ENBRIDGE STORAGE (CUSHING) L.L.C.

hazardous_liquid Incident — — August 10, 2020

Incident Information

Incident DateAugust 10, 2020
OperatorENBRIDGE STORAGE (CUSHING) L.L.C.
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates35.93432, -96.75096

Cause

CauseCORROSION FAILURE
SubcauseINTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$160,000
Emergency Response$5,000
Other Costs$0

Location Map

Incident Narrative

ON AUGUST 10, 2020 AT APPROXIMATELY 11:30 AM CDT CRUDE OIL WAS DISCOVERED IN THE TANK BERM OF TANK 3013 BY FIELD PERSONNEL PERFORMING ROUTINE ROUNDS AT THE CUSHING TERMINAL. THE CUSHING CONTROL CENTER WAS CONTACTED AND THE AREA OF CONCERN WAS ISOLATED AND PIPELINE MAINTENANCE PERSONNEL BEGAN EXCAVATING TO INVESTIGATE THE SOURCE OF THE RELEASE. DUE TO STRONG WINDS AND LIGHTENING, THE EXCAVATION AND CLEANUP WORK WAS DELAYED. A CALL TO THE NRC WAS MADE ON AUGUST 11, 2020 AT 11:46 AM CDT (REPORT #1284289) ONCE THE SOURCE OF THE RELEASE WAS IDENTIFIED AS A PINHOLE IN THE RELIEF LINE TO TANK 3013 AND IT WAS DETERMINED THAT THE COSTS WOULD EXCEED THE NRC REPORTING THRESHOLD. THE 48-HOUR NRC NOTIFICATION WAS MADE ON AUGUST 13, 2020 AT 10:46 AM CDT (REPORT #1284450). AFTER FURTHER INVESTIGATION IT WAS DETERMINED THAT INTERNAL CORROSION CAUSED THE PINHOLE WHICH LED TO THE RELEASE OF TWO BARRELS OF CRUDE OIL. ADDITIONAL INTEGRITY ISSUES HAVE BEEN IDENTIFIED WITH THE TANK LINE AND IT IS CURRENTLY ISOLATED FROM ALL SOURCES OF PRODUCT UNTIL FINAL REPAIR DETERMINATION IS MADE. CONTAMINATED SOIL HAS BEEN CLEANED UP AND DISPOSED OF AT AN APPROVED SITE. ADDITIONAL SOIL REMEDIATION IS EXPECTED TO BE ONGOING.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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