SFPP, LP
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | SFPP, LP |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 33.23804, -115.50447 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 3/30/21 AT APPROXIMATELY 1424 PST, UNIT #2 ON THE NILAND TO IMPERIAL 6"" (LS58) ACHIEVED A HIGH AMP WARNING AT 70 AMPS BUT DID NOT REACH THE 75 AMP HIGH AMP SHUT-DOWN. OPERATIONS ACKNOWLEDGED THE WARNING AND S/D THE UNIT AT 1431. AT THE SAME TIME THE CONDITION OCCURRED, THE LOCAL LINE RIDER WAS AT THE FACILITY FOR A REGULAR SCHEDULED SITE INSPECTION. THE LINE RIDER RECOGNIZED THE ISSUE AND DETERMINED THERE WAS A RELEASE OF DIESEL AND CALLED THE FIELD CONTROLLER AND AREA MANAGER TO INSURE THE SYSTEM WAS SHUT-DOWN. THE OSRO WAS NOTIFIED IMMEDIATELY AND DISPATCHED TO THE FACILITY. THE RELEASE OCCURRED AS A RESULT OF A FAILED SWAGELOK ""T"" FITTING. UPDATE (7/14/21): THE TUBING DESIGN AND INSTALLATION WAS INADEQUATE FOR THE OPERATING CONDITIONS OF THE UNIT. THE TUBING DESIGN HAD AN UNNECESSARY RECIRCULATING LINE THAT ALLOWED THE ""T"" FITTING UPSTREAM OF THE ISOLATION VALVE TO BE UNDER CONSTANT PRESSURE AND FLOW. IF THE ISOLATION VALVE HAD BEEN INSTALLED UPSTREAM OF THE ""T"" FITTING, THE RELEASE WOULD HAVE BEEN PREVENTED.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.