QUESTAR PIPELINE COMPANY

gas_transmission Incident — — November 27, 2011

Incident Information

Incident DateNovember 27, 2011
OperatorQUESTAR PIPELINE COMPANY
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates41.49168, -110.27543

Cause

CauseEQUIPMENT FAILURE
SubcauseOTHER EQUIPMENT FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$500
Emergency Response$300
Other Costs$0

Location Map

Incident Narrative

SUPPLEMENTAL BEING FILED TO CLARIFY THE CAUSE OF THE INCIDENT. TUBING FOR A SENSING LINE TO A PRESSURE TRANSDUCER WAS INADEQUATELY SECURED DURING INITIAL INSTALLATION AND BROKE FREE FROM ITS CONNECTION POINT BECAUSE OF PROLONGED VIBRATION FROM NORMAL OPERATION. LOCAL OPERATOR RESPONDED AND ISOLATED THE SENSING LINE VALVES. THE OPERATOR REPAIRED THE TUBING AND REPORTED THE EVENT TO QUESTAR PIPELINE COMPANY'S GAS CONTROL. AFTER GAS LOSS CALCULATIONS WERE MADE IT WAS DETERMINED THAT THIS EVENT MET THE CRITERIA OF AN UNINTENTIONAL RELEASE OF GAS IN EXCESS OF 3 MMSCF AND THE EVENT WAS REPORTED TO THE NRC.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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