SUNOCO PIPELINE L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorSUNOCO PIPELINE L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates39.89399, -75.43151

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 11/11/19 AT APPROXIMATELY 17:11 THE CONTROL CENTER RECEIVED AN LEL ALARM AT THE GLEN RIDDLE JUNCTION STATION. THE ALARM WAS NOT CONTINUOUS, BUT RATHER ALARMED, CLEARED AND THEN ALARMED AGAIN. THE CONTROLLER CONTACTED FIELD OPERATIONS MANAGEMENT AT 17:17 TO RESPOND TO THE LEL ALARM CONDITION. LOCAL OPERATIONS PERSONNEL WERE DISPATCHED TO THE SITE TO INVESTIGATE. LOCAL FIELD OPERATIONS PERSONNEL ARRIVED ONSITE AT APPROXIMATELY 17:36 AND CONFIRMED A RELEASE OF GASOLINE. CONTROL CENTER WAS NOTIFIED OF CONFIRMED RELEASE AND AT 17:38 THE CONTROLLER SHUT DOWN THE INBOUND STREAM AND ISOLATED THE GLEN RIDDLE JUNCTION STATION. IT WAS LATER ESTIMATED THAT TOTAL COSTS WOULD EXCEED $50,000 AND NRC WAS NOTIFIED ON 11/11/19 AT 20:45 (REPORT 1263699). WHEN LEL LEVELS WERE SAFE FOR ENTRY INTO THE STATION THE SOURCE OF THE RELEASE WAS IDENTIFIED AT A VALVE BODY BLEED TUBING FITTING ON VALVE 8112. ALL FREE PRODUCT WAS RECOVERED AND WORK BEGAN TO REMOVE IMPACTED GRAVEL AND SOIL TO BE DISPOSED OF OFFSITE. THE FAILED TUBING AND FITTING WERE REPLACED AND THE STATION WAS RETURNED TO NORMAL OPERATION ON 11/11/19 AT 23:46. REQUIRED 48 HOUR NRC UPDATE WAS MADE ON 11/13/19 (REPORT 1263853). THE TUBING FITTING WAS PART OF THE VALVE AS PROVIDED BY THE MANUFACTURER. POST-INCIDENT EVALUATION BY THE TUBING VENDOR IDENTIFIED THAT THE TUBING FITTING HAD NOT BEEN ASSEMBLED CORRECTLY BY THE MANUFACTURER. THE TUBING WAS NOT INSERTED THROUGH THE FERRULE FAR ENOUGH WHICH DID NOT ALLOW THE FERRULE TO PROPERLY ENGAGE ON THE TUBING. ALL SIMILAR FITTINGS AND ASSEMBLIES IN THE STATION WERE CHECKED FOR SIMILAR ISSUE. SITE INVESTIGATION EFFORTS CONTINUE FOR REMEDIATION PURPOSES. SUPPLEMENTAL REPORT(S) WILL BE SUBMITTED AS REQUIRED. SUPPLEMENTAL/FINAL REPORT - SOIL CHARACTERIZATION AT THE SITE TO DATE HAS INDICATED NO ADDITIONAL VOLUME RELEASED NOR HAS ANY ADDITIONAL PRODUCT BEEN RECOVERED AND NONE IS ANTICIPATED MOVING FORWARD.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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