OperatorROSE ROCK MIDSTREAM L.P.
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates36.01472, -96.75556

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$500
Emergency Response$24,915
Other Costs$0

Location Map

Incident Narrative

ON DECEMBER 6TH, 2018 AT APPROXIMATELY 3:05 PM CST, OIL THAT HAD LEAKED NEAR AND AROUND TANK 2535 WAS DISCOVERED. UPON FURTHER INVESTIGATION THE SOURCE OF THE CRUDE OIL LEAK WAS FROM THE SEAL ON THE NORTHWEST MIXER. THE CRUDE OIL HAD ACCUMULATED PRIMARILY ON THE WEST SIDE OF TANK 2535 AND HAD MIGRATED IN LOW LYING AREAS AROUND THE TANK TO THE NORTHEAST AND SOUTHWEST. APPROXIMATELY 28 BARRELS OF CRUDE OIL WAS RELEASED, THE VOLUME OF THE RELEASE WAS DETERMINED BY SCADA INFORMATION AND THE AMOUNT OF PRODUCT RECOVERED. COMPANY PERSONNEL WERE ABLE TO STOP THE RELEASE BY PLACING THE MIXER IN A MAINTENANCE MODE. EMERGENCY RESPONSE AND CLEAN UP EFFORTS WERE CONDUCTED BY COMPANY PERSONNEL AND CONTRACT PERSONNEL UNDER THE DIRECTION OF THE MAINTENANCE SUPERVISOR. AIR MONITORING WAS ON SITE CONTINUOUSLY THROUGHOUT THE CLEAN UP TO ENSURE BENZENE LEVELS WERE SAFE AND ALL READINGS WERE LESS THAN THE ACTION LEVEL. THE INITIAL CLEAN UP WAS CONCLUDED AT 10 PM CST ON DEC. 6TH. CLEAN UP EFFORTS TO RESTORE THE IMPACTED AREA WERE COMPLETED BY DEC. 11TH.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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