ROCKIES EXPRESS PIPELINE LLC

gas_transmission Incident — — September 12, 2025

Incident Information

Incident DateSeptember 12, 2025
OperatorROCKIES EXPRESS PIPELINE LLC
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates39.92978, -81.25021

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$220
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

"AT 16:31 ON 9/12/2025 PSV-5201, A DISCHARGE OVER-PRESSURE RELIEF VALVE ON UNIT 5200 AT SENECA COMPRESSOR STATION BEGAN TO VENT GAS BELOW THE DESIRED ACTIVATION SETPOINT. THIS ACTIVATION WAS DUE TO A PIPE NIPPLE FAILURE ON THE FIELD TEST PORT. THE SCADA SYSTEM ALERTED OCC AND THE MECHANIC ON CALL FOR THE STATION WHEN IT DETECTED HI GAS LEVELS IN THE COMPRESSOR BUILDING. THE MECHANIC ON CALL RECEIVED THE ALARMS AND BEGAN DRIVING TO SENECA STATION. WHILE THE MECHANIC WAS ON THE WAY THE OPERATIONS TEAM ASKED OCC TO ISSUE A REMOTE STOP COMMAND TO THE TWO UNITS RUNNING AT THE STATION, UNIT 5100 AND 5200. THIS COMMAND STOPPED THE UNIT AND COMMANDED THE SUCTION AND DISCHARGE VALVES CLOSED, STOPPING THE FLOW OF GAS TO THE PSV. WHEN THE MECHANIC ARRIVED ON SITE, HE DISCOVERED THE BROKEN PIPE NIPPLE AND REMOVED THE ASSEMBLY AND REPLACED IT WITH A PLUG. THE UNIT WAS THEN CHECKED AND MADE AVAILABLE FOR SERVICE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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