WILLIAMS FIELD SERVICES - GULF COAST COMPANY, LP
hazardous_liquid Incident — — February 10, 2022
Incident Information
| Incident Date | February 10, 2022 |
| Operator | WILLIAMS FIELD SERVICES - GULF COAST COMPANY, LP |
| Commodity | HVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 29.75878, -94.91171 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | OTHER EQUIPMENT FAILURE |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $10,000 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
2/10/22 LOPC AT BTN1 WILLIAMS AND COVESTRO CONTROL CENTERS RESPOND TO GAS DETECTOR ALARMS AT 1:47 AM. COVESTRO PERSONAL REPORTED WHAT APPEARS TO BE A STEM LEAK ON MOV-0201. GAS DETECTOR READINGS SPIKED AT 120 PPM. WITH WATER SPRAY, READINGS DROPPED TO 16-18 PPM RANGE. AT 1:47AM, LINE PRESSURE WAS 351 UPSTREAM OF -0201, INLET TEMP WAS 54.29. DATA BEING GATHERED FOR LEAK CALCULATION. CONTROL CENTER CALLED TECHNICIANS TO RESPOND. BRYAN CALLED OPS SUPERVISOR AT 2:04 AM AT BTN1, SDV-0201 AND SDV-0205 HAVE BEEN CLOSED. AT BTN2 UPSTREAM, SDV-0201 WAS CLOSED. THE SOC HAS BEEN CALLED. TECHNICIANS ARE RESPONDING TO THE LOCATION. 4:10 AM TECHNICIANS HAVE MADE IT ON SITE. STARTED TO INJECT PACKING INTO THE VALVE STEM. 4:19 AM OPS SUPERVISOR RECEIVES CALL FROM EPA RESPONSE FOLKS ASKING IF THE LEAK HAD BEEN STOPPED. PROVIDED NRC#1328571AND CALL BACK # 866-372-7745 5:45 AM LEAK IS STOPPED WITH MOV-201 VALVE FULLY OPENED OR CLOSED. WAS NOT ABLE TO STOP THE LEAK WHEN THE VALVE IS IN TRANSIT. THE VALVE IS LOCKED OUT IN THE OPEN POSITION. 7:25 AM TEMP MOC BEING CREATED TO LEAVE MOV-0201 POWERED OFF AND USE BTN1-MOV-0205 AS THE VALVE TO BE CLOSED FOR A NORMAL SHUTDOWN OF THE PIPE. A THIRD PARTY CONTRACTOR WILL BE BROUGHT IN TO FLUSH STEM PACKING. 7:31 AM THE CONTROL CENTER HAS BEEN NOTIFIED THAT NORMAL FLOW CAN RESUME. 8:45 FOLLOW UP CALL FROM EPA RESPONSE FOLKS TO SEE IF LEAK WAS STOPPED? HOW IT WAS STOPPED? REPORTED AS STOPPED AT 5:45 AM. FROM PACKING INJECTION. 9:25 AM SENT ADDITIONAL INFORMATION TO DIVISION ENGINEER FOR LEAK CALCULATION. UPDATE: THE ROOT CAUSE WAS A STEM PACKING FAILURE DUE TO DRIED OUT PACKING. AS A MITIGATIVE RESPONSE, WE HAVE ESTABLISHED PM'S TO FLUSH THE PACKING AND PREVENT IT FROM DRYING OUT AGAIN.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.