Showing 1,744 complaints for WINNEBAGO
DRIVER SIDE FRONT TIRE SEPARATED AT 55 MPH. 100 MILES LATER, THE DRIVERS SIDE REAR TIRES SEPARATED AT 55 MPH. *AK
Incident date: Jan 1, 1901
WHILE DRIVING VEHICLE STALLED DUE TO A MALFUNCTION IN THE IGNITION SWITCH WIRING. VEHICLE WAS TAKEN TO THE DEALER, WHO FOUND DETERMINED THAT IGNITION SWITCH WIRES MELTED. IGNITION SWITCH WAS REPLACED THREE TIMES. *AK AUTO PARK SYSTEM FAILED MULTIPLE TIMES. ALSO, SPARK PLUG WIRES BURNED UP. IT WAS ASSUMED THAT THERE WAS A FAULT IN THE FUEL PUMP, BUT VEHICLE STILL MALFUNCTIONED AFTER THE RE
... PLACEMENT OF THE FUEL PUMP. WHEN AIR CONDITIONER IS ON, ENGINE TEMPERATURE ROSE AROUND 210 DEGREES FAHRENHEIT, DEALER CHECKED VEHICLE AND FOUND THAT THERMOSTAT NEEDS TO BE REPLACED. INSTALLED NEW THERMOSTAT. VEHICLE WAS RUNNING ROUGH WHEN BEING DRIVEN UPHILL. UPON INSPECTION, IT WAS FOUND THAT SPARK PLUGS WHERE WORN OUT. DEALER REPLACED SPARK PLUGS AND IGNITION WIRES. *LARead more
Incident date: Jan 1, 1901
WHILE DRIVING VEHICLE STALLED DUE TO A MALFUNCTION IN THE IGNITION SWITCH WIRING. VEHICLE WAS TAKEN TO THE DEALER, WHO FOUND DETERMINED THAT IGNITION SWITCH WIRES MELTED. IGNITION SWITCH WAS REPLACED THREE TIMES. *AK AUTO PARK SYSTEM FAILED MULTIPLE TIMES. ALSO, SPARK PLUG WIRES BURNED UP. IT WAS ASSUMED THAT THERE WAS A FAULT IN THE FUEL PUMP, BUT VEHICLE STILL MALFUNCTIONED AFTER THE RE
... PLACEMENT OF THE FUEL PUMP. WHEN AIR CONDITIONER IS ON, ENGINE TEMPERATURE ROSE AROUND 210 DEGREES FAHRENHEIT, DEALER CHECKED VEHICLE AND FOUND THAT THERMOSTAT NEEDS TO BE REPLACED. INSTALLED NEW THERMOSTAT. VEHICLE WAS RUNNING ROUGH WHEN BEING DRIVEN UPHILL. UPON INSPECTION, IT WAS FOUND THAT SPARK PLUGS WHERE WORN OUT. DEALER REPLACED SPARK PLUGS AND IGNITION WIRES. *LARead more
Incident date: Jan 1, 1901
WHILE DRIVING VEHICLE STALLED DUE TO A MALFUNCTION IN THE IGNITION SWITCH WIRING. VEHICLE WAS TAKEN TO THE DEALER, WHO FOUND DETERMINED THAT IGNITION SWITCH WIRES MELTED. IGNITION SWITCH WAS REPLACED THREE TIMES. *AK AUTO PARK SYSTEM FAILED MULTIPLE TIMES. ALSO, SPARK PLUG WIRES BURNED UP. IT WAS ASSUMED THAT THERE WAS A FAULT IN THE FUEL PUMP, BUT VEHICLE STILL MALFUNCTIONED AFTER THE RE
... PLACEMENT OF THE FUEL PUMP. WHEN AIR CONDITIONER IS ON, ENGINE TEMPERATURE ROSE AROUND 210 DEGREES FAHRENHEIT, DEALER CHECKED VEHICLE AND FOUND THAT THERMOSTAT NEEDS TO BE REPLACED. INSTALLED NEW THERMOSTAT. VEHICLE WAS RUNNING ROUGH WHEN BEING DRIVEN UPHILL. UPON INSPECTION, IT WAS FOUND THAT SPARK PLUGS WHERE WORN OUT. DEALER REPLACED SPARK PLUGS AND IGNITION WIRES. *LARead more
Incident date: Jan 1, 1901
WHILE DRIVING VEHICLE STALLED DUE TO A MALFUNCTION IN THE IGNITION SWITCH WIRING. VEHICLE WAS TAKEN TO THE DEALER, WHO FOUND DETERMINED THAT IGNITION SWITCH WIRES MELTED. IGNITION SWITCH WAS REPLACED THREE TIMES. *AK AUTO PARK SYSTEM FAILED MULTIPLE TIMES. ALSO, SPARK PLUG WIRES BURNED UP. IT WAS ASSUMED THAT THERE WAS A FAULT IN THE FUEL PUMP, BUT VEHICLE STILL MALFUNCTIONED AFTER THE RE
... PLACEMENT OF THE FUEL PUMP. WHEN AIR CONDITIONER IS ON, ENGINE TEMPERATURE ROSE AROUND 210 DEGREES FAHRENHEIT, DEALER CHECKED VEHICLE AND FOUND THAT THERMOSTAT NEEDS TO BE REPLACED. INSTALLED NEW THERMOSTAT. VEHICLE WAS RUNNING ROUGH WHEN BEING DRIVEN UPHILL. UPON INSPECTION, IT WAS FOUND THAT SPARK PLUGS WHERE WORN OUT. DEALER REPLACED SPARK PLUGS AND IGNITION WIRES. *LARead more
Incident date: Mar 7, 2004
RECALL NOT ACCOMPLISHED BY SAMSUNG OF AMERICA ON MICROWAVE MODEL MR6699GB I HAD TO REPLACE THE MICROWAVE AT MY OWN COST SAMSUNG MHAS NOT REINBURSED ME FOR THIS ACTION. I HAVE A LETTER STATING THAT I WOULD BE REINBURSED IN JANUARY.*AK
Incident date: Jul 27, 2003
WE HAVE A 1997 MINNIE WINNIE MOTORHOME WITH FIRESTONE STEELTEX RADIAL TIRES R4S LT225/75R16 M/S. ONE OF THE REAR DUALLY TIRES BLEW ON A TRIP WITH LESS THAN 18,000 MILES. WE REPLACED THE TIRE AND DIDN'T THINK MUCH ABOUT IT UNTIL WE TOOK ANOTHER TRIP AND ONE OF THE DUALLY TIRES ON THE OTHER SIDE BLEW OUT CAUSING SOME DAMAGE. I DO HAVE PICTURES OF THE SECOND BLOWOUT, NOT SURE ON THE FIRST. WE WER
... E NOT ON THE ROAD LONG WHEN THE SECOND BLOWOUT OCCURED AND HAD INSPECTED, AND CHECKED THE PRESSURE BEFORE OUR DEPARTURE. NOW THE FRONT TIRES ON THE VEHICLEHAVE AREAS IN MID SECTION OF THE TIRES WHERE THERE ARE DIPS. A FIRESTONE REPRESENTATIVE TOLD US IT LOOKS LIKE "CUPPING" AND PROBABLY CAUSED FROM BEING OUT OF BALANCE. A GOODYEAR TIRE DEALER TOLD US THE TREAD IS SEPARATING FROM THE BELT. WE FEEL ALL THE TIRES ON THE VEHICLE ARE DEFECTIVE. IT IS NOT SAFE TO DRIVE! WE ARE LUCKY THE FRONT DID NOT BLOW OR PROBABLY WOULD HAVE FATALITIES INVOLVED. WE WILL SUBMIT WHAT IS LEFT OF THE SECOND TIRE TO FIRESTONE AT OUR OWN EXPENSE FOR THEIR REVIEW OF OUR CLAIM. THEY CERTAINLY DON'T MAKE IT EASY. (THE FIRST BLOWOUT WAS LEFT WITH THE DEALER WE PURCHASED REPLACEMENT TIRE FROM. *AKRead more
Incident date: Feb 25, 2004
CONSUMER RECEIVED MANUFACTURER'S RECALL LETTER MR6699GB CONCERNING SAMSUM MICROWAVE IN NOVEMBER 2003. WALCO LOCAL INDEPENDENT SHOP REPLACED THE PART ON RECALL, AND IT FAILED. CONSUMER BOUGHT A NEW MICROWAVE, AND NO BODY WANTED TO BE RESPONSIBLE FOR REFUNDING THE MONEY. *AK
Incident date: Nov 7, 2003
STEAL BELT/TREAD CAME FLYING OFF THE VEHICLE AT 70 MPH. TIRE WAS A DUALLY ON THE OUTSIDE RIGHT REAR. IN JULY, INSIDE REAR, AND 1 YEAR AGO, INSIDE LEFT REAR CAME OFF. *AK *MR
Incident date: Jun 17, 2003
WHILE DRIVING OVER 50 MPH VEHICLE SWERVED AND BOUNCED ALL OVER THE HIGHWAY. DEALER EXAMINED THE VEHICLE, AND CLAIMED THAT THE VEHICLE WAS HANDLING NORMALLY. *AK
Incident date: Apr 15, 2002
WHEN DRIVING IN THE RAIN VEHICLE STALLED, CAUSING THE DRIVER TO PULL OFF THE ROAD. *AK
Incident date: Jan 16, 2004
THE CONSUMER RECEIVED THE WRONG PART FOR HIS SAMSUNG MICROWAVE. THE CONSUMER CALLED THE MANUFACTURER AND EXPLAINED THE MISTAKE. THE MANUFACTURER INDICATED THAT THEY DID NOT HAVE THE CORRECT PART AT THIS MOMENT AND WERE NOT SURE WHEN IT WOULD BE AVAILABLE. *NM
Incident date: Sep 12, 2003
PROPANE FURNACE IN BRAND NEW RV QUITS WORKING WHENEVER THE TEMPERATURE DROPS BELOW 50 DEGREES FAHRENHEIT OR SO, ENDANGERING THE OCCUPANTS SLEEPING IN THE VEHICLE. THE PROPANE ALARM GOES OFF FREQUENTLY INDICATING PROPANE IN THE VEHICLE. DEALER, NOR MANUFACTURER WILL REPAIR THE PROBLEM, DESPITE 6 VISITS. *LA
Incident date: Nov 10, 2003
ON A NYS INSPECTION AND TIRE ROTATIO THE FRONT RIGHT TIRE SIDEWALL WAS CRACKED AND SPLIT AROUND THE CIRCUMFERENCE,BUT DID NOT BLOW. *AK
Incident date: Oct 13, 2003
THE VEHICLE EXPERIENCED A BLOW OUT OF THE LEFT REAR DUAL TIRE.*MR FLYING TIRE DEBRIS CAUSED DAMAGE TO THE VEHICLE AS IT PULLED TO THE SIDE OF THE ROAD. *PH *NM
Incident date: May 21, 2003
REF: 10042704. NVS 216 GMH. NEW MOTOR HOME WITH NUMEROUS SAFETY ISSUES. THE FOLLOWING ITEMS HAVE NOT BEEN FIXED: ALIGNMENT, TRAVEL DIRECTION (TRACKS TO THE RIGHT WHEN GOING DOWN THE ROAD), BANGING IN THE FRONT END, ELECTRONIC PROBLEMS IN DASH, TAIL PIPE INSTALLED INCORRECTLY, EASY CHAIR THAT CONTINUOUSLY ROCKS AND IS DISTRACTING. THE FOLLOWING ITEMS HAVE BEEN REPAIRED: HOLE IN DUST CAP ON LE
... FT FRONT WHEEL, WATER IN LEFT FRONT HEAD LIGHT, SOUND ON BACK UP MONITOR, FLORESCENT LIGHT COVERS FALLING OFF, BROKEN CUPBOARD LATCH, GAS LEAK ON GENERATOR, RUSTY LP GAS LINES, AND CLAMPS BROKEN ON LP GAS LINES. I HAVE BEEN TRYING FOR MONTHS TO GET A "NEW" MOTOR HOME PROPERLY REPAIRED. SOME OF THE ITEMS ARE APPEARANCE RELATED BUT MOST OF THEM ARE SAFETY ISSUES. I WILL ENCLOSE COPIES OF FILES THAT INCLUDE LISTS OF ISSUES AND SOME THINGS THAT HAVE BEEN DONE TO ATTEMPT REPAIRS. I BELIEVE THIS MOTOR HOME SHOULD NOT BE USED FOR LONG DISTANCE TRAVEL UNTIL PROPERLY REPAIRED. MY FAMILY AND FRIENDS FEEL I WAS TAKEN ADVANTAGE OF. FOR ME TO GET OUT OF THIS SITUATION, I WILL HAVE TO SELL OR TRADE TO ANOTHER UNSUSPECTING CONSUMER JUST AS HAPPENED TO ME. IF THIS HAD BEEN A USED MOTOR HOME, I WOULD HAVE THOUGHT IT HAD BEEN IN AN ACCIDENT. THE STRESS TO MY FAMILY AND ME AND THE DISAPPOINTMENT EXPERIENCED BY US AND OUR GRANDCHILDREN ARE INDESCRIBABLE. WE PLANNED ON TRAVELING TO THE SOUTH THIS WINTER BUT HAVE DECIDED NOT TO CHANCE THE TRAVEL WITH THIS MOTOR HOME.*AKRead more
Incident date: May 21, 2003
REF: 10042704. NVS 216 GMH. NEW MOTOR HOME WITH NUMEROUS SAFETY ISSUES. THE FOLLOWING ITEMS HAVE NOT BEEN FIXED: ALIGNMENT, TRAVEL DIRECTION (TRACKS TO THE RIGHT WHEN GOING DOWN THE ROAD), BANGING IN THE FRONT END, ELECTRONIC PROBLEMS IN DASH, TAIL PIPE INSTALLED INCORRECTLY, EASY CHAIR THAT CONTINUOUSLY ROCKS AND IS DISTRACTING. THE FOLLOWING ITEMS HAVE BEEN REPAIRED: HOLE IN DUST CAP ON LE
... FT FRONT WHEEL, WATER IN LEFT FRONT HEAD LIGHT, SOUND ON BACK UP MONITOR, FLORESCENT LIGHT COVERS FALLING OFF, BROKEN CUPBOARD LATCH, GAS LEAK ON GENERATOR, RUSTY LP GAS LINES, AND CLAMPS BROKEN ON LP GAS LINES. I HAVE BEEN TRYING FOR MONTHS TO GET A "NEW" MOTOR HOME PROPERLY REPAIRED. SOME OF THE ITEMS ARE APPEARANCE RELATED BUT MOST OF THEM ARE SAFETY ISSUES. I WILL ENCLOSE COPIES OF FILES THAT INCLUDE LISTS OF ISSUES AND SOME THINGS THAT HAVE BEEN DONE TO ATTEMPT REPAIRS. I BELIEVE THIS MOTOR HOME SHOULD NOT BE USED FOR LONG DISTANCE TRAVEL UNTIL PROPERLY REPAIRED. MY FAMILY AND FRIENDS FEEL I WAS TAKEN ADVANTAGE OF. FOR ME TO GET OUT OF THIS SITUATION, I WILL HAVE TO SELL OR TRADE TO ANOTHER UNSUSPECTING CONSUMER JUST AS HAPPENED TO ME. IF THIS HAD BEEN A USED MOTOR HOME, I WOULD HAVE THOUGHT IT HAD BEEN IN AN ACCIDENT. THE STRESS TO MY FAMILY AND ME AND THE DISAPPOINTMENT EXPERIENCED BY US AND OUR GRANDCHILDREN ARE INDESCRIBABLE. WE PLANNED ON TRAVELING TO THE SOUTH THIS WINTER BUT HAVE DECIDED NOT TO CHANCE THE TRAVEL WITH THIS MOTOR HOME.*AKRead more
Incident date: May 21, 2003
REF: 10042704. NVS 216 GMH. NEW MOTOR HOME WITH NUMEROUS SAFETY ISSUES. THE FOLLOWING ITEMS HAVE NOT BEEN FIXED: ALIGNMENT, TRAVEL DIRECTION (TRACKS TO THE RIGHT WHEN GOING DOWN THE ROAD), BANGING IN THE FRONT END, ELECTRONIC PROBLEMS IN DASH, TAIL PIPE INSTALLED INCORRECTLY, EASY CHAIR THAT CONTINUOUSLY ROCKS AND IS DISTRACTING. THE FOLLOWING ITEMS HAVE BEEN REPAIRED: HOLE IN DUST CAP ON LE
... FT FRONT WHEEL, WATER IN LEFT FRONT HEAD LIGHT, SOUND ON BACK UP MONITOR, FLORESCENT LIGHT COVERS FALLING OFF, BROKEN CUPBOARD LATCH, GAS LEAK ON GENERATOR, RUSTY LP GAS LINES, AND CLAMPS BROKEN ON LP GAS LINES. I HAVE BEEN TRYING FOR MONTHS TO GET A "NEW" MOTOR HOME PROPERLY REPAIRED. SOME OF THE ITEMS ARE APPEARANCE RELATED BUT MOST OF THEM ARE SAFETY ISSUES. I WILL ENCLOSE COPIES OF FILES THAT INCLUDE LISTS OF ISSUES AND SOME THINGS THAT HAVE BEEN DONE TO ATTEMPT REPAIRS. I BELIEVE THIS MOTOR HOME SHOULD NOT BE USED FOR LONG DISTANCE TRAVEL UNTIL PROPERLY REPAIRED. MY FAMILY AND FRIENDS FEEL I WAS TAKEN ADVANTAGE OF. FOR ME TO GET OUT OF THIS SITUATION, I WILL HAVE TO SELL OR TRADE TO ANOTHER UNSUSPECTING CONSUMER JUST AS HAPPENED TO ME. IF THIS HAD BEEN A USED MOTOR HOME, I WOULD HAVE THOUGHT IT HAD BEEN IN AN ACCIDENT. THE STRESS TO MY FAMILY AND ME AND THE DISAPPOINTMENT EXPERIENCED BY US AND OUR GRANDCHILDREN ARE INDESCRIBABLE. WE PLANNED ON TRAVELING TO THE SOUTH THIS WINTER BUT HAVE DECIDED NOT TO CHANCE THE TRAVEL WITH THIS MOTOR HOME.*AKRead more
Incident date: May 21, 2003
REF: 10042704. NVS 216 GMH. NEW MOTOR HOME WITH NUMEROUS SAFETY ISSUES. THE FOLLOWING ITEMS HAVE NOT BEEN FIXED: ALIGNMENT, TRAVEL DIRECTION (TRACKS TO THE RIGHT WHEN GOING DOWN THE ROAD), BANGING IN THE FRONT END, ELECTRONIC PROBLEMS IN DASH, TAIL PIPE INSTALLED INCORRECTLY, EASY CHAIR THAT CONTINUOUSLY ROCKS AND IS DISTRACTING. THE FOLLOWING ITEMS HAVE BEEN REPAIRED: HOLE IN DUST CAP ON LE
... FT FRONT WHEEL, WATER IN LEFT FRONT HEAD LIGHT, SOUND ON BACK UP MONITOR, FLORESCENT LIGHT COVERS FALLING OFF, BROKEN CUPBOARD LATCH, GAS LEAK ON GENERATOR, RUSTY LP GAS LINES, AND CLAMPS BROKEN ON LP GAS LINES. I HAVE BEEN TRYING FOR MONTHS TO GET A "NEW" MOTOR HOME PROPERLY REPAIRED. SOME OF THE ITEMS ARE APPEARANCE RELATED BUT MOST OF THEM ARE SAFETY ISSUES. I WILL ENCLOSE COPIES OF FILES THAT INCLUDE LISTS OF ISSUES AND SOME THINGS THAT HAVE BEEN DONE TO ATTEMPT REPAIRS. I BELIEVE THIS MOTOR HOME SHOULD NOT BE USED FOR LONG DISTANCE TRAVEL UNTIL PROPERLY REPAIRED. MY FAMILY AND FRIENDS FEEL I WAS TAKEN ADVANTAGE OF. FOR ME TO GET OUT OF THIS SITUATION, I WILL HAVE TO SELL OR TRADE TO ANOTHER UNSUSPECTING CONSUMER JUST AS HAPPENED TO ME. IF THIS HAD BEEN A USED MOTOR HOME, I WOULD HAVE THOUGHT IT HAD BEEN IN AN ACCIDENT. THE STRESS TO MY FAMILY AND ME AND THE DISAPPOINTMENT EXPERIENCED BY US AND OUR GRANDCHILDREN ARE INDESCRIBABLE. WE PLANNED ON TRAVELING TO THE SOUTH THIS WINTER BUT HAVE DECIDED NOT TO CHANCE THE TRAVEL WITH THIS MOTOR HOME.*AKRead more
Incident date: May 21, 2003
REF: 10042704. NVS 216 GMH. NEW MOTOR HOME WITH NUMEROUS SAFETY ISSUES. THE FOLLOWING ITEMS HAVE NOT BEEN FIXED: ALIGNMENT, TRAVEL DIRECTION (TRACKS TO THE RIGHT WHEN GOING DOWN THE ROAD), BANGING IN THE FRONT END, ELECTRONIC PROBLEMS IN DASH, TAIL PIPE INSTALLED INCORRECTLY, EASY CHAIR THAT CONTINUOUSLY ROCKS AND IS DISTRACTING. THE FOLLOWING ITEMS HAVE BEEN REPAIRED: HOLE IN DUST CAP ON LE
... FT FRONT WHEEL, WATER IN LEFT FRONT HEAD LIGHT, SOUND ON BACK UP MONITOR, FLORESCENT LIGHT COVERS FALLING OFF, BROKEN CUPBOARD LATCH, GAS LEAK ON GENERATOR, RUSTY LP GAS LINES, AND CLAMPS BROKEN ON LP GAS LINES. I HAVE BEEN TRYING FOR MONTHS TO GET A "NEW" MOTOR HOME PROPERLY REPAIRED. SOME OF THE ITEMS ARE APPEARANCE RELATED BUT MOST OF THEM ARE SAFETY ISSUES. I WILL ENCLOSE COPIES OF FILES THAT INCLUDE LISTS OF ISSUES AND SOME THINGS THAT HAVE BEEN DONE TO ATTEMPT REPAIRS. I BELIEVE THIS MOTOR HOME SHOULD NOT BE USED FOR LONG DISTANCE TRAVEL UNTIL PROPERLY REPAIRED. MY FAMILY AND FRIENDS FEEL I WAS TAKEN ADVANTAGE OF. FOR ME TO GET OUT OF THIS SITUATION, I WILL HAVE TO SELL OR TRADE TO ANOTHER UNSUSPECTING CONSUMER JUST AS HAPPENED TO ME. IF THIS HAD BEEN A USED MOTOR HOME, I WOULD HAVE THOUGHT IT HAD BEEN IN AN ACCIDENT. THE STRESS TO MY FAMILY AND ME AND THE DISAPPOINTMENT EXPERIENCED BY US AND OUR GRANDCHILDREN ARE INDESCRIBABLE. WE PLANNED ON TRAVELING TO THE SOUTH THIS WINTER BUT HAVE DECIDED NOT TO CHANCE THE TRAVEL WITH THIS MOTOR HOME.*AKRead more
CONSUMER STATED MICROWAVE TURNED ON AND OFF BY ITSELF. THE DEALER'S AGREED TO PAY FOR HALF OF THE WORK THAT NEEDED TO BE DONE. *AK
Incident date: Dec 3, 2003
WHILE DRIVING 45 MPH STEERING WHEEL VIBRATED UNCONTROLLABLY. DRIVER WAS ABLE TO DRIVE THE MOTORHOME TO A DEALER FOR ANALYSIS, BUT THE MECHANIC WAS NOT ABLE TO RESOLVE THE PROBLEM. *AK
Incident date: Nov 20, 2003
ON MY 1996 WINNEBAGO MOTOR HOME (34 FEET) (16,000 GVW) I LOST THE "SERPENTINE FAN BELT" WHILE TRAVELING AT 65 MPH ON INTERSTATE 81 IN VIRGINIA. THIS CAUSED A LOSS OF MY POWER STEERING , AND I LOST MY POWER BRAKES! IT WAS A LITTLE DIFFICULT TO STEER THE VEHICLE BUT IT WAS VIRTUALLY IMPOSSIBLE TO STOP THE VEHICLE. I AM OVER 6 FEET TALL AND WEIGH MORE THAN 200 POUNDS BUT NO MATTER HOW HARD I PUS
... HED ON THE BRAKE PEDAL IT STILL TOOK OVER 500 FEET TO FINALLY STOP. THERE WERE NO INJURIES, NO DAMAGES. *LARead more
Incident date: Nov 20, 2003
WHILE DRIVING 65 MPH, THE VEHICLE'S FAN BELT FAILED. THIS CAUSED THE POWER STEERING AND POWER BRAKES TO BECOME INOPERATIVE. PLEASE PROVIDE ADDITIONAL INFORMATION. *JB
CONSUMER RECEIVED RECALL 03E044000 SUBJECT: MICROWAVE OVENS/CIRCUIT SHORT. THE CONSUMER DID NOT LIKE THAT THE MANUFACTURER OF THE MICROWAVE WAS SENDING THE REPLACEMENT PARTS TO THE INDIVIDUAL CONSUMERS AND MAKING THEM RESPONSIBLE FOR FINDING A DEALER TO INSTALL THE PARTS. ALSO, CONSUMER WAS DISPLEASED WITH THE PHONE NUMBER PROVIDED TO GET INFORMATION ABOUT THIS RECALL.*AK
WHILE DRIVING VEHICLE IS UNSTABLE AND WANDERS IN BOTH DIRECTIONS. *AK THE CONSUMER'S PERSONAL MECHANIC TRIED EVERYTHING FROM CHANGING THE TIRE PRESSURE TO HAVING THE FRONT ALIGNED AND WEIGHTED TO NO AVAIL. *PH
Incident date: Nov 7, 2003
WHILE DRIVING 70 MPH TREAD SEPARATED ON THE OUTSIDE DUAL TIRE ON THE DRIVER'S SIDE. *AK
Incident date: Nov 9, 2003
THERE IS AN EXTREME AMOUNT OF VIBRATION THAT CAUSES THE DASHBOARD TO BOUNCE ENOUGH TO MAKE IT HARD TO READ THE GAUGES. THIS VIBRATION IS FELT IN THE STEERING WHEEL AS WELL AS THE FLOOR. THE VIBRATION IS VERY FATIGUING ON OUR HANDS. *AK ALSO THE UNIT HAS A LOT OF BACK AND FORTH SWAY IN TURNS AND PASSING OTHER TRUCKS AND CARS. OUR COMMENTS-LET'S TAKE IT FROM THE TOP. FIRST OF ALL, WE HAVE HE
... ARD MANY OF YOUR COMPLAINTS FROM OTHER OWNERS OF THE WINNEBAGO SIGHTSEER, SO THIS IS NOT THE FIRST TIME WE HAVE BEEN DOWN THIS ROAD. THE MOST COMMON COMPLAINT REGARDING THIS MODEL IS POOR HANDLING IN THE WIND AND WE WOULD SUGGEST BOTH SWAY BAR AND SHOCK UPGRADES. THAT WILL TAME SOME OF THE WANDER. YOU ALSO WILL WANT TO GET YOUR COACH WEIGHED TO BE SURE THAT YOU HAVE ENOUGH WEIGHT ON THE FRONT AXLE. REMEMBER, 1/3 OF THE GW ON THE FRONT AXLE, 2/3S ON THE BACK AXLE. OKAY, NOW ONTO THE VIBRATION. BALANCING AND ALIGNMENT DO NO GOOD IF THE WHEELS ARE OUT OF ROUND, AN ONGOING PROBLEM WITH THE FORD CHASSIS, OR ALSO A POSSIBILITY, THE TIRES ARE OUT OF ROUND. SOMEONE NEEDS TO CHECK THE RUN-OUT ON THE TIRES. FOR THE RECORD, WE HAVE DRIVEN THE FORD CHASSIS SEVERAL TIMES IN TYPE AS AND VIBRATION IS NOT NORMALLY PART OF THE MENU. YOUR CD PLAYER IS ALMOST SURELY SKIPPING DUE TO VIBRATION, IF IT IS AS BAD AS YOU DESCRIBE. UNLESS YOUR DEALER IS A CERTIFIED FORD SERVICE CENTER, WE WOULD TRY WORKING WITH A FORD DEALER THAT ROUTINELY DEALS WITH MOTORHOMES. SOME NOISE FROM THE POWER STEERING PUMP MAY BE NORMAL. IT DEPENDS ON HOW MUCH. ARE YOU HAVING ANY PROBLEM WITH IT? AGAIN, WHY NOT HAVE FORD CHECK IT RATHER THAN YOU DEALER? AS A FINAL NOTE, YOUR CHASSIS IS WARRANTED BY FORD, WHY DO YOU CARE WHAT YOUR DEALER WANTS? IF THEY CAN'T FIX IT, GET TO SOMEONE THAT CAN!! VIBRATION OF THIS MAGNITUDE MAY BE DANGEROUS. FILE A REPORT WITH THE NATIONAL HIGHWAY SAFETY ADMINISTRATION. THANKS FOR WRITING THE STAFF @ MRORead more
Incident date: Nov 1, 2003
I HAVE A 1995 WINNEBAGO CLASS A MOTORHOME WITH A P-30 CHASSIS. I STOPPED TO GAS UP AND MY AUTO PARK BRAKE SYSTEM LOCKED UP. I HAD TO DISABLE THE SYSTEM BY DISCONNECTING THE CABLE TO AUTO BRAKE SYSTEM. IF THIS WOULD HAVE HAPPENED WHILE ON THE HIGHWAY IT COULD HAVE BEEN FATAL . I WAS IN THE MOUNTAINS OF MISSOURI. GM SHOULD MAKE A RECALL ON THIS PROBLEM BECAUSE IT IS A VERY DANGEROUS SITUATION I
... F IT WOULD HAVE LOCKED UP ON THE HIGHWAY. *LARead more
Incident date: Oct 28, 2003
AUTOMATIC PARK BRAKE LIGHT ON, AUTOMATIC PARK BRAKE STAYS ON WHEN IN DRIVE OR REVERSE. THIS IS ON WINNABAGO ADVENTURE 1995 P-30 CHEV. CHASSIS.*AK
WILLIAM COUCH VS. WINNEBAGO INDUSTRIES.*MR CONSUMER ONLY USED THE MOTORHOME FOR TWO WEEKS AFTER PURCHASE. THE REST OF THE TIME IT WAS AWAITING REPAIRS. THE VEHICLE HAD OVER 30 SAFETY AND QUALITY ISSUES. CONSUMER SENT IN A CD AND PICTURES TO THE CEO; NUMEROUS EMAILS TO THE EMPLOYEES AND THE CONSUMER HAS HEARD NOTHING. CONSUMER WANTS THE MOTORHOME REPLACED PLUS REIMBURSE EXPENSES OR REFUND MONEY
... AND REIMBURSE EXPENSE AND TRADE IN VALUE OF ORIGINAL MOTORHOME. *PH *NLMRead more
Incident date: Sep 16, 2003
THE OWNER NOTICED FUEL LEAKING FROM UNDERNEATH THE VEHICLE. THE VEHICLE WAS TAKEN TO THE DEALERSHIP AND THE MECHANIC INDICATED THAT THE FUEL LINE RUPTURED AND WOULD NEED TO BE REPAIRED. *AK THERE WAS A GAS ODOR WHEN THE VEHICLE WAS IN MOTION. THE LEAK HAD COME FROM A SHORT NEOPRENE HOSE WHICH LEAD TO THE TANK TO THE ENGINE. *SCC *JB (WINNEBAGO RIALTA 2000)
Incident date: Jan 15, 2000
THE VEHICLE WOULD ROLL WHETHER THE PARK BRAKE WAS USED OR NOT. THE VEHICLE WAS TAKEN TO DEALER NUMEROUS TIMES, THE EMERGENCY BRAKE GEAR WAS REPLACED 3-4 TIMES, BUT THE PROBLEM CONTINUED. THE CONSUMER RECEIVED A LETTER FROM CHEVROLET IN JANUARY 2001 ADVISING OF PARK BRAKE PROBLEMS. *AK *SCC *JB
Incident date: Oct 10, 2003
SECOND FIRESTONE STEELTEX RADIAL LT225/75R16 HAD A COMPLETE BLOW-OUT ON OUTSIDE RIGHT REAR DUAL. FIRST COMPLAINT # 10023970. THE THREAD DESTROYED SEWER COMPARTMENT. *LA
Incident date: Apr 1, 2003
WHILE DRIVING AT APPROXIMATELY 35 MPH PLASTIC HINGE PIN SHEARED OFF, CAUSING THE THROTTLE PEDAL TO DETACH. ROADSIDE ASSISTANCE INSTALLED A TEMPORARY PIN, AND THE RECREATIONAL VEHICLE WAS TAKEN TO THE DEALER, WHO REPLACED THE TEMPORARY HINGE PIN WITH A PERMANENT STEEL HINGE PIN. *AK
THE DRIVER SAID, "THERE WAS A STRONG SMELL OF HOT BRAKE FLUID". HE COULD HEAR THE BRAKE FLUID BOILING WHILE INSIDE OF MOTOR HOME". AS A RESULT, THE BRAKES HAD TO BE PUMPED IN ORDER TO STOP. *AK
Incident date: Oct 16, 2003
MY MOTORHOME (1994 WINNEBAGO ELANTE) CONTAINS A P-30 CHASSIS. THE AUTOBRAKE SYSTEM IS VERY POORLY DESIGNED. THE HYDRAULIC ASSIST ACTUATOR IS POWERED BY THE POWER STEERING PUMP WHICH CONTAINS A VERY VERY SMALL RESERVOIR FOR THE PUMP. THE ACTUATOR LEAKS BADLY REQUIRING VERY FREQUENT ADDITIONS OF FLUID TO THE RESERVOIR. THE LEAK IS SO BAD THAT IT COVERS ALL SURFACES UNDER THE MOTOROME WITH FLUID
... WHICH I AM SURE IS A FIRE HAZARD. CHEVROLET HAS TOLD ME THAT THE ACTUATOR IS NO LONGER AVAILABLE FROM GENERAL MOTORS AND THAT I SHOULD TRY TO GET A LOCAL SHOP TO REBUILD THE UNIT FOR ME. I HAVE ALSO BEEN INFORMED BY CHEVROLET THAT IF I LET THE FLUID RUN LOW ENOUGH, THE AUTOBRAKE WILL FAIL WHICH WILL ALLOW THE PARKING BRAKE TO BE APPLIED WHILE GOING DOWN THE ROAD. THIS OF COURSE IS A MAJOR SAFETY HAZARD. CAN YOU IMAGINE WHAT WOULD HAPPEN IN THIS EVENT IF I WERE GOING SAY 60 MILES PER HOUR ? THERE HAS NOT YET BEEN A WRECK OR AN INCIDENT WHERE THERE WAS VEHICLE DAMAGE; HOWEVER, IT REQUIRES CONSTANT ATTENTION TO ADD FLUID AS SOON AS YOU HEAR THE POWER STEERING PUMP SUCKING IN AIR BUBBLES. THE RESERVOI CONTAINS ONLY ABOUT A QUART OR SO OF FLUID AND THE LEAK IS SO BAD THAT I HAVE TO ADD FLUID ABOUT EVERY 50 MILES OR SO. I AM VERY CONCERNED ABOUT A FIRE SINCE THIS FLUID IS COATING THE EXHAUST PIPES AND MUFFLER UNDER THE MOTORHOME. ALSO I AM VERY UPSET WITH GENERAL MOTORS IN THAT THEY HAVE DISCONTINUED THE MANUFACTURE OF THE ACTUATOR AND ABOVE THAT THERE IS NO RECALL FOR THIS PROBLEM. THIS IS A MAJOR DESIGN MISTAKE THAT THREATENS THE LIVES OF MY FAMILY AND POSSIBLY LIVES OF AN ON COMING VEHICLE IN THE EVENT OF FAILURE. *LARead more
Incident date: Sep 9, 2003
CRACKS (8 FRACTURES) IN THE RIGHT REAR FRAME RAIL OF WINNEBAGO 1995 LUXURY CLASS A MOTORHOME BUILT ON AN OSHKOSH CHASSIS HAVE OCCURRED. IN LEFT UNREPAIRED, THE SUSPENSION SYSTEM WOULD HAVE SEPARATED FROM THE CHASSIS, RENDERING THE MOTORHOME UNCONTROLLABLE. THE CRACKS IN OUR MOTORHOME CHASSIS WERE DETECTED IN JUNE 2003, WHEN REAR BRAKES WERE REPLACED AT MILEAGE 98,000. CHASSIS REPAIR WAS SUBSEQU
... ENTLY COMPLETED BY FREIGHT LINER CUSTOM CHASSIS CORPORATION ON 9/9/03 (INVOICE 36119), GAFFNEY, SC. FRIEGHT LINER CUSTOMER SERVICE PROVIDED US WITH A COPY OF OSHKOSH CORPORATION SERVICE BULLETIN V035RT, DATED 7/15/1995, REGARDING THE PROBLEM OF A "CRACKED FRAME RAIL, CAUSED BY INPUTS FROM THE REAR AXLE LATERAL TORQUE ROD." THIS SERVICE BULLETIN PROVIDED OPPORTUNITY FOR FREE REPAIR IF OWNERS REQUESTED REPAIR WITHIN THE WARRANTY PERIOD (3 YEARS OR 36,000 MILES FROM THE DELIVERY DATE). OSHKOSH CLAIMS TO HAVE SENT LETTERS TO ALL OWNERS OF RECORD AS OF THE DATE OF THE SERVICE BULLETIN REGARDING THE RISK OF A CRACKED RAIL FRAME; THEY DID NOT PUT INTO MOTION A MEANS TO SEND OUT LETTERS TO FUTURE OWNER AFTER THAT DATE. OUR MOTOR HOME (VIN [XXX]) WAS MANUFACTURED BY OSHKOSH IN FEBRUARY 1995, SHIPPED TO WINNEBAGO INDUSTRIES WHO COMPLETED THE MOTORHOME CONSTRUCTION ON 5/22/1995, AND WHO THEN SHIPPED THE COMPLETED MOTORHOME TO A DISTRIBUTOR IN CALIFORNIA (SADDLEBACK RV, TUSTIN, CA). WE PURCHASED THE RV NEW ON 7/7/1997. REGARDING OUR CHASSIS FOR WHICH THERE WAS NO OWNER OF RECORD AT THE TIME OF THE ISSUANCE OF THE SERVICE BULLETIN, OSHKOSH CLAIMS THAT WINNEBAGO INDUSTRIES WAS NOTIFIED OF THE FLAWED CHASSIS ISSUE. WINNEBAGO DID NOT NOTIFY US OF THE SERVICE BULLETIN OR OF THE POTENTIAL FLAW, NOR DOES IT APPEAR THAT WINNEBAGO NOTIFIED ANY OTHER PURCHASERS OF THE 1995 LUXURY MOTORHOME PRODUCT LINE. BASED ON THE EXPERIENCE OF OUR CHASSIS, IT APPEARS THAT ACTUAL CRACKS IN THE FRAME RAIL DO NOT BEGIN TO APPEAR UNTIL THERE HAS BEEN SIGNIFICANT MILEAGE ON THE CHASSIS. *LA INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACRead more
Incident date: Sep 17, 2002
DRIVER'S SIDE WALL IS NOT ATTACHED TO THE CHASSIS PLATFORM. THE WALL IS STEADILY SLIDING DOWN TO THE SIDE OF VEHICLE. THERE IS A COVER OVER THE REAR DUAL WHEELS THAT MAKES IT DIFFICULT TO FILL THE GAS TANK. THE MANUFACTURER OFFERED TO REPAIR THE PROBLEM AT NO COST TO THE CONSUMER. *AK THE MANUFACTURER WOULD NOT WARRANT THAT THE LONG TERM RELIABILITY OF THE VEHICLE HAS NOT BEEN COMPROMISED
... . *NLMRead more
MICHELIN BRAND NEW TIRES MANUFACTURED IN 2000. CONSUMER HAD A BLOW OUT AT 17,000, AND TWO MORE AT 21,000. WHILE DRIVING AT 60 MPH DRIVER'S REAR INSIDE TIRE SPLIT 8 INCHES, CONSUMER TEMPORARILY LOST CONTROL. THE SECOND BLOW OUT OF DRIVER'S REAR TIRE OCCURRED AT 65 MPH. PASSENGER'S SIDE REAR TIRE WAS THE THIRD TO BLOW OUT AT 50 MPH. *AK CONSUMER WOULD LIKE MICHELIN TO REIMBURS
... E HIM A THOUSAND DOLLARS FOR OUT OF POCKET COST. *PHRead more
Incident date: Jun 17, 2003
FRAME MOUNTS UNDER REAR WHEEL WELLS ON 2000 WINNEBAGO JOURNEY FAILED DUE TO FAULTY WELDING; NOTICED PROBLEM WHEN METAL IN WHEEL WELLS STARTED COLLAPSING; THESE WELDS JOIN THE CHASSIS TO FRAME OF RV; HAVE NO REAL INDICATION OF WHEN WELDS FAILED BUT HAS BEEN SEVERAL MONTHS; BECAUSE OF FAULTY WELDS, LOTS OF SHIFTING AND SAGGING IN BACK OF RV ALSO CAUSING POSSIBLE FIRE HAZARD AND HAS FALLEN ON AIR LIN
... ES. *JBRead more
Incident date: Sep 16, 2002
PASSENGER FRONT TIRE BLEW OUT AT AROUND 20,000 MILES ON ODOMETER; SECOND DRIVER SIDE TIRE FOUND TO HAVE BUBBLE ON INSIDE SIDEWALL AROUND 25,000 MILES ON ODOMETER; SECOND TIRE TAKEN TO MICHELIN DEALER WHOM STATED THAT TIRE APPEARED TO BE AFFECTED BY IMPACT AND NOT COVERED BY WARRANTY; TIRES HAVE ONLY BEEN IMPACTED BY NORMAL POTHOLES, ETC; TALKED TO SEVERAL FOLKS INCLUDING CHASSIS MANUFACTURER (FREI
... GHTLINER) AND FOUND THAT SIDEWALLS VERY THIN ON XRV TIRES AND FREQUENTLY EXPERIENCE BLOWOUTS; ALSO FOUND SEVERAL OTHER COMPLAINTS ON INTERNET OF FOLKS EXPERIENCING BLOWOUTS AT SIMILAR MILEAGE; HAVE SINCE REPLACED TIRES WITH XVE SINCE THESE ARE MUCH THICKER SIDEWALLS AND HAVE LONGER WEAR.*JBRead more
Incident date: Aug 28, 2003
WHILE PERFORMING REPAIRS FOR RECALL 02E019000 CONCERNING THE REFRIGERATOR COOLING UNIT FIRES, THE MECHANIC BROKE THE GAS LINE AND CHARGED THE CONSUMER TO REPAIR THE GAS LINE. *AK *LA *JB
THE LAMINATION ON EACH SIDE NEAR THE REAR OF VEHICLE WAS PEELING OFF. CONSUMER FEARS THAT IF THE PEELING CONTINUES THE END CAPS THAT HOLD THE TWO CORNERS DOWN WILL EVENTUALLY SNAP OFF WHILE IN TRAFFIC. MANUFACTURER HAVE BEEN NOTIFIED OF THE PROBLEM.*AK
Incident date: Sep 7, 2003
MY 2000 WINNEBAGO MOTORHOME WITH FIRESTONE STEELTEX RADIAL LT225/75R16 TIRES HAD A BLOWOUT, CATASTROPHIC TREAD SEPARATION. CAUSED DAMAGE TO TAILPIPE, MUDFLAP, SIDE PANEL. *AK
CONSUMER RECEIVED RECALL NOTICE 02E019000 SUBJECT CONCERNING REFRIGERATOR COOLING UNIT FIRE. DEALER DID NOT HAVE THE PARTS TO PERFORM REPAIRS. DEALER AND CONSUMER CONTACTED NORCOLD TO ORDER THE PARTS, AND HAD NOT RECEIVED A RESPONSE FOR SIX WEEKS.*AK
Incident date: Jul 19, 2003
COMPLETE TREAD SEPARATION. HIGHWAY 2 NEAR CRESTON, WA. 2 LANE HWY, SPEED APPROX 60 MPH. TEMP 102. VEHICLE WINNEBAGO 27 FT RV, FORD CHASSIS. ORIG EQUIP TIRE, APPROX 33,000 MI. RIGHT FRONT TIRE. PRESSURE CHECKED FREQUENTLY AND WAS CORRECT. TIRE DID NOT DEFLATE. PROPERTY DAMAGE NEGLIBIBLE. *AK THE CONSUMER WANTS TO KNOW WHY ARE THE TIRES STILL ON THE ROAD? THE PROBLEMS ARE WITH THE STEELT
... EX R4S SEPARATING THE TREAD. THE CONSUMER FEELS THEY SHOULD BE RECALLED. *CBRead more
Incident date: Jul 20, 2003
COMPLETE TREAD SEPARATION. I90, LIVINGSTON, MT, INTERSTATE HIGHWAY, SPEED 70 MPH. TEMP 100. VEHICLE WINNEBAGO 27 FT RV, FORD CHASIS. ORIG EQUIP TIRE, APPROX 33,300 MI. RIGHT REAR INNER DUAL. TIRE DID NOT DEFLATE. THIS IS THE SECOND TIRE OF THIS SERIES TO SEPARATE THE TREAD ON THIS VEHICLE. PROPERTY DAMAGE WAS NEGLIBIBLE, BUT CONFIDENCE DAMAGE WAS GREAT. IS THERE A PROBLEM WITH FIRESTONE STEEL
... TEX R4S TIRES? I HAVE FOUR MORE ON MY RV AND I NO LONGER FEEL CONFIDENT WITH THEM? CAN YOU ADVISE??*AKRead more
Incident date: Oct 1, 2002
VEHICLE COMES EQUIPPED WITH AN AUTOMATIC EMERGENCY PARKING BRAKE, THAT ENGAGES WHEN VEHICLE IS PUT INTO PARK. WHEN PARKING BRAKES GO OUT OF ADJUSTMENT IT DOESN'T HOLD AND VEHICLE ROLLS FORWARD.*AK CONSUMER PUT THE TRANSMISSION IN PARK TO SET THE BRAKE. WHEN HE AND HIS WIFE STARTED TO EXIT HE VEHICLE, IT STARTED TO ROLL. THE CONSUMER HAD TO GATHER ROCK TO HOLD THE VEHICLE IN PLACE. THE BR
... AKE SHOES WERE REPLACED AND THE BRAKES WERE ADJUSTED AT AN INDEPENDENT TRUCK SHOP ($200.). CONSUMER AGAIN EXPERIENCED THE SAME DEFECT IN AUGUST OF 2003. ANOTHER INDEPENDENT TRUCK CO. ATTEMPTED TO ADJUST THE BRAKES JUST SO THE CONSUMER COULD GET BY ($144.). LATER HE FOUND A GM TRUCK DEALER WHO REPLACED THE BRAKE SHOES AND TWO BRAKE CABLES (OVER $700.) THE REPAIRMAN STATED THE CABLE WAS TO CLOSE TO THE EXHAUST SYSTEM RESULTING IN FAILURE. THE CABLE WASN'T RELEASING THE BRAKE SHOES CAUSING THEM TO BURN OUT AND FAIL. THERE WAS NO WARNING ON THE DASH TO INDICATE ANY TYPE OF BRAKE FAILURE. *PH *NLMRead more
Incident date: Oct 1, 2002
VEHICLE COMES EQUIPPED WITH AN AUTOMATIC EMERGENCY PARKING BRAKE, THAT ENGAGES WHEN VEHICLE IS PUT INTO PARK. WHEN PARKING BRAKES GO OUT OF ADJUSTMENT IT DOESN'T HOLD AND VEHICLE ROLLS FORWARD.*AK CONSUMER PUT THE TRANSMISSION IN PARK TO SET THE BRAKE. WHEN HE AND HIS WIFE STARTED TO EXIT HE VEHICLE, IT STARTED TO ROLL. THE CONSUMER HAD TO GATHER ROCK TO HOLD THE VEHICLE IN PLACE. THE BR
... AKE SHOES WERE REPLACED AND THE BRAKES WERE ADJUSTED AT AN INDEPENDENT TRUCK SHOP ($200.). CONSUMER AGAIN EXPERIENCED THE SAME DEFECT IN AUGUST OF 2003. ANOTHER INDEPENDENT TRUCK CO. ATTEMPTED TO ADJUST THE BRAKES JUST SO THE CONSUMER COULD GET BY ($144.). LATER HE FOUND A GM TRUCK DEALER WHO REPLACED THE BRAKE SHOES AND TWO BRAKE CABLES (OVER $700.) THE REPAIRMAN STATED THE CABLE WAS TO CLOSE TO THE EXHAUST SYSTEM RESULTING IN FAILURE. THE CABLE WASN'T RELEASING THE BRAKE SHOES CAUSING THEM TO BURN OUT AND FAIL. THERE WAS NO WARNING ON THE DASH TO INDICATE ANY TYPE OF BRAKE FAILURE. *PH *NLMRead more