KINDER MORGAN CRUDE AND CONDENSATE LLC

hazardous_liquid Incident — — November 23, 2020

Incident Information

Incident DateNovember 23, 2020
OperatorKINDER MORGAN CRUDE AND CONDENSATE LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates29.06510, -96.36023

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$100
Emergency Response$3,500
Other Costs$2,000

Location Map

Incident Narrative

(11/23/2020) AT APPROXIMATELY 0300 KMCC PERSONNEL WAS CALLED OUT TO INVESTIGATE A SUMP LEVEL ALARM AT OUR LOUISE METER STATION LOCATED AT 4754 CR 315, LOUISE TX, IN WHARTON COUNTY. WHEN THEY ARRIVED THEY OBSERVED STAINING ON PIPE AND GRAVEL MEASURING APPROXIMATELY 106'X45'. THERE WAS NO POOLING OF PRODUCT. IT WAS DETERMINED THAT A 1/4"" NIPPLE HAD FAILED FROM A PRV TEST PORT AND SPRAYED A MIST OF CRUDE CONDENSATE. OUR SPILL VOLUME ESTIMATE IS 13.3 GALLONS / .31 BBL. OF CRUDE CONDENSATE RELEASED. OUR OSRO RESPONDED AND CLEANED UP, AND THE FAILED COMPONENT WAS REPLACED AND HAS BEEN SENT OFF FOR METALLURGICAL ANALYSIS FOR CAUSE OF FAILURE. BECAUSE THE CAUSE OF THE RELEASE IS STILL UNDER INVESTIGATION THE APPARENT CAUSE WILL BE NOTED ON THE SUPPLEMENTAL AND FINAL 7000.1. 1/20/2021 - METALLURGICAL ANALYSIS HAS DETERMINED THE APPARENT CAUSE OF THE FAILURE TO BE EQUIPMENT FAILURE DUE TO A FATIGUE FRACTURE IN THE THREADS OF TEH FAILED 1/4"" PIPE NIPPLE. A CONTRIBUTING FACTOR TO THE FAILURE WAS A VALVE ATTACHED TO THE NIPPLE WITH NO SUPPORT.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in