Showing 1,744 complaints for WINNEBAGO
Incident date: Apr 11, 2013
TL* THE CONTACT OWNS A 2010 WINNEBAGO VIEW MOTOR HOME. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE REAR DRIVER AND PASSENGER TIRE HUB CAPS DETACHED FROM THE VEHICLE. THE CONTACT STATED THAT THEY WERE NOT SECURED PROPERLY. THE RV WAS NOT TAKEN TO A DEALER FOR AN INSPECTION. THE FAILURE WAS NOT REPORTED TO THE MANUFACTURER. THE FAILURE MILEAGE WAS 20,000. THE CURRENT MILEAGE WAS 21,000. UPDA
... TED 07/16/13*LJ BOTH REAR WHEEL COVERS WERE REPLACED BY THE DEALER. ..UPDATED 08-07-13 *BF PHOTOS RECEIVED. 08/20/13Read more
Incident date: Apr 11, 2013
TL* THE CONTACT OWNS A 2010 WINNEBAGO VIEW MOTOR HOME. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE REAR DRIVER AND PASSENGER TIRE HUB CAPS DETACHED FROM THE VEHICLE. THE CONTACT STATED THAT THEY WERE NOT SECURED PROPERLY. THE RV WAS NOT TAKEN TO A DEALER FOR AN INSPECTION. THE FAILURE WAS NOT REPORTED TO THE MANUFACTURER. THE FAILURE MILEAGE WAS 20,000. THE CURRENT MILEAGE WAS 21,000. UPDA
... TED 07/16/13*LJ BOTH REAR WHEEL COVERS WERE REPLACED BY THE DEALER. ..UPDATED 08-07-13 *BF PHOTOS RECEIVED. 08/20/13Read more
Incident date: Apr 19, 2001
THIS MOTORHOME WAS PURCHASED NEW IN MAR OF 2001. IN APR OF THAT YEAR THE PARKING BRAKES WOULD NOT DISENGAGE. IT WAS TOWED TO A SERVICE FACILITY AND REMAINED THERE FOR SEVERAL WEEKS BECAUSE OF PARTS SHORTAGE. OVER THE YEARS THE PARKING BRAKES HAVE LOCKED EITHER WHILE THE VEHICLE WAS IN MOTION (62 MPH) OR WHILE ATTEMPTING TO PLACE IT IN MOTION: 20 APR 2005, 13 OCT 2006, 19 OCT 2006, 5 SEP 2008,2 FEB
... 2011. NOW THE PARKING BRAKES INTERMITTENTLY DO NOT ENGAGE: 13 MAR 2012, 5 JUN 2012, 11 DEC 2012, 11 JAN 2013, 15 MAY 2013. *TRRead more
Incident date: May 1, 2013
2013 WINNEBAGO VISTA. CONSUMER WRITES IN REGARDS TO VEHICLE UNSTABLE STEERING. *SMD THE CONSUMER STATED THE RV HAS ROLL, SWAY, WANDER AND TRUCK PUSH PROBLEMS. THE RV WAS ALREADY VULNERABLE DUE TO ITS HEIGHT, WEIGHT AND SIZE. IT WAS RECOMMENDED IT THE RV DIDN'T HAVE IMPROVED STEERING CONTROL, IT SHOULD NOT BE DRIVEN OR 60 MPH, AND LESS WITH INCREASED WINDS.
Incident date: May 1, 2013
2013 WINNEBAGO VISTA. CONSUMER WRITES IN REGARDS TO VEHICLE UNSTABLE STEERING. *SMD THE CONSUMER STATED THE RV HAS ROLL, SWAY, WANDER AND TRUCK PUSH PROBLEMS. THE RV WAS ALREADY VULNERABLE DUE TO ITS HEIGHT, WEIGHT AND SIZE. IT WAS RECOMMENDED IT THE RV DIDN'T HAVE IMPROVED STEERING CONTROL, IT SHOULD NOT BE DRIVEN OR 60 MPH, AND LESS WITH INCREASED WINDS.
Incident date: May 1, 2013
2013 WINNEBAGO VISTA. CONSUMER WRITES IN REGARDS TO VEHICLE UNSTABLE STEERING. *SMD THE CONSUMER STATED THE RV HAS ROLL, SWAY, WANDER AND TRUCK PUSH PROBLEMS. THE RV WAS ALREADY VULNERABLE DUE TO ITS HEIGHT, WEIGHT AND SIZE. IT WAS RECOMMENDED IT THE RV DIDN'T HAVE IMPROVED STEERING CONTROL, IT SHOULD NOT BE DRIVEN OR 60 MPH, AND LESS WITH INCREASED WINDS.
Incident date: May 3, 2013
THIS REPORT IS ON A FAILED ODOMETER. AT AROUND 53100 MILES THE ODOMETER SET TO ZERO AND STARTED COUNTING FORWARD AGAIN. I BROUGHT THE COACH TO A FREIGHTLINER DEALER IN DALLAS, TX. WHEN THE COACH WAS RECEIVED I WAS INFORMED THAT THE ODOMETER COULD NOT BE CALIBRATED TO THE CORRECT AND KNOWN MILEAGE INDICATED BY ANOTHER ENGINE MONITORING COMPUTER. THE ACTUAL MILEAGE ON THE COACH AT THE TIME OF TH
... E REPAIR WAS 53913. WHILE WAITING FOR THE REPAIRS TO BE COMPLETED I FOUND ANOTHER COACH THROUGH THE INTERNET IN FL THAT I WANTED TO TRADE MY COACH FOR. WHEN I TOLD THE RV DEALER OF THE ODOMETER FAILURE HE TOLD ME THAT HE WOULD NOT TAKE MY COACH IN TRADE IF THE ODOMETER WERE NOT CORRECTED TO THE ACTUAL MILEAGE OF THE UNIT. WE PROCEEDED TO WORK ON A DEAL AND I QUALIFIED FOR A LOAN AND HAVE A BANK READY TO LEND ME THE MONEY FOR THE NEW TO ME USED COACH OF A LATER MODEL YEAR. THE DEALER HAS VALUED MY COACH AT $124,900. AS OF THIS WRITING I HAVE NOT BEEN ABLE TO FIND A ODOMETER REPAIR SHOP THAT CAN CALIBRATE MY ODOMETER TO THE CORRECT READING OF USAGE. I HAVE CONTACTED FREIGHTLINER ABOUT THIS MATTER AND THEY STAND FIRM THAT IT IS ILLEGAL FOR THEM TO CALIBRATE THE ODOMETER AND THERE IS NO POSSIBLE MEANS FOR THIS TO BE ACCOMPLISHED. BY THEIR DECREE MY COACH HAS BECOME VALUELESS. *TRRead more
Incident date: Mar 1, 2013
2011 WINNEBAGO ITASCA. CONSUMER WRITES IN REGARDS TO VEHICLE STEPS FAILED TO EXTEND. *SMD THE CONSUMER STATED THE RV HAD BEEN PARKED FOR TWO MONTHS. THE CONSUMER DISCOVERED THE BATTERY WAS DEAD. HE USED THE TRICKLE CHARGER TO START THE RV, AS HE WAS INSTRUCTED TO DO, IF THE UNIT DID NOT START. THE NEXT DAY, THE CONSUMER OPENED THE DOOR AND DID NOT NOTICE THE STEPS FAILED TO EXTEND, WHICH RESU
... LTED IN HIM FALLING OUT OF THE UNIT AND INJURING HIS SHOULDER IN THE PROCESS. HE CONTACTED THE TECHNICIANS TO GET AN EXPLANATION AS TO WHY THE CHASSIS BATTERY WAS DEAD, AND WHY THE TRICKLE CHARGER DID NOT WORK, IF THE CHASSIS BATTERY WAS ON A SEPARATE CHARGER THAT FAILED. THE CONSUMER WAS INFORMED THE MANUFACTURER NO LONGER WIRED THE CHASSIS BATTERY INTO THE CHARGING SYSTEM, BECAUSE VARIOUS SYSTEMS ON THE UNIT COULD DRAIN THE CHASSIS BATTERY EVEN IF THE BATTERY WAS DISCONNECTED USING THE DISCONNECT SWITCH AND THE STEPS WORKED SOLELY FROM POWER PROVIDED BY THE CHASSIS BATTERY... UPDATED 04-05-13 *BF PICTURES RECEIVED. UPDATED 04/18/13Read more
1 injured
Incident date: Mar 1, 2013
2011 WINNEBAGO ITASCA. CONSUMER WRITES IN REGARDS TO VEHICLE STEPS FAILED TO EXTEND. *SMD THE CONSUMER STATED THE RV HAD BEEN PARKED FOR TWO MONTHS. THE CONSUMER DISCOVERED THE BATTERY WAS DEAD. HE USED THE TRICKLE CHARGER TO START THE RV, AS HE WAS INSTRUCTED TO DO, IF THE UNIT DID NOT START. THE NEXT DAY, THE CONSUMER OPENED THE DOOR AND DID NOT NOTICE THE STEPS FAILED TO EXTEND, WHICH RESU
... LTED IN HIM FALLING OUT OF THE UNIT AND INJURING HIS SHOULDER IN THE PROCESS. HE CONTACTED THE TECHNICIANS TO GET AN EXPLANATION AS TO WHY THE CHASSIS BATTERY WAS DEAD, AND WHY THE TRICKLE CHARGER DID NOT WORK, IF THE CHASSIS BATTERY WAS ON A SEPARATE CHARGER THAT FAILED. THE CONSUMER WAS INFORMED THE MANUFACTURER NO LONGER WIRED THE CHASSIS BATTERY INTO THE CHARGING SYSTEM, BECAUSE VARIOUS SYSTEMS ON THE UNIT COULD DRAIN THE CHASSIS BATTERY EVEN IF THE BATTERY WAS DISCONNECTED USING THE DISCONNECT SWITCH AND THE STEPS WORKED SOLELY FROM POWER PROVIDED BY THE CHASSIS BATTERY... UPDATED 04-05-13 *BF PICTURES RECEIVED. UPDATED 04/18/13Read more
1 injured
Incident date: Mar 1, 2013
RECALL MADE DECEMBER 2005 TO REPAIR/REPLACE ACTIA INSTRUMENT CLUSTER (BULLETIN #8051-IA, REPLACES 80201-I, DATED MARCH 2002). HAVE HAD MOTOR HOME AT REPAIR SHOP SINCE OCTOBER, 2012 & HAVE NOT BEEN ABLE TO GET "WORKHORSE (NAVISTAR) CUSTOMER SERVICE TO CORRECT THE FAULT. KEEP GETTING PROMISE, WEEKLY, WITH NO RESULT. HAVE WRITTEN WINNEBAGO & WORKHORSE (NAVISTAR) ON OTHER PROBLEMS AND GET NO HELP F
... ROM EITHER. THIS MOTOR HOME COST $86,000 NEW AND THEY REFUSE TO CORRECT A FAULT THAT MIGHT COST THEM LESS THAN $1,000 (MY GUESS). NEED SOMEONE TO PUT THEIR FEET TO THE FIRE AND GET THIS COMPLETED (AT NO COST TO ME) BFORE TRYING TO READ LCD READOUTS CAUSES A CATASTROPHIC EVENT. [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Dec 27, 2012
TL* THE CONTACT OWNS A 2002 WINNEBAGO SIGHTSEER. THE CONTACT STATED THAT THE BRAKES FAILED. THE CONTACT WAS ABLE TO COAST TO A STOP AND THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE MECHANIC ADVISED HIM THAT THERE WAS A RECALL FOR THE FAILURE UNDER NHTSA CAMPAIGN ID NUMBER: 09V186000 (SERVICE BRAKES: HYDRAULIC). THE CONTACT DID NOT CONFIRM WITH THE MANUFACTURER IF HIS PARTICULAR VIN WAS IN
... CLUDED IN THE RECALL CAMPAIGN. THE VEHICLE WAS REPAIRED. THE FAILURE AND THE CURRENT MILEAGES WERE 44,000. ... UPDATED 02/28/13 *BF UPDATED 03/12/2013 *JSRead more
Incident date: Dec 27, 2012
TL* THE CONTACT OWNS A 2002 WINNEBAGO SIGHTSEER. THE CONTACT STATED THAT THE BRAKES FAILED. THE CONTACT WAS ABLE TO COAST TO A STOP AND THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE MECHANIC ADVISED HIM THAT THERE WAS A RECALL FOR THE FAILURE UNDER NHTSA CAMPAIGN ID NUMBER: 09V186000 (SERVICE BRAKES: HYDRAULIC). THE CONTACT DID NOT CONFIRM WITH THE MANUFACTURER IF HIS PARTICULAR VIN WAS IN
... CLUDED IN THE RECALL CAMPAIGN. THE VEHICLE WAS REPAIRED. THE FAILURE AND THE CURRENT MILEAGES WERE 44,000. ... UPDATED 02/28/13 *BF UPDATED 03/12/2013 *JSRead more
Incident date: Dec 27, 2012
TL* THE CONTACT OWNS A 2002 WINNEBAGO SIGHTSEER. THE CONTACT STATED THAT THE BRAKES FAILED. THE CONTACT WAS ABLE TO COAST TO A STOP AND THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE MECHANIC ADVISED HIM THAT THERE WAS A RECALL FOR THE FAILURE UNDER NHTSA CAMPAIGN ID NUMBER: 09V186000 (SERVICE BRAKES: HYDRAULIC). THE CONTACT DID NOT CONFIRM WITH THE MANUFACTURER IF HIS PARTICULAR VIN WAS IN
... CLUDED IN THE RECALL CAMPAIGN. THE VEHICLE WAS REPAIRED. THE FAILURE AND THE CURRENT MILEAGES WERE 44,000. ... UPDATED 02/28/13 *BF UPDATED 03/12/2013 *JSRead more
Incident date: Dec 27, 2012
TL* THE CONTACT OWNS A 2002 WINNEBAGO SIGHTSEER. THE CONTACT STATED THAT THE BRAKES FAILED. THE CONTACT WAS ABLE TO COAST TO A STOP AND THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE MECHANIC ADVISED HIM THAT THERE WAS A RECALL FOR THE FAILURE UNDER NHTSA CAMPAIGN ID NUMBER: 09V186000 (SERVICE BRAKES: HYDRAULIC). THE CONTACT DID NOT CONFIRM WITH THE MANUFACTURER IF HIS PARTICULAR VIN WAS IN
... CLUDED IN THE RECALL CAMPAIGN. THE VEHICLE WAS REPAIRED. THE FAILURE AND THE CURRENT MILEAGES WERE 44,000. ... UPDATED 02/28/13 *BF UPDATED 03/12/2013 *JSRead more
Incident date: Oct 22, 2012
TL* THE CONTACT 2003 WINNEBAGO BRAVE CLASS A. THE CONTACT STATED THAT AFTER PARKING HIS VEHICLE HE APPLIED THE PARKING BRAKE. AFTER EXITING THE VEHICLE HE NOTICED THAT IT STARTED TO ROLL BACKWARDS. HE IMMEDIATELY GOT BACK INTO THE VEHICLE AND DEPRESSED ON THE BRAKES. THE VEHICLE WAS LATER TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE SWITCH FOR THE PARKING BRAKE WAS BLOWN AND NEEDED TO B
... E REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS CONTACTED AND THEY OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 55,018. THE CURRENT MILEAGE WAS APPROXIMATELY 55,518.Read more
Incident date: Oct 5, 2010
TL* THE CONTACT OWNS A 2008 WINNEBAGO VISTA. THE CONTACT STATED THAT WHILE DRIVING 60 MPH THE PASSENGER SIDE WINDSHIELD WIPER BECAME UNSCREWED FROM THE SHAFT AND CAUSED BOTH WIPERS TO MALFUNCTION. THE CONTACT TIGHTENED THE SCREW AND 10 MILES LATER IT LOOSENED AGAIN CAUSING THE FAILURE TO RECUR. HE THEN DETACHED THE PASSENGER SIDE WIPER AND CONTINUED TO DRIVE WITH ONLY THE DRIVER SIDE WIPER. IN ADD
... ITION, THE CONTACT MENTIONED THAT THE ALUMINUM IN THE BUMPER HAD CORRODED AND WOULD HAVE FALLEN OFF IF HE HAD NOT REINFORCED IT WITH STEEL. THE MANUFACTURER WAS NOTIFIED BUT OFFERED NO ASSISTANCE. THE FAILURE AND CURRENT MILEAGE WAS 31,199. ..UPDATED 01/17/2013 *BF THE CONSUMER STATED THE ISSUE WITH THE WIPER IS THERE IS A LACK OF ADEQUATE SUPPORT FOR THE MECHANISM ON THE PASSENGER'S SIDE. UPDATED 1/24/2013 *JSRead more
Incident date: Oct 5, 2010
TL* THE CONTACT OWNS A 2008 WINNEBAGO VISTA. THE CONTACT STATED THAT WHILE DRIVING 60 MPH THE PASSENGER SIDE WINDSHIELD WIPER BECAME UNSCREWED FROM THE SHAFT AND CAUSED BOTH WIPERS TO MALFUNCTION. THE CONTACT TIGHTENED THE SCREW AND 10 MILES LATER IT LOOSENED AGAIN CAUSING THE FAILURE TO RECUR. HE THEN DETACHED THE PASSENGER SIDE WIPER AND CONTINUED TO DRIVE WITH ONLY THE DRIVER SIDE WIPER. IN ADD
... ITION, THE CONTACT MENTIONED THAT THE ALUMINUM IN THE BUMPER HAD CORRODED AND WOULD HAVE FALLEN OFF IF HE HAD NOT REINFORCED IT WITH STEEL. THE MANUFACTURER WAS NOTIFIED BUT OFFERED NO ASSISTANCE. THE FAILURE AND CURRENT MILEAGE WAS 31,199. ..UPDATED 01/17/2013 *BF THE CONSUMER STATED THE ISSUE WITH THE WIPER IS THERE IS A LACK OF ADEQUATE SUPPORT FOR THE MECHANISM ON THE PASSENGER'S SIDE. UPDATED 1/24/2013 *JSRead more
Incident date: Oct 5, 2010
TL* THE CONTACT OWNS A 2008 WINNEBAGO VISTA. THE CONTACT STATED THAT WHILE DRIVING 60 MPH THE PASSENGER SIDE WINDSHIELD WIPER BECAME UNSCREWED FROM THE SHAFT AND CAUSED BOTH WIPERS TO MALFUNCTION. THE CONTACT TIGHTENED THE SCREW AND 10 MILES LATER IT LOOSENED AGAIN CAUSING THE FAILURE TO RECUR. HE THEN DETACHED THE PASSENGER SIDE WIPER AND CONTINUED TO DRIVE WITH ONLY THE DRIVER SIDE WIPER. IN ADD
... ITION, THE CONTACT MENTIONED THAT THE ALUMINUM IN THE BUMPER HAD CORRODED AND WOULD HAVE FALLEN OFF IF HE HAD NOT REINFORCED IT WITH STEEL. THE MANUFACTURER WAS NOTIFIED BUT OFFERED NO ASSISTANCE. THE FAILURE AND CURRENT MILEAGE WAS 31,199. ..UPDATED 01/17/2013 *BF THE CONSUMER STATED THE ISSUE WITH THE WIPER IS THERE IS A LACK OF ADEQUATE SUPPORT FOR THE MECHANISM ON THE PASSENGER'S SIDE. UPDATED 1/24/2013 *JSRead more
Incident date: Aug 15, 2012
TL* THE CONTACT OWNS A 2008 WINNEBAGO VIEW. THE CONTACT STATED THAT WHILE TRAVELING 50 MPH ON AN INCLINE, THE VEHICLE DECELERATED ABNORMALLY, DESPITE THE ACCELERATOR BEING DEPRESSED. THE VEHICLE WAS TAKEN TO A LOCAL REPAIR SHOP AND THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 18,500 AND THE CURRENT MILEAGE WAS 19,800. UPDATED 10/25/12*LJ
... THE CONSUMER STATED THE TURBO AND EXHAUST MANIFOLD WERE BOTH REPLACED DUE TO RUSTED/BROKEN BOLTS. UPDATED 10/26/2012 *JSRead more
Incident date: Jun 15, 2012
TL* THE CONTACT OWNS A 2012 WINNEBAGO ONE 26 RK TRAVEL TRAILER. THE CONTACT STATED THAT THE SLIDING WALLS DEVELOPED A FRACTURE. ALSO, THE CONTACT MENTIONED THAT THE ROOF WAS LIFTED AND WATER WAS SEEPING INTO THE CABIN CAUSING WATER DAMAGE. THE VEHICLE WAS TAKEN TO THE DEALER WHO STATED THAT THE FAILURE WAS DUE TO THE WALLS SLIDING IMPROPERLY. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID
... NOT OFFER ANY ASSISTANCE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS UNKNOWN.Read more
Incident date: Aug 29, 2012
TL* THE CONTACT OWNS A 2005 WINNEBAGO ITASCA MOTOR HOME 38R. THE CONTACT STATED THAT PROPANE FUEL FUMES WERE EMITTED INTO THE VEHICLE. THE VEHICLE TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE PROPANE TANK NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE SINCE THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN ID NUMBER: 04V114000 (EQUIP
... MENT). THE FAILURE MILEAGE WAS 55,000 AND THE CURRENT MILEAGE WAS 65,000. THE VIN WAS NOT AVAILABLE.Read more
Incident date: Jul 23, 2012
TL* THE CONTACT OWNS A 2001 WINNEBAGO ADVENTURER. THE CONTACT STATED THAT THE VEHICLE WAS TAKEN TO A MECHANIC FOR ROUTINE MAINTENANCE. THE MECHANIC ADVISED THE CONTACT THAT THE BRAKES WERE OVERHEATED AND CAUSING THE CALIPERS TO STICK AND BOIL THE BRAKE FLUID. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 41,000.
Incident date: Jul 8, 2012
WE PURCHASED A 2012 WINNEBAGO NAVION 24J FROM CAMPING WORLD SUPERCENTER NEW BRAUNSFEL, TX JUNE 29, 2012. RETURNING FROM A TRIP TO OHIO ON JULY 8, 2012, WE ENCOUNTERED HEAVY STORMS, AVOIDING A NEAR COLLISION WE DISCOVERED THE HORN DID NOT WORK! WE REPORTED THE MALFUNCTION TO CAMPING WORLD AND WERE TOLD TO BRING THE RV INTO THE SERVICE DEPARTMENT ON JULY 17TH, 2012. JULY 20, 2012 WE WERE TOLD ALL I
... SSUES WERE ADDRESSED AND THE VEHICLE READY FOR OUR PICKUP ON JULY 24, 2012. WE WENT TO RETRIEVE THE VEHICLE JULY 25, 2012 ONLY TO DISCOVER THE HORN STILL DID NOT WORK. [XXX], SALES MANAGER, WAS INFORMED AND HE INSISTED THE RV PASSED THEIR "INTERNAL" INSPECTION AND PREDELIVERY CHECK. WE REITERATED THE HORN IS STILL NOT WORKING. WE INQUIRED AS TO WHY WERE WE TOLD TO PICK THE VEHICLE UP IF THE HORN STILL MALFUNCTIONED. NO ANSWER TO THIS INQUIRY. NOW WE ARE TOLD THE PROBLEM LIES WITHIN THE ELECTRICAL SYSTEM AND HAS TO BE SERVICED ELSEWHERE. WE HAVE NOT HAD ACCESS TO OUR NEW VEHICLE SINCE JULY 17. WE FURTHER REFUSE TO ACCEPT THE VEHICLE UNDER ITS CURRENT HAZARDOUS CONDITIONS. WE ARE DEMANDING CAMPING WORLD REMEDY THIS DANGEROUS DEFECT. WE ARE PREPARED TO FILE A TX DEPARTMENT OF TRANSPORTATION LEMON LAW CLAIM AGAINST CAMPING WORLD. WE ARE REQUESTING ANY FURTHER ASSISTANCE AND/OR INFORMATION THAT CAN BE PROVIDED BY THIS DEPARTMENT. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Jul 9, 2012
TL*THE CONTACT OWNS A 2007 WINNEBAGO VISTA. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE BRAKE PEDAL WAS DEPRESSED AND IT STUCK TO THE FLOOR. THE CONTACT WAS ABLE TO STOP THE VEHICLE BY APPLYING THE EMERGENCY BRAKE. THE VEHICLE WAS THEN TAKEN TO A LOCAL MECHANIC. THE MECHANIC STATED THAT THE BRAKE LINES WERE CORRODED BECAUSE OF A DEFECTIVE PROTECTIVE SHIELD THAT ALLOWED MOISTURE TO PENETRATE.
... THE LOCAL MECHANIC REPLACED THE PROTECTIVE SHIELD AND BRAKE LINES. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE AND CURRENT MILEAGES WERE 30,500....UPDATED 08-03-12 *BF UPDATED 08/09/2012 *JSRead more
Incident date: May 14, 2012
AFTER ARRIVING HOME FROM A 3-HOUR DRIVE ON FEDERAL INTERSTATE I-10, WE DISCOVERED THAT THE FIBERGLASS LOWER REAR PANEL WAS GONE. THE 9 FT WIDE X 2.5 FT TALL PANEL HAD SEPARATED FROM THE ATTACHMENT POINTS. IT APPEARS THAT THE ADHESIVE BETWEEN THE PANEL AND THE CHASSIS SUPPORTS FAILED. NO OTHER MOTORISTS NOTIFIED US THAT THE PANEL WAS GONE/MISSING. IF THIS PROBLEM OCCURS IN TRAFFIC, A POTENTIAL MA
... JOR TRAFFIC ACCIDENT COULD OCCUR FROM THIS LARGE PANEL IMPACTING A PASSENGER CAR OR SIMILAR AT FREEWAY SPEEDS. PHOTOS ARE AVAILABLE. *TRRead more
Incident date: May 27, 2012
TL* THE CONTACT OWNS A 2000 WINNEBAGO BRAVE SE RV. THE CONTACT STATED WHILE DRIVING 40 MPH, HE REALIZED THAT THE BRAKES WERE INOPERABLE. THE CONTACT ASSUMED THAT THE FAILURE WAS CAUSED BY A LACK OF BRAKE FLUID. THE CONTACT WAS ABLE TO REGAIN BRAKING POWER AFTER SEVERAL MINUTES. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THEY STATED THAT THE BRAKE SYSTEM WOULD NEED REPLACING BECAUSE IT HAD OVERHE
... ATED AND SEIZED. THE MANUFACTURER WAS CONTACTED BUT PROVIDED NO ASSISTANCE. THE FAILURE MILEAGE WAS 260,000 AND THE CURRENT 600,800.Read more
Incident date: Jul 18, 2006
TL* THE CONTACT OWNS A NORCOLD REFRIGERATOR, MODEL NUMBER: 1201LRIMWPM WHICH WAS HOUSED IN A 2007 WINNEBAGO JOURNEY MOTOR HOME. THE CONTACT STATED THAT THE REFRIGERATOR WAS LEAKING AMMONIA. THE REFRIGERATOR WAS LOCATED IN THE REAR CENTER OF THE VEHICLE. A DEALER WAS CONTACTED WHO ADVISED THAT THE REFRIGERATOR WAS NOT UNDER RECALL AND OFFERED NO FURTHER ASSISTANCE. THE MANUFACTURER WAS NOT NOTIFI
... ED OF THE FAILURE. THE FAILURE MILEAGE WAS 38,000. UPDATED 07/10/12*LJ THE CONSUMER STATED THE REFRIGERATOR WAS HOT, SINCE THE FIRST DAY OF PURCHASE. ON SEPTEMBER 16, 2006 THE REFRIGERATOR COMPLETELY STOPPED WORKING. THE DEALERSHIP REPAIRED IT, BUT IT NEVER FUNCTIONED PROPERLY. THE REFRIGERATOR STOPPED WORKING AGAIN FOR THE SECOND TIME. THE CONSUMER OBTAINED THE PARTS AND WAS ABLE TO FIX IT, BUT THE EXTERIOR WAS STILL TOO HOT. ABOUT A WEEK LATER, THE CONSUMER PULLED THE REFRIGERATOR OUT AND DISCOVERED THAT BOTH COOLING FANS WERE NOT WORKING PROPERLY AND PART OF THE THERMAL INSULATION WAS MISSING. NORCOLD DIDN'T WANT TO DO ANYTHING ABOUT THE ISSUE, UNTIL WINNEBAGO BECAME INVOLVED. AFTER WINNEBAGO BECAME INVOLVED, NORCOLD REPLACED THE FANS AND SENT ADDITIONAL INSULATION. UPDATE 07/11/12. *JB THE CONSUMERS LAWYER WROTE IN ON BEHALF OF THE CONSUMER. UNDER THE RECALL, THE COOLING UNIT WAS RETROFITTED WITH A THERMAL SWITCH KIT THAT WAS SUPPOSED TO PROTECT THE COOLING UNIT FROM LEAKING. UNFORTUNATELY, THE REPAIR WAS INEFFECTIVE AS THE UNIT CONTINUED TO LEAK REFRIGERANT. UPDATED 08/09/12Read more
Incident date: Jul 18, 2006
TL* THE CONTACT OWNS A NORCOLD REFRIGERATOR, MODEL NUMBER: 1201LRIMWPM WHICH WAS HOUSED IN A 2007 WINNEBAGO JOURNEY MOTOR HOME. THE CONTACT STATED THAT THE REFRIGERATOR WAS LEAKING AMMONIA. THE REFRIGERATOR WAS LOCATED IN THE REAR CENTER OF THE VEHICLE. A DEALER WAS CONTACTED WHO ADVISED THAT THE REFRIGERATOR WAS NOT UNDER RECALL AND OFFERED NO FURTHER ASSISTANCE. THE MANUFACTURER WAS NOT NOTIFI
... ED OF THE FAILURE. THE FAILURE MILEAGE WAS 38,000. UPDATED 07/10/12*LJ THE CONSUMER STATED THE REFRIGERATOR WAS HOT, SINCE THE FIRST DAY OF PURCHASE. ON SEPTEMBER 16, 2006 THE REFRIGERATOR COMPLETELY STOPPED WORKING. THE DEALERSHIP REPAIRED IT, BUT IT NEVER FUNCTIONED PROPERLY. THE REFRIGERATOR STOPPED WORKING AGAIN FOR THE SECOND TIME. THE CONSUMER OBTAINED THE PARTS AND WAS ABLE TO FIX IT, BUT THE EXTERIOR WAS STILL TOO HOT. ABOUT A WEEK LATER, THE CONSUMER PULLED THE REFRIGERATOR OUT AND DISCOVERED THAT BOTH COOLING FANS WERE NOT WORKING PROPERLY AND PART OF THE THERMAL INSULATION WAS MISSING. NORCOLD DIDN'T WANT TO DO ANYTHING ABOUT THE ISSUE, UNTIL WINNEBAGO BECAME INVOLVED. AFTER WINNEBAGO BECAME INVOLVED, NORCOLD REPLACED THE FANS AND SENT ADDITIONAL INSULATION. UPDATE 07/11/12. *JB THE CONSUMERS LAWYER WROTE IN ON BEHALF OF THE CONSUMER. UNDER THE RECALL, THE COOLING UNIT WAS RETROFITTED WITH A THERMAL SWITCH KIT THAT WAS SUPPOSED TO PROTECT THE COOLING UNIT FROM LEAKING. UNFORTUNATELY, THE REPAIR WAS INEFFECTIVE AS THE UNIT CONTINUED TO LEAK REFRIGERANT. UPDATED 08/09/12Read more
Incident date: Apr 11, 2012
I AM THE OWNER OF A 2008 WINNEBAGO SIGHTSEER WITH A WORKHORSE W18 CHASSIS WHICH WAS PURCHASED NEW IN 2009. ON 4/11/12, I HAD AN ABS WARNING LIGHT ON THE DASHBOARD THAT DISPLAYED AN INDICATION TO "CHECK ABS!" AND TOOK IT TO CHILHOWEE RV ON 4/14/12. AFTER INSPECTION OF THE CHASSIS AND FRONT WHEELS, CHILHOWEE DETERMINED THAT THE ABS SENSOR ON THE DRIVER FRONT WHEEL HAD BURNED OUT DUE TO OVERHEATING O
... F THE WHEEL. THE FRONT BRAKES HAD EXCESSIVELY WORN PADS AND A SCORCHED ROTOR, CALIPERS WOULDN'T RELEASE, AND BRAKE LINE WAS NOT RELEASING FLUID CAUSED BY A COLLAPSED BRAKE LINE AND/OR CALIPER DEFECT. THE REAR BRAKES WERE INSPECTED AND FOUND TO BE IN GOOD SHAPE. MY WORKHORSE WARRANTY DOESN'T EXPIRE UNTIL 7/7/12. CHILHOWEE RV SUBMITTED A WARRANTY CLAIM TO WORKHORSE AND PROVIDED ALL NECESSARY EXPLANATIONS AND PICTURES TO DOCUMENT THE CLAIM. WORKHORSE CLAIMS OFFICE DENIED THE CLAIM BECAUSE OF OPERATOR FAILURE -- "SOUNDS LIKE SOMEONE DROVE DOWN A HILL WITH THE FOOT ON THE BRAKE"; AND "IT IS A DRIVER/VEHICLE OPERATION FAILURE AND AS SUCH NOT A WORKHORSE WARRANTY REPAIR." THE REPAIRS WERE FINALLY COMPLETED ON 5/30/12 WITH A TOTAL COST OF $4,490.03. PARTS CAN ONLY BE PURCHASED THROUGH WORKHORSE WHICH AMOUNTED TO $3,418.70. IN THE END, WORKHORSE TURNED A $3,418.70 DEBT INTO A $3,418.70 PROFIT. THERE ARE PROBABLY THOUSANDS OF W18 CHASSIS IN SERVICE WITH THIS POTENTIAL DEFECT. YOU DO THE MATH ON HOW MUCH MONEY WORKHORSE CAN MAKE BY DENYING CLAIMS AND SELLING REPLACEMENT PARTS WHILE PUTTING LIVES AT RISK. THERE HAVE BEEN 31 BRAKE RECALLS ISSUED BY WORKHORSE OVER THE PAST 10 YEARS FOR W20/21/22 CHASSIS WITH EXACTLY THE SAME BRAKE PROBLEMS. THE REPAIR INVOICE FROM CHILHOWEE RV, WORKHORSE REGISTRATION OF MY RV, WORKHORSE WARRANTY STATEMENT, ALL THE E-MAILS BETWEEN CHILHOWEE RV AND WORKHORSE, PICTURES OF THE DEFECTIVE PARTS AND THE DEFECTIVE PARTS THEMSELVES ARE AVAILABLE UPON REQUEST. *TRRead more
Incident date: Dec 28, 2011
SIX MORE INCIDENTS OF ENGINE ACCELERATION - NOW A TOTAL OF EIGHT 28 DEC 2011WATERLOO, IA 1:13 PM @ 5548 MILES. AFTER COMING TO A STOP AND PLACING SHIFT LEVER IN PARK, ENGINE SPED UP TO 2800 RPM THEN BACK TO IDLE. DURATION 2 TO 3 SECONDS. 4 JAN 2012 SOUTH OF WACO, TX GOING SOUTH ON I-35 NEAR EXIT 320 @ 1:10 PM WITH 6780 MILES ON ODOMETER. CRUISE CONTROL SET TO 60 MPH FOR SOME TIME GOIN
... G UP AND DOWN GRADES AND EVEN ON MODERATE GRADES RPM ONLY WENT TO 3800 RPM. THIS TIME ON A SLIGHT GRADE, ENGINE RACED FROM 2500 RPM TO 5000 RPM FOR 4 TO 5 SECONDS THEN BACK TO NORMAL. FEET WERE NOT ON ANY PEDALS. 4 JAN 2012 AT 1:35 PM ON I-35 NEAR EXIT 300 WITH 6805 MILES ON ODOMETER AND WITH CRUISE CONTROL SET TO 60 MPH, ENGINE RACED FROM 2400 RPM TO 5100 RPM FOR ABOUT 3 SECONDS THEN BACK TO NORMAL. SLIGHT INCLINE WITH FEET OFF OF ALL PEDALS. 4 JAN 2012 AT 1:43 PM ON I-35 NEAR EXIT 293 WITH 6811 MILES ON ODOMETER AND CRUISE CONTROL STILL SET AT 60 MPH. UPON APPROACHING A STEEPER GRADE, ENGINE RAPIDLY SPED UP FROM 2400 RPM TO 3400, TO 3800, TO 4300, TO 5200 RPM WITH THIS TOTAL SEQUENCE TAKING ABOUT 3 SECONDS. FEET OFF BOTH PEDALS; AS IT IS MY USUAL CUSTOM WHEN ON CRUISE CONTROL. 2 FEB 2012AT 2:36 PM GOING NORTH ON I-35 [KS TURNPIKE IN WICHITA] WITH 8246 MILES ON ODOMETER AND CRUISE CONTROL SET TO 70 MPH AND OPERATING NORMALLY AT 2600 RPM, IT WAS DISENGAGED FOR ABOUT 1 MINUTE BY DRIVER. UPON PRESSING THE RESUME BUTTON ENGINE RACED DIRECTLY TO 5100 RPM FOR ABOUT 30 SECONDS THEN BACK TO 2600 RPM. ALL OTHER RE-ENGAGEMENTS BY RESUME FUNCTIONS WERE UNDER 4200 RPM. 3 FEB 20126:50 PM ON I-35 TWO MILES SOUTH OF ALBERT LEE MN AND CRUISE CONTROL SET AT 60 MPH. ON A SLIGHT INCLINE ENGINE RACED FROM 2200 RPM DIRECTLY TO 5100 RPM FOR ABOUT 15 SECONDS. NOTE: TWO PRIOR INCIDENTS REPORTED IN NHTSA ODI ID NO.: 10453149. *TRRead more
Incident date: Dec 28, 2011
SIX MORE INCIDENTS OF ENGINE ACCELERATION - NOW A TOTAL OF EIGHT 28 DEC 2011WATERLOO, IA 1:13 PM @ 5548 MILES. AFTER COMING TO A STOP AND PLACING SHIFT LEVER IN PARK, ENGINE SPED UP TO 2800 RPM THEN BACK TO IDLE. DURATION 2 TO 3 SECONDS. 4 JAN 2012 SOUTH OF WACO, TX GOING SOUTH ON I-35 NEAR EXIT 320 @ 1:10 PM WITH 6780 MILES ON ODOMETER. CRUISE CONTROL SET TO 60 MPH FOR SOME TIME GOIN
... G UP AND DOWN GRADES AND EVEN ON MODERATE GRADES RPM ONLY WENT TO 3800 RPM. THIS TIME ON A SLIGHT GRADE, ENGINE RACED FROM 2500 RPM TO 5000 RPM FOR 4 TO 5 SECONDS THEN BACK TO NORMAL. FEET WERE NOT ON ANY PEDALS. 4 JAN 2012 AT 1:35 PM ON I-35 NEAR EXIT 300 WITH 6805 MILES ON ODOMETER AND WITH CRUISE CONTROL SET TO 60 MPH, ENGINE RACED FROM 2400 RPM TO 5100 RPM FOR ABOUT 3 SECONDS THEN BACK TO NORMAL. SLIGHT INCLINE WITH FEET OFF OF ALL PEDALS. 4 JAN 2012 AT 1:43 PM ON I-35 NEAR EXIT 293 WITH 6811 MILES ON ODOMETER AND CRUISE CONTROL STILL SET AT 60 MPH. UPON APPROACHING A STEEPER GRADE, ENGINE RAPIDLY SPED UP FROM 2400 RPM TO 3400, TO 3800, TO 4300, TO 5200 RPM WITH THIS TOTAL SEQUENCE TAKING ABOUT 3 SECONDS. FEET OFF BOTH PEDALS; AS IT IS MY USUAL CUSTOM WHEN ON CRUISE CONTROL. 2 FEB 2012AT 2:36 PM GOING NORTH ON I-35 [KS TURNPIKE IN WICHITA] WITH 8246 MILES ON ODOMETER AND CRUISE CONTROL SET TO 70 MPH AND OPERATING NORMALLY AT 2600 RPM, IT WAS DISENGAGED FOR ABOUT 1 MINUTE BY DRIVER. UPON PRESSING THE RESUME BUTTON ENGINE RACED DIRECTLY TO 5100 RPM FOR ABOUT 30 SECONDS THEN BACK TO 2600 RPM. ALL OTHER RE-ENGAGEMENTS BY RESUME FUNCTIONS WERE UNDER 4200 RPM. 3 FEB 20126:50 PM ON I-35 TWO MILES SOUTH OF ALBERT LEE MN AND CRUISE CONTROL SET AT 60 MPH. ON A SLIGHT INCLINE ENGINE RACED FROM 2200 RPM DIRECTLY TO 5100 RPM FOR ABOUT 15 SECONDS. NOTE: TWO PRIOR INCIDENTS REPORTED IN NHTSA ODI ID NO.: 10453149. *TRRead more
Incident date: Jul 1, 2008
I HAVE A 2005 WINNEBAGO JOURNEY 39F MOTORHOME. SINCE THE MOTORHOME WAS TWO YEARS OLD (IT SAT ON THE DEALER'S LOT, IN THE OPEN, FOR ONE YEAR BEFORE I PURCHASED IT) WHILE DRIVING IN THE RAIN, WATER DRIPS ONTO THE DASH FROM ABOVE THE LEFT (DRIVER'S) WINDSHIELD. I CONTACTED WINNEBAGO AND THEY SAID TO PUT SILICON AROUND THE LIGHTS ABOVE THE WINDSHIELD, WHICH I DID. THE CONDITION REMAINS THE SAME. T
... HE INTERNET HAS REPORTED THAT THE METAL FRAME AROUND THE GLASS RUSTS OUT CAUSING THE LEAKS. I WORRY THAT THE ENTIRE WINDOW FRAME HAS RUSTED OUT WITH THE POSSIBILITY OF THE WINDOW BREAKING OR COMING LOOSER. THE VAST NUMBER OF COMPLAINTS ABOUT THIS SPECIFIC PROBLEM LEADS TO THE OBVIOUS CONCLUSION THAT THERE IS A DEFECT IN THE DESIGN AND/OR CONSTRUCTION OF THE WINDSHIELD FRAMES. THANK YOU *TRRead more
Incident date: Jul 1, 2008
I HAVE A 2005 WINNEBAGO JOURNEY 39F MOTORHOME. SINCE THE MOTORHOME WAS TWO YEARS OLD (IT SAT ON THE DEALER'S LOT, IN THE OPEN, FOR ONE YEAR BEFORE I PURCHASED IT) WHILE DRIVING IN THE RAIN, WATER DRIPS ONTO THE DASH FROM ABOVE THE LEFT (DRIVER'S) WINDSHIELD. I CONTACTED WINNEBAGO AND THEY SAID TO PUT SILICON AROUND THE LIGHTS ABOVE THE WINDSHIELD, WHICH I DID. THE CONDITION REMAINS THE SAME. T
... HE INTERNET HAS REPORTED THAT THE METAL FRAME AROUND THE GLASS RUSTS OUT CAUSING THE LEAKS. I WORRY THAT THE ENTIRE WINDOW FRAME HAS RUSTED OUT WITH THE POSSIBILITY OF THE WINDOW BREAKING OR COMING LOOSER. THE VAST NUMBER OF COMPLAINTS ABOUT THIS SPECIFIC PROBLEM LEADS TO THE OBVIOUS CONCLUSION THAT THERE IS A DEFECT IN THE DESIGN AND/OR CONSTRUCTION OF THE WINDSHIELD FRAMES. THANK YOU *TRRead more
Incident date: Feb 3, 2012
I TRIED TWO DAYS AGO BUT MY MEMO DID NOT GO THRU. MY REFERENCE # 447680 WHILE IN AN I95 REST STOP IN SANTEE, SC MY UNIT BROKE INTO FLAMES WHEN THE GENERATOR WAS STARTED TO MAKE COFFEE. I WAS ABLE TO EXTINGUISH THE FIRE AND CALL 911. SANTEE FD RESPONDED QUICKLY. AFTER CHECKING THE UNIT CAREFULLY AND TURNING OFF THE BATTERIES TO THE HOUSE PORTION THEY CLEARED ME TO DRIVE HOME TO RICHMOND, VA T
... HIS FIRE WAS IN AN INACCESSIBLE AREA BEHIND THE WALL UNDER THE BATHROOM SINK. I AM A SENIOR AND AN AMPUTEE THIS COULD HAVE BEEN A DISASTER. *TRRead more
Fire
Incident date: May 3, 2012
THIS RV WAS BOUGHT IN NOV 2011, FROM THE DEALER AND DROVE IT HOME ABOUT 3 MILES DISTANCE. DRIVING AT 40MPH, I FELT THERE WAS ALOT OF POWER STEERING AND I FOUGHT THE STEERING TO STAY IN MY LANE.THE VEHICLE WAS STORED IN MY DRIVEWAY FOR THE WINTER MONTHS. FREQUENT TURNING ENGINE TO WARM UP AND SHORELINE HOOKED TO HOUSE POWER. MAY3, 2012, I, WIFE AND ADULT SON DEPARTED TO WILLIAMS, AZ ABOUT 130 MILE
... S FOR CAMPING AT A FEDERAL CAMP SITE. I DROVE MOSTLY ON THE BACK ROADS AND AVOIDED THE I-HIGHWAY 40. OVER 40 MPH I COULD SENSE THAT THIS VEC. HAS ALOT OF POWER STEERING, AND UP TO 60 MPH. I COULD NOT CONTROL THE STEERING AT ALL..THE VEC. WAS GOING WHERE IT WANTED TO GO EITHER LEFT OR RIGHT AND I HAD TO COUNTER THIS BY TURNING SLIGHTLY BACK INTO THE PROPER LANE. AT TIMES, ON COMING VEC. WOULD SWAY TO THEIR RIGHT, AS THIS RV WAS OVER THE CENTER LINE AND I HAD TO COMPENSATED THE STEERING. WE EXITED THE BACK ROAD AND ENTERED THE I-40 HWY. AND, I FOUGHT THE STEERING CONTROL AGAIN UNTIL WE REACH THE FED. CAMP SITE(KAIBAB LAKE, WILLIAMS,AZ) MAY 11, 2012, WE JOURNEYED BACK HOME. AGAIN, DRIVING ABOUT 20 MILES ON I-40, UNTIL WE GOT BACK ONTO THE BACK ROAD OF ROUTE66...FOLLOWING DAY, I CALLED AN RV REPAIR SHOP ABOUT MY STEERING PROBLEM AND TOOK IN THAT, SAME MORNING FOR AN INSPECTION. FEW HOURS LATER, THE RV TECHNICIAN CALLED AND STATED THAT, I HAD NO STEERING STABILIZER. I ASKED, IF IT WAS A MANUFACTURERS DEFECT.. HE AGAIN STATED, THAT THERE ISN'T ANY STEERING STABILIZER..THEIR IS NO WARRANTY, ON THIS USED VEC. BOUGHT NOV 2011. AND, DRIVEN FOR A LONG TRIP FOR THE 1ST TIME ON MAY 3, AND AGAIN FOR THE RTN TRIP MAY 11. I AM NOW PAYING FOR A BILL THAT, NEARLY COST ME AND MY FAMILIES LIFE. VEC. IS A 2007 WINNEBAGO SIGHTSEER 28P, CHEV MOTOR, GAS, WORKHORSE CHASIS. VIN: [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Apr 19, 2012
TL* THE CONTACT OWNS A 2005 WINNEBAGO SUN CRUISER. THE CONTACT WAS DRIVING 53 MPH WHEN THE WINDSHIELD FRACTURED. THE CONTACT ATTEMPTED TO HAVE THE WINDOW REPAIRED BUT DUE TO RUST, THE GLASS COULD NOT BE PROPERLY SEALED INTO THE CHANNEL. THE VEHICLE WAS REPAIRED. THE FAILURE MILEAGE WAS 41,000 AND THE CURRENT MILEAGE WAS 41,200. THE VIN WAS NOT AVAILABLE.
Incident date: May 8, 2012
WE HAVE A WATER LEAK AT THE TOP OF THE WINDSHIELD AND THERE APPEARS TO BE A SMALL AMOUNT OF RUST STARTING IN THE UPPER PASSENGER SIDE CORNER. *TR
Incident date: May 8, 2012
WE HAVE A WATER LEAK AT THE TOP OF THE WINDSHIELD AND THERE APPEARS TO BE A SMALL AMOUNT OF RUST STARTING IN THE UPPER PASSENGER SIDE CORNER. *TR
Incident date: Jun 1, 2011
TL* THE CONTACT OWNS A 2004 WINNEBAGO JOURNEY MOTOR HOME. THE CONTACT STATED THAT THE MOTOR HOME EMITTED A STRONG PROPANE ODOR. THE CONTACT ALSO NOTICED THAT THE PROPANE TANK HAD A HOLE IN THE BRACKET MOUNTING AREA DUE TO DEFECTIVE WELDING. THE MANUFACTURER DENIED ASSISTANCE WITH THE REPAIR. THE MOTOR HOME WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 55,000 AND THE CURRENT MILEAGE WAS 65,000. THE VIN
... WAS UNAVAILABLE.Read more
Incident date: Mar 5, 2012
WINDSHIELD FRAME RUSTED CAUSING WINDSHIELD TO BECOME LOOSE. I FIND FLAKES OF RUST ON THE DASH. POSSIBLE SAFETY ISSUE. *JS
Incident date: Apr 11, 2012
THE LEFT SIDE THE ROOF CAME LOOSE SITTING IN STORAGE FROM WINDS OF A LESSER SPEED THAN IF ONE WAS DRIVING 55 MPH. THERE HAS BEEN CASES WHERE THE ROOF ON THESE MODELS HAVE CAME LOOSE WHILE DRIVING. THE ROOF MEMBRANE IS BIG ENOUGH TO BLOCK A FOLLOWING VEHICLES VIEW IF IT WERE TO COME OFF IN TRAFFIC. THIS IS A COMMON PROBLEM FOR THIS MODEL YEAR. IT IS CAUSED BY IMPROPER INSTALLATION AT THE FACTORY. T
... HIS PROBLEM NEEDS TO BE ADDRESSED BEFORE A DEATH OCCURS DUE TO THIS MALFUNCTIONING BODY PART. LAWS IN SOME STATES ARE VERY STRICT IN SECURING LOADS, THIS MALFUNCTION SHOULD BE ADDRESSED BY WINNEBAGO. *TRRead more
Incident date: May 21, 2011
RUNAWAY FORD V-10 ENGINE IN A 2010 WINNEBAGO OUTLOOK RV INCIDENT # 1 - 21 MAY 2011 - CANON FALLS MN WE WERE ON OUR WAY BACK ON HWY52 COMING TO A STOP LIGHT IN CANON FALLS AND I WAS SLOWING DOWN FROM REGULAR HWY SPEEDS 60-65MPH. I DIDN'T NOTICE ANYTHING DIFFERENT UNTIL I WAS GOING AROUND 10-15 MPH. I THEN NOTICED THE RV'S BRAKES DID NOT SEEM TO BE SLOWING US DOWN LIKE NORMAL AND THEN I COULD HE
... AR THE ENGINE ROARING SO I LOOKED AT THE RPM'S AND IT WAS STILL SOMEWHERE BETWEEN 2000-3000RPM.S AND NOT GOING DOWN AT ALL. I WAS PUSHING THE BRAKE ALL THE WAY TO THE FLOOR STILL PROBABLY JUST GOING 5MPH OR SO AND IT DID NOT FEEL LIKE IT WAS GOING TO STOP. ALL OF THE SUDDEN IT JUST SLOWED QUICKLY THE LAST FEW FEET AS I WAS ALMOST IN THE INTERSECTION THE ENGINE STILL ROARING AND ONCE IT STOPPED I QUICKLY PUT IT IN NEUTRAL AND THEN THE RPM'S WENT DOWN BACK TO NORMAL. I SHIFTED BACK INTO DRIVE AND IT WORKED THE REST OF THE WAY HOME WITH OUT ANY PROBLEMS. INCIDENT # 2 - 19 JUNE 2011- SAVAGE MINNESOTA WHILE SLOWING DOWN [LESS THAN 20 MPH] TO A STOP AND BRAKING, RV WOULD NOT SLOW FOR A STOP. HAD TO "STAND" ON BRAKE TO HOLD IT BACK, BUT IT WOULD NOT STOP!. PUT IT IN NEUTRAL, ENGINE RACED TO 4000+ RPM, TURNED KEY OFF, RV STOPPED. UPON RESTART ALL OK??? 2ND INCIDENT OF THIS SAFETY PROBLEM [ABOVE GIVEN TO FORD RV CUSTOMER ASSISTANCE]. *TRRead more
Incident date: Feb 1, 2011
STRUCTURAL ROOM SLIDE GEARS, AND TEETH CORRODED OFF MAKING THE ROOM UNABLE TO FULLY LOCK INTO PLACE. WE BELIEVE THIS COULD CAUSE THE ROOM TO SHIFT OPEN DURING TRAVEL. *TR
Incident date: Feb 1, 2011
STRUCTURAL ROOM SLIDE GEARS, AND TEETH CORRODED OFF MAKING THE ROOM UNABLE TO FULLY LOCK INTO PLACE. WE BELIEVE THIS COULD CAUSE THE ROOM TO SHIFT OPEN DURING TRAVEL. *TR
Incident date: Dec 1, 2000
TL* THE CONTACT OWNS A 1999 WINNEBAGO MINNIE WINNIE RV. THE CONTACT STATED THAT A FAULTY SUSPENSION SYSTEM CAUSED REPEATED TIRE FAILURES. THERE WERE APPROXIMATELY SEVEN TIRE FAILURES IN WHICH THE STEEL BELTS AND THE TREAD WOULD SUFFER EXCESSIVE WEAR. THE VEHICLE WAS TAKEN TO AN INDEPENDENT REPAIR SHOP AND THEY WERE UNABLE TO DIAGNOSE THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS
... NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 7,000. THE VIN WAS UNAVAILABLE.Read more
Incident date: Feb 11, 2010
TL* THE CONTACT OWNS A 2002 WINNEBAGO ITASCA RV. THE CONTACT STATED THAT BOTH OF THE SIDE DOUBLE PANE WINDOWS WERE BECOMING CLOUDY, CAUSING REDUCED VISIBILITY OF THE ROADWAY. THE VEHICLE WAS NOT TAKEN TO THE DEALER FOR INSPECTION OR REPAIRS. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE AND ADVISED THE CONTACT TO PURCHASE NEW WINDOWS FOR THE VEHICLE. THE VEHICLE W
... AS NOT REPAIRED. THE FAILURE AND THE CURRENT MILEAGE WAS 63,500.Read more
Incident date: Feb 6, 2004
TL* THE CONTACT OWNS A 2002 WINNEBAGO SIGHTSEER RV WITH A WORKHORSE CHASSIS, MODEL NUMBER: WPD27C. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 20 MPH AND DEPRESSING THE BRAKES, HE NOTICED SMOKE COMING FROM THE WHEELS. AFTER INSPECTING THE VEHICLE, HE DISCOVERED THAT THE BRAKES WERE EXTREMELY HOT TO THE TOUCH. THE CONTACT HAD TO WAIT APPROXIMATELY 2-3 HOURS BEFORE THE BRAKES COOLED OFF. THE
... VEHICLE WAS TAKEN TO THE DEALER WHERE THEY ADVISED HIM THAT HE NEEDED TO REPLACE ALL OF THE BENNIX BRAKE CALIPERS. THE VEHICLE HAD NOT BEEN REPAIRED. THE MANUFACTURER WAS CONTACTED AND THEY OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 14,000.Read more
Incident date: Dec 14, 2011
TL* THE CONTACT OWNS A 2006 WINNEBAGO ADVENTURER RV. THE CONTACT STATED THAT THERE WAS A LARGE FRACTURE ON THE FRAME. THE VEHICLE WAS INSPECTED BY A DEALER AND THEY ADVISED THE CONTACT THAT THE FRAME HAD BEEN WELDED ONTO THE VEHICLE. THE MANUFACTURER WAS CONTACTED AND THEY OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 68,000.
Incident date: May 10, 2011
THIS COACH CAN NOT BE LOADED TO CAPACITY ADVERTISED WITHOUT OVER LOADING STEER TIRE RATING. STEER TIRES ARE RATED FOR 14300 #'S , AND GVWR OF 44300 #'S. HOWEVER, WITH FUEL FULL, WATER AT 1/3, PROPANE FULL, AND A GROSS WEIGHT OF 38000 #'S (MOST HEAVY CARGO TOWARD REAR) THE STEER AXLE WEIGHT IS 14620 #'S. THIS CREATES AN UNSAFE SITUATION. WINNEBAGO REFUSES TO FIX PROBLEM. *TR
Incident date: Oct 1, 2009
TL* THE CONTACT OWNS A 2002 WINNEBAGO ITASCA RV. THE CONTACT STATED THAT BOTH OF THE FRONT DOUBLE PAINTED WINDOWS FAILED. THE CONTACT MENTIONED THAT MOISTURE WAS GETTING BETWEEN THE PAINT CAUSING THE WINDOWS TO FOG AND OBSTRUCTED HIS VISIBILITY. THE VEHICLE WAS NOT TAKEN TO A DEALER. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE. THE VEHICLE WAS NOT REPAIRED. THE
... FAILURE MILEAGE WAS 45,000 AND THE CURRENT MILEAGE WAS 61,000. UPDATED 03/05/12*LJ THE CONSUMER STATED THE MANUFACTURER'S ORIGINAL DOUBLE PANE WINDOWS IN THE DRIVER'S COMPARTMENT ON BOTH SIDE OF THE RV WERE BECOMING PROGRESSIVELY OCCLUDED DUE TO THE FAILURE OF THE SEAL THAT WAS SUPPOSED TO PREVENT AIR/MOISTURE. ETC, FROM GETTING BETWEEN THE GLASS PANES. THE CONSUMER STATED HE WAS UNABLE TO SEE THROUGH EITHER OF THE FRONT SIDE WIDOWS. UPDATED 03/08/12Read more