Showing 15,069 complaints for VOLVO
Incident date: May 26, 2017
TL* THE CONTACT OWNS A 2002 VOLVO S80. WHILE DRIVING 30 MPH, THE ACCELERATOR PEDAL TRAVELED TO THE FLOORBOARD AND SMOKE APPEARED UNDER THE HOOD. THE VEHICLE WAS TAKEN TO SEVERAL UNKNOWN INDEPENDENT MECHANICS WHO DETERMINED THAT THE FUEL PUMP NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 160,000.
Fire
Incident date: May 26, 2017
TL* THE CONTACT OWNS A 2002 VOLVO S80. WHILE DRIVING 30 MPH, THE ACCELERATOR PEDAL TRAVELED TO THE FLOORBOARD AND SMOKE APPEARED UNDER THE HOOD. THE VEHICLE WAS TAKEN TO SEVERAL UNKNOWN INDEPENDENT MECHANICS WHO DETERMINED THAT THE FUEL PUMP NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 160,000.
Fire
Incident date: Jun 13, 2017
SUNROOF BLEW UP, OR SPONTANEOUSLY COMBUSTED. WAS NOT HIT BY AN OBJECT, LOUD SOUND WAS HEARD PRIOR TO THE INCIDENT. CAR WAS IN MOTION AT THE TIME, GOING ABOUT 60MPH. CONDITIONS CLEAR, COOL TEMPERATURES NOT VERY HOT OR COLD OUTSIDE.
Incident date: Jun 12, 2017
CAR EXPERIENCES PREDETONATION/PREIGNITION OF THE SPARK PLUGS. THIS CAUSES THE TIMING TO BE RETARDED, CAUSING A VERY DANGEROUS LACK OF POWER, I HAVE TAKEN THE CAR IN 7X FOR RESOLUTION, THEY HAVE REBUILT THE ENGINE, ISSUE IS REOCCURRING. VOLVO CARS OF NA IS DOING NOTHING TO RESOLVE THE ISSUE. THERE ARE MULTIPLE REPORTS OF THIS ISSUE ON THE INTERNET (SWEEDESPEED ETHUSIAST FORUM) AS WELL AS MANY OTHER
... EXAMPLES OF THIS YET, ONCE AGAIN, VOLVO CARS NA IS REFUSING TO ADDRESS OR RESOLVE THIS ISSUE RESULTING IN A DANGER TO THE AMERICAN PUBLIC. I HAVE INCLUDED THE LETTER I SENT TO SCOTT DOERING, VP OF CUSTOMER SERVICE, HE HAD ONE OF HIS TEAM CALL ME TODAY TO DENY MY REQUEST TO EXTEND THE WARRANTY OR RESOLVE THE ISSUE. IN MY LETTER IS THE CHRONOLOGY OF SERVICE VISITS, OF WHICH I ALSO HAVE THE RECEIPTS. *JSRead more
Incident date: Jun 14, 2017
I AM 88 YEARS OLD AND DEPEND ON THIS VEHICLE ( OUR ONLY VEHICLE) AS MY TRANSPORTATION FOR MYSELF MY SON AND MY 15 YEAR OLD GREAT GRAND DAUGHTER. MORE TIMES THAN I CARE TO REMEMBER THIS CAR HAS STALLED OUT ON ROUTE 50, WHERE I WAS TRAVELING 50 TO 55 MILES AN HOUR. I LIVE ABOUT 1 HOUR AWAY FROM OCEAN CITY, MARYLAND. EACH TIME IS TERRIFYING. SOMETIMES IT ONLY TAKES A FEW MINUTES TO RESTART AND THEN
... THERE ARE TIMES WHERE IT HAS TAKEN OVER AN HOUR. THE LATEST EVENT WAS 6/14/2017. I HAVE HAD THIS CAR FOR A YEAR. THIS PROBLEM ONLY OCCURS WHEN IN MOTION. THERE HAVE BEEN A FEW TIMES WHEN IT DID NOT START FOR A WHILE BUT IT IS TERRIFYING WHEN IT STALLS OUT ON THE HIGHWAY.Read more
Incident date: Apr 27, 2017
TL* THE CONTACT OWNS A 1993 VOLVO 240 STATION WAGON. WHILE WAITING FOR ONCOMING TRAFFIC TO PASS TO PULL INTO THE DRIVEWAY, THE DRIVER'S SIDE AIR BAG DEPLOYED WITHIN THE STEERING WHEEL. THE AIR BAG DEPLOYED WITH FORCE AND EMITTED A GRAY SUBSTANCE. THE VEHICLE WAS PULLED INTO THE CONTACT'S DRIVEWAY AND THE MANUFACTURER WAS NOTIFIED WEEKS LATER. THE DRIVER SUSTAINED MINOR BRUISING, WHICH REQUIRED MED
... ICAL ATTENTION. THE VEHICLE WAS NOT INCLUDED IN NHTSA ACTION NUMBER: EA94015 (AIR BAGS) AND NHTSA ACTION NUMBER: PE93095 (AIR BAGS). IN ADDITION, THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 94V185000 (AIR BAGS), ALTHOUGH THE FAILURES WERE IDENTICAL. THE VIN AND FAILURE MILEAGE WERE NOT AVAILABLE.Read more
1 injured
Incident date: Jun 12, 2017
I BOTH THE VOLVO 780 SEMI TRUCK 8 MONTHS AGO AND I DO STILL HAVE A PROBLEM. I DO REPLACE WHOLE SUSPENSION, MAKE A 6 TIMES ALIGNMENT AND TRUCK STILL SWAY IN THE ROAD. DEALER FROM CONNECTICUT DO TEST DRIVE AND HE SAID MY WHOLE CAB SWAY FROM RIGHT TO THE LEFT. HE RECOMMENDED REPLACEMENT CAB SHOCKS AND I DID, JUST WHOLE CAB IT'S SWAY ANY WAY. POOR WATHER LIKE WIND IT'S IS DIFFICULT DRIVING, ROAD ZONE
... NOT EVEN LANE IT'S TERRIBLE AND AWCORSE IN THE TAKE A CURVE I HAVE TO SLOW DOWN TO THE MINIMUM SPEED, MAKE A DENGER FOR OTHER DRIVER. I WILL BE PUT TRUCK FOR SHOP DO INVESTIGATION, JUST I'M PUT IN ALMOST $10.000 FOR REPAIR LIKE I DO NOT HAVE TO REPLACE MY WHOLE SUSPENSION AND OTHER STUFF, ALSO I STILL HAVE A TRUCK PAYMENT AND INSURANCE AND I HAVE TO TO RUN. LIKE I READ OTHER COMPLAIN, OTHER DRIVERS HAVE A SIMILAR PROBLEM. PLESE DO SOMETHING. TRULY WESLEY O/O . HAVE A NICE DAYRead more
Incident date: Jun 2, 2017
TL* THE CONTACT OWNS A 2010 VOLVO V70. THE CONTACT STATED THAT THE ANTI-THEFT TAMPER DEVICE FAILED AND IMPACTED THE RADIATOR. THE CONTACT INDICATED THAT THE MANUFACTURER EXCLUDED THE VEHICLE FROM A SERVICE CAMPAIGN. THE CONTACT WAS UNABLE TO DETERMINE IF THE DEALER'S SOLUTION WOULD REPAIR THE VEHICLE. A WARNING INDICATOR ILLUMINATED TO SERVICE THE ENGINE AND SERVICE LOSS OF POWER. THE VEHICLE WAS
... TAKEN TO THE DEALER (VOLVO CARS CAPE COD, 270 NORTH ST, HYANNIS, MA 02601, 508-815-5400) FOR DIAGNOSTIC TESTING. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 90,000.Read more
Incident date: Jun 2, 2017
TL* THE CONTACT OWNS A 2010 VOLVO V70. THE CONTACT STATED THAT THE ANTI-THEFT TAMPER DEVICE FAILED AND IMPACTED THE RADIATOR. THE CONTACT INDICATED THAT THE MANUFACTURER EXCLUDED THE VEHICLE FROM A SERVICE CAMPAIGN. THE CONTACT WAS UNABLE TO DETERMINE IF THE DEALER'S SOLUTION WOULD REPAIR THE VEHICLE. A WARNING INDICATOR ILLUMINATED TO SERVICE THE ENGINE AND SERVICE LOSS OF POWER. THE VEHICLE WAS
... TAKEN TO THE DEALER (VOLVO CARS CAPE COD, 270 NORTH ST, HYANNIS, MA 02601, 508-815-5400) FOR DIAGNOSTIC TESTING. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 90,000.Read more
Incident date: Jun 8, 2017
WINDSHIELD WATER LEAK AT GASKET, ABOVE THE STEERING WEEL AREA.
Incident date: Jun 9, 2017
THE RECALL STATES: IMPROPERLY FUNCTIONING ON-BOARD EMISSION-RELATED DIANOTIC SYSTEM THAT VIOLATES CALIFORNIA AND FEDERAL STANDARD AND REGULATIONS.
Incident date: Jun 7, 2017
TL* THE CONTACT OWNS A 2005 VOLVO XC90. THE CONTACT STATED THAT THE VEHICLE RANDOMLY STALLED WITHOUT WARNING. THE VEHICLE WAS TOWED AND PARKED ON THE CONTACT'S STREET DUE TO THE FAILURE. THE MANUFACTURER WAS NOTIFIED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS NOT AVAILABLE.
Incident date: Jun 7, 2017
TL* THE CONTACT OWNS A 2005 VOLVO XC90. THE CONTACT STATED THAT THE VEHICLE RANDOMLY STALLED WITHOUT WARNING. THE VEHICLE WAS TOWED AND PARKED ON THE CONTACT'S STREET DUE TO THE FAILURE. THE MANUFACTURER WAS NOTIFIED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS NOT AVAILABLE.
Incident date: Feb 18, 2017
MY HUSBAND, MOTHER-IN-LAW, AND THREE YEAR OLD SON WERE DRIVING IN THE VEHICLE SATURDAY, FEBRUARY 18TH, 2017. AS MY HUSBAND TURNED DOWN OUR ROAD HE STATED HE SMELLED SMOKE, BUT DIDN'T REALIZE IT WAS COMING FROM THE VEHICLE. HE PULLED INTO OUR DRIVEWAY AND PARKED. THEY THEN SAW SMOKE SEEPING OUT OF THE HOOD. MY MOTHER-IN-LAW EXITED AND MY HUSBAND REMOVED MY SON FROM THE BURNING CAR. I CAME OUTSIDE T
... O GREET THEM AND WITNESSED THIS. HE THEN OPENED THE HOOD AND THERE WERE SIGNIFICANT FLAMES ON THE DRIVER SIDE POSTERIOR AREA OF THE ENGINE. HE RAN FOR OUR FIRE EXTINGUISHER WHILE I CALLED 911. HE PUT OUT THE FIRE WITH THE EXTINGUISHER AND THE FIRE DEPARTMENT ARRIVED WITHIN FIVE MINUTES. THEY INSPECTED, OPENED THE TOP COVER OF THE BATTERY AND DISCONNECTED IT. THEY REPORTED TO US THAT IT APPEARED TO BE AN ELECTRICAL FIRE OCCURRING AT THE AREA OF THE BATTERY. AFTER INSPECTION BY VOLVO AND OUR INSURANCE COMPANY, THE DAMAGE WAS DETERMINED TO BE CAUSED BY RODENTS CHEWING ON THE ELECTRICAL WIRING INSIDE THE ENGINE CAUSING THE SHORTAGE AND SUBSEQUENT FIRE. THE DAMAGE WAS VALUED AND PAID AT A COST OF $11,000 (COVERED BY INSURANCE AFTER DEDUCTIBLE). THERE ARE MULTIPLE ARTICLES INDICATING ATTRACTION OF RODENTS TO THE NEWER SOY-BASED ELECTRICAL WIRE INSULATION. HTTPS://WWW.FORBES.COM/SITES/MICHAELDUNNE/2017/02/19/RATS-NEW-CARS-SOY-COATED-WIRES-GIVE-RODENTS-PLENTY-TO-CHEW-ON/#2C8BCBD780AB HTTP://WWW.NBCLOSANGELES.COM/NEWS/LOCAL/CLASS-ACTION-LAWSUIT-ALLEGES-RODENTS-CHEWING-EATING-CAR-WIRING-393480601.HTML WE ARE CONCERNED FOR FUTURE USE AND FOR THE SAFETY OF OTHERS.Read more
Fire
Incident date: Feb 18, 2017
MY HUSBAND, MOTHER-IN-LAW, AND THREE YEAR OLD SON WERE DRIVING IN THE VEHICLE SATURDAY, FEBRUARY 18TH, 2017. AS MY HUSBAND TURNED DOWN OUR ROAD HE STATED HE SMELLED SMOKE, BUT DIDN'T REALIZE IT WAS COMING FROM THE VEHICLE. HE PULLED INTO OUR DRIVEWAY AND PARKED. THEY THEN SAW SMOKE SEEPING OUT OF THE HOOD. MY MOTHER-IN-LAW EXITED AND MY HUSBAND REMOVED MY SON FROM THE BURNING CAR. I CAME OUTSIDE T
... O GREET THEM AND WITNESSED THIS. HE THEN OPENED THE HOOD AND THERE WERE SIGNIFICANT FLAMES ON THE DRIVER SIDE POSTERIOR AREA OF THE ENGINE. HE RAN FOR OUR FIRE EXTINGUISHER WHILE I CALLED 911. HE PUT OUT THE FIRE WITH THE EXTINGUISHER AND THE FIRE DEPARTMENT ARRIVED WITHIN FIVE MINUTES. THEY INSPECTED, OPENED THE TOP COVER OF THE BATTERY AND DISCONNECTED IT. THEY REPORTED TO US THAT IT APPEARED TO BE AN ELECTRICAL FIRE OCCURRING AT THE AREA OF THE BATTERY. AFTER INSPECTION BY VOLVO AND OUR INSURANCE COMPANY, THE DAMAGE WAS DETERMINED TO BE CAUSED BY RODENTS CHEWING ON THE ELECTRICAL WIRING INSIDE THE ENGINE CAUSING THE SHORTAGE AND SUBSEQUENT FIRE. THE DAMAGE WAS VALUED AND PAID AT A COST OF $11,000 (COVERED BY INSURANCE AFTER DEDUCTIBLE). THERE ARE MULTIPLE ARTICLES INDICATING ATTRACTION OF RODENTS TO THE NEWER SOY-BASED ELECTRICAL WIRE INSULATION. HTTPS://WWW.FORBES.COM/SITES/MICHAELDUNNE/2017/02/19/RATS-NEW-CARS-SOY-COATED-WIRES-GIVE-RODENTS-PLENTY-TO-CHEW-ON/#2C8BCBD780AB HTTP://WWW.NBCLOSANGELES.COM/NEWS/LOCAL/CLASS-ACTION-LAWSUIT-ALLEGES-RODENTS-CHEWING-EATING-CAR-WIRING-393480601.HTML WE ARE CONCERNED FOR FUTURE USE AND FOR THE SAFETY OF OTHERS.Read more
Fire
Incident date: Jun 6, 2017
ALREADY HAD TO REPLACE PASSENGER SIDE REAR SPRING AND NOW HAVE TO REPLACE BOTH FRONT SPRINGS. THEY HAVE ALL BROKEN WILL DRIVING ON CITY STREETS. REPLACED THE REAR 11/2015. WILL BE REPLACING BOTH FRONT SPRINGS 6/2017.
Incident date: Jan 1, 2016
THIS PARTICULAR MODEL HAS A PROBLEM WITH FUEL TANKS CRACKING. IT ISN'T HAPPENING TO THE ONES THAT AREN'T ALL WHEEL DRIVE. I NEED MINE REPLACED. PEOPLE ARE APPREHENSIVE ABOUT PULLING A USED TANK FROM A YARD BECAUSE IT MIGHT ALSO BE CRACKED. I WAS TOLD THE ALL WHEEL DRIVE SYSTEM BUILT AROUND IT IS PUTTING PRESSURE ON IT.
Incident date: Mar 22, 2017
I OWNED A 1986 240 GL VOLVO 4 DOOR SEDAN. ONE NIGHT LAST MONTH MY WIFE WAS DRIVING HOME AND WITHIN A BLOCK OF OUR HOUSE SHE NOTICED A FIRE ON THE BACK OF THE CAR. THE DRIVER'S SIDE TAIL LIGHT WAS ON FIRE. I CONTACTED VOLVO USA AND ABOUT A MONTH LATER THEY HAD AN "EXPERT" INSPECT OUR CAR. THEY WILL NOT GIVE ME A WRITTEN REPORT. THE EXECUTIVE, JOSEPH (
[email protected]) CALLED ME AND LEF
... T A MESSAGE SAYING THAT WE HAD TOO LARGE OF A FUSE IN THE FUSE BLOCK AND THIS IS WHAT CAUSED THE FIRE. I'VE TRIED REPEATEDLY TO TELL THEM THAT TOO LARGE OF A FUSE DIDN'T CAUSE THE DEAD SHORT FIRE ON OUR TAIL LIGHT. I GOOGLED TAIL LIGHT FIRES ON VOLVO'S AND FOUND SEVERAL PAGES. I'VE HAD TO SCRAP THE CAR. THE TOW TRUCK DRIVER WASN'T SHOCKED TO SEE THE MELTED TAIL LIGHT ON MY VOLVO. HE TOLD ME HE HAD A 1984 VOLVO JUST LIKE MINE AS HIS FIRST CAR. HE SAID HIS TOO HAD THE SAME MELTED TAIL LIGHT FIRE AS MINE.Read more
Fire
Incident date: May 5, 2017
THE PASSENGER SIDE HEAD LIGHT WHILE I WAS DRIVING HOME FROM WORK BULB WENT OUT HAD MESSAGE STATING BULB FAILURE REPLACED BULBS AND WITHIN 2 DAYS. LIGHTS WERE OUT AGAIN AND THE WIRING CONNECTED TO HEAD LIGHTS WERE FRAYED AS IF THEY HAD SHORTED OUT OR HAD MELTED AND THE BACK SIDE SIGNAL ON PASSENGER SIDE STOPPED WORKING THE CAR WAS BEING DRIVEN AT THAT TIME
Incident date: May 5, 2017
THE PASSENGER SIDE HEAD LIGHT WHILE I WAS DRIVING HOME FROM WORK BULB WENT OUT HAD MESSAGE STATING BULB FAILURE REPLACED BULBS AND WITHIN 2 DAYS. LIGHTS WERE OUT AGAIN AND THE WIRING CONNECTED TO HEAD LIGHTS WERE FRAYED AS IF THEY HAD SHORTED OUT OR HAD MELTED AND THE BACK SIDE SIGNAL ON PASSENGER SIDE STOPPED WORKING THE CAR WAS BEING DRIVEN AT THAT TIME
Incident date: May 1, 2015
TL* THE CONTACT OWNS A 2011 VOLVO XC60. WHILE DRIVING AT AN UNKNOWN SPEED, THE CONTACT LOST CONTROL OF THE VEHICLE AND CRASHED. THE FRONT END OF THE VEHICLE WAS SEVERELY DAMAGED, BUT THE AIR BAGS DID NOT DEPLOY. A POLICE REPORT WAS FILED AND THERE WERE NO INJURIES. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 50,000.
Crash
Incident date: May 2, 2017
THE CAR WAS CONSUMING OIL AT A SHOCKING RATE - 12 QUARTS OVER THE COURSE OF 2 MONTHS AND THE OIL LIGHT DID NOT ILLUMINATE, EVEN WHEN THE ENGINE WAS COMPLETELY OUT OF OIL! I OPENED A CASE WITH VOLVO USA AT THE TIME AND WAS TOLD TO BRING THE CAR TO A DEALER. THE DEALER COULD NOT FIND A LEAK AND DID NOT RESOLVE THE PROBLEM. I RETURNED TO THE DEALER AGAIN FOR THE SAME ISSUE AND IT WAS STILL NOT RES
... OLVED. A FEW WEEKS AFTER MY MOST RECENT VISIT TO THE DEALER, THE CAR MADE A LOUD NOISE WHILE IN TRAFFIC GOING ABOUT 30 MPH. THE CAR WAS DEAD IN THE MIDDLE OF ATLANTA TRAFFIC. IT TURNS OUT THE ENGINE "THREW A ROD" AND THE ENTIRE ENGINE WOULD NEED TO BE REPLACED ($11K)! THIS CAR HAS 78K MILES ON IT. I AGAIN REACHED OUT TO VOLVO USA AND WAS TOLD THAT ALL GOODWILL REPAIRS WERE AT THE DISCRETION OF THE DEALER AND THE DEALER DID NOT FEEL ANY ASSISTANCE WAS IN ORDER IN THIS CASE. AT THIS TIME I HAVE A VERY GOOD LOOKING AND EXPENSIVE BOAT ANCHOR IN MY DRIVEWAY. AFTER READING MANY SIMILAR COMPLAINTS ON THIS SITE, I HAVE ONCE AGAIN REACHED OUT TO VOLVO USA FOR ASSISTANCE. THERE IS OBVIOUSLY A PROBLEM WITH THE 2012 S60 T5 ENGINE.Read more
Incident date: May 5, 2017
TL* THE CONTACTS GIRLFRIEND OWNS A 2005 VOLVO S80. THE CONTACT STATED THAT WHILE THE BRAKE PEDAL WAS DEPRESSED, THE VEHICLE WAS DIFFICULT TO STOP. THE CONTACT STATED THAT HE HAD TO APPLY PRESSURE WITH FORCE IN ORDER TO STOP. THE CONTACT ALSO STATED THAT THE ENGINE STALLED. THE ABS AND THE CHECK ENGINE WARNING LIGHTS ILLUMINATED. THE CONTACT CALLED THE LOCAL DEALER AT ONTARIO VOLVO AT PHONE NUMBER:
... 909-230-9653 AND THE DEALER STATED THAT THE VEHICLE WAS NOT INCLUDED IN ANY RECALL. THE VEHICLE WAS NOT DIAGNOSED. THE CONTACT STATED THAT HE REPLACED THE BRAKES. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 106,000.Read more
Incident date: Dec 25, 2012
THE RADIATOR FAN RAN CONSISTENTLY ALTHOUGH I WAS DRIVING IN THE WINTER COMING BACK FROM LAKE TAHOE. WHILE DRIVING ON THE HIGHWAY A SMELL OF BURNED RUBBER STARTED TO SPREAD INSIDE THE CAR SO I IMMEDIATELY SLOWED DOWN AND PARKED IT ON THE EMERGENCY LANE. AFTER OPENING THE HOOD, A FIRE CAME OUT. THE ENTIRE FAN MELTED AS A RESULT OF OVERHEATED DUE TO IT RUNNING NONSTOP.
Incident date: Apr 20, 2017
POSIBLE TASKATA RECALL AIR BAG LIGHT ON/ENGINE MISSING BAD/TRANMISSION SHIFT FAST AND HARD-SUN ROOF DON'T WORKS HAD TUNE-UP DONE CHANGE TURBO CHARGER REPLACED/REPLACED TROLLDER BODY-REPLACE THE RADIATOR BETWEEN AND A/C EVAPORATOR THAT CONNECT FROM TURBO AND TROLLER BODY ROUGH IDLEING WHILD STARTING AND DRIVING ON THE CITY STREETS. I WOULD ASK THE POWER TRAIN AND THE SPEED CONTROL TO INCLUDE THE E
... LECTRICAL SYSTEM BE REVIEWED FOR SERVICE AND ANY UNKNOWN OR OTHER.Read more
Incident date: Apr 20, 2017
POSIBLE TASKATA RECALL AIR BAG LIGHT ON/ENGINE MISSING BAD/TRANMISSION SHIFT FAST AND HARD-SUN ROOF DON'T WORKS HAD TUNE-UP DONE CHANGE TURBO CHARGER REPLACED/REPLACED TROLLDER BODY-REPLACE THE RADIATOR BETWEEN AND A/C EVAPORATOR THAT CONNECT FROM TURBO AND TROLLER BODY ROUGH IDLEING WHILD STARTING AND DRIVING ON THE CITY STREETS. I WOULD ASK THE POWER TRAIN AND THE SPEED CONTROL TO INCLUDE THE E
... LECTRICAL SYSTEM BE REVIEWED FOR SERVICE AND ANY UNKNOWN OR OTHER.Read more
Incident date: Apr 20, 2017
POSIBLE TASKATA RECALL AIR BAG LIGHT ON/ENGINE MISSING BAD/TRANMISSION SHIFT FAST AND HARD-SUN ROOF DON'T WORKS HAD TUNE-UP DONE CHANGE TURBO CHARGER REPLACED/REPLACED TROLLDER BODY-REPLACE THE RADIATOR BETWEEN AND A/C EVAPORATOR THAT CONNECT FROM TURBO AND TROLLER BODY ROUGH IDLEING WHILD STARTING AND DRIVING ON THE CITY STREETS. I WOULD ASK THE POWER TRAIN AND THE SPEED CONTROL TO INCLUDE THE E
... LECTRICAL SYSTEM BE REVIEWED FOR SERVICE AND ANY UNKNOWN OR OTHER.Read more
Incident date: May 23, 2017
MY VOLVO S80 SPONTANEOUSLY COMBUSTED IN MY DRIVEWAY, WHEN I WAS AWAY FROM HOME. THE CAR HAD NOT BEEN DRIVEN FOR APPROXIMATELY TWO HOURS, WHEN IT CAUGHT FIRE (UNDER THE HOOD) AND BURNED.
Fire
Incident date: Apr 10, 2017
TL* THE CONTACT OWNS A 2002 VOLVO V70. WHILE DRIVING, THE EXTERIOR LIGHTING FAILED TO ILLUMINATE, WHICH INCLUDED THE HEADLIGHTS, BRAKE LIGHTS, AND TURN SIGNALS. THE "POSITION LIGHT FAILURE, STOP LIGHT AND MULTIPLE BULBS FAILURE" MESSAGE APPEARED ON THE INSTRUMENT PANEL. THE CONTACT STATED THAT THE HEADLIGHT BULBS HAD BEEN REPLACED SEVERAL TIMES. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO
... DISCOVERED THAT SEVERAL LIGHT SOCKETS WERE MELTED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 80,000.Read more
Fire
Incident date: Jan 3, 2017
AT LEAST 3 TIMES, MY CAR HAS BRAKED ITSELF (AT AROUND 50 MILES PER HOUR) WHEN THERE WAS NOTHING IN FRONT OF ME. THIS WAS VERY UNSAFE- IF SOMEONE HAD BEEN BEHIND ME, I WOULD HAVE BEEN HIT. THIS SEEMS TO BE THE COLLISION MITIGATION SYSTEM ENGAGING FOR NO REASON. THE DEALER HAS SAID THEY "FIXED IT" (DON BEYER VOLVO) BUT I BELIEVE THEY HAVE JUST TURNED THE SYSTEM PRETTY MUCH OFF SO THAT IT NOW WOULD N
... OT STOP IF THERE WAS A REAL OBJECT IN FRONT OF ME. I HAD A LOANER IN WHICH THE SYSTEM WAS STILL ON AND MINE NO LONGER WORKS LIKE THAT. I THINK THEY DON'T REALLY HAVE A FIX FOR THIS SO THEY JUST TURN IT OFF IN THE CARS THAT HAVE THIS DEFECT. THIS IS A MAJOR SAFETY ISSUE. ALSO, HAVE HAD THE NAVIGATION SYSTEM GO BLANK WHILE DRIVING THEN IT SHOWS THAT YOU ARE SOMEWHERE ELSE AND GET STUCK THERE FOR DAYS. (MANY OTHER PROBLEMS ALSO, A NOISE IN THE SEAT (SECOND ROW) THAT THEY MAYBE FIXED AFTER THREE TIMES BUT NOW THE SECOND ROW SEAT DOES NOT WORK PROPERLY (GOT STUCK OUT OF THE SOCKET BUT WE GOT IT BACK IN AND I THINK THIS IS A SAFETY ISSUE.)Read more
Incident date: Jan 3, 2017
AT LEAST 3 TIMES, MY CAR HAS BRAKED ITSELF (AT AROUND 50 MILES PER HOUR) WHEN THERE WAS NOTHING IN FRONT OF ME. THIS WAS VERY UNSAFE- IF SOMEONE HAD BEEN BEHIND ME, I WOULD HAVE BEEN HIT. THIS SEEMS TO BE THE COLLISION MITIGATION SYSTEM ENGAGING FOR NO REASON. THE DEALER HAS SAID THEY "FIXED IT" (DON BEYER VOLVO) BUT I BELIEVE THEY HAVE JUST TURNED THE SYSTEM PRETTY MUCH OFF SO THAT IT NOW WOULD N
... OT STOP IF THERE WAS A REAL OBJECT IN FRONT OF ME. I HAD A LOANER IN WHICH THE SYSTEM WAS STILL ON AND MINE NO LONGER WORKS LIKE THAT. I THINK THEY DON'T REALLY HAVE A FIX FOR THIS SO THEY JUST TURN IT OFF IN THE CARS THAT HAVE THIS DEFECT. THIS IS A MAJOR SAFETY ISSUE. ALSO, HAVE HAD THE NAVIGATION SYSTEM GO BLANK WHILE DRIVING THEN IT SHOWS THAT YOU ARE SOMEWHERE ELSE AND GET STUCK THERE FOR DAYS. (MANY OTHER PROBLEMS ALSO, A NOISE IN THE SEAT (SECOND ROW) THAT THEY MAYBE FIXED AFTER THREE TIMES BUT NOW THE SECOND ROW SEAT DOES NOT WORK PROPERLY (GOT STUCK OUT OF THE SOCKET BUT WE GOT IT BACK IN AND I THINK THIS IS A SAFETY ISSUE.)Read more
Incident date: Jan 3, 2017
AT LEAST 3 TIMES, MY CAR HAS BRAKED ITSELF (AT AROUND 50 MILES PER HOUR) WHEN THERE WAS NOTHING IN FRONT OF ME. THIS WAS VERY UNSAFE- IF SOMEONE HAD BEEN BEHIND ME, I WOULD HAVE BEEN HIT. THIS SEEMS TO BE THE COLLISION MITIGATION SYSTEM ENGAGING FOR NO REASON. THE DEALER HAS SAID THEY "FIXED IT" (DON BEYER VOLVO) BUT I BELIEVE THEY HAVE JUST TURNED THE SYSTEM PRETTY MUCH OFF SO THAT IT NOW WOULD N
... OT STOP IF THERE WAS A REAL OBJECT IN FRONT OF ME. I HAD A LOANER IN WHICH THE SYSTEM WAS STILL ON AND MINE NO LONGER WORKS LIKE THAT. I THINK THEY DON'T REALLY HAVE A FIX FOR THIS SO THEY JUST TURN IT OFF IN THE CARS THAT HAVE THIS DEFECT. THIS IS A MAJOR SAFETY ISSUE. ALSO, HAVE HAD THE NAVIGATION SYSTEM GO BLANK WHILE DRIVING THEN IT SHOWS THAT YOU ARE SOMEWHERE ELSE AND GET STUCK THERE FOR DAYS. (MANY OTHER PROBLEMS ALSO, A NOISE IN THE SEAT (SECOND ROW) THAT THEY MAYBE FIXED AFTER THREE TIMES BUT NOW THE SECOND ROW SEAT DOES NOT WORK PROPERLY (GOT STUCK OUT OF THE SOCKET BUT WE GOT IT BACK IN AND I THINK THIS IS A SAFETY ISSUE.)Read more
Incident date: Apr 29, 2017
I WAS DEPARTING MY HOME VILLAGE ABOUT A BLOCK FROM MY HOME AND I HEARD A LOUD BANG IN THE FRONT DRIVER SIDE AT ABOUT 15 MPH!! NO BUMP.. NOTHING! I LOOKED UNDER THE CAR AND THERE WAS NO OBVIOUS ISSUE AT THE INITIAL LOOK AND I DROVE ANOTHER QUARTER MILE AND HEARD A SLIGHT GRIND OR NOISE ON SMALL BUMPS... THEN A CLANK. I BACKED UP AND THERE WAS A PIECE OF THE COIL SPRING ON THE ROAD!!!! THE FRONT LEF
... T - DRIVERS SIDE - COIL SPRING SNAPPED IN TWO. AT 101,000 MILES. THE CLEAN BREAK AND NO RUST OR UNUSUAL CORROSION INDICATES A FAULTY METAL. HOW CAN I TRUST THE VOLVO XC AGAIN!! SAFETY AND VOLVO ARE NO LONGER WORDS THAT SHOULD BE USED TOGETHER. MY COMPLAINTS TO VOLVO AMERICA WERE RESPONDED TO WITH NO CONSIDERATION TO THE MAGNITUDE OF THE ISSUE. VOLVO DID NOT STAND BEHIND THE OBVIOUS FLAW IN THE CONSTRUCTION OF THE VEHICLE. MANY OTHER COMPLAINTS ON NHTSA AND ONLINE FORUMS INDICATE A COMMON ISSUE WITH VOLVO XC SUSPENSION COIL SPRINGS. SO DANGEROUS!Read more
Incident date: May 18, 2017
MY VOLVO XC 90 CANNOT SHIFT TO PARK OR REVERSE, IT REMAINED IN DRIVE OR NEUTRAL POSITION. WAS UNABLE TO REMOVE KEYS FROM IGNITION DUE TO PROBLEM. IT IS A SAFETY HAZARD THAT WHEN I SEARCHED U-TUBE FOUND THERE WERE NUMEROUS PEOPLE THAT ENCOUNTERED THE SAME PROBLEM. IT JUST HAD A SERVICE 1 MONTH AGO
Incident date: May 18, 2017
MY VOLVO XC 90 CANNOT SHIFT TO PARK OR REVERSE, IT REMAINED IN DRIVE OR NEUTRAL POSITION. WAS UNABLE TO REMOVE KEYS FROM IGNITION DUE TO PROBLEM. IT IS A SAFETY HAZARD THAT WHEN I SEARCHED U-TUBE FOUND THERE WERE NUMEROUS PEOPLE THAT ENCOUNTERED THE SAME PROBLEM. IT JUST HAD A SERVICE 1 MONTH AGO
Incident date: May 13, 2017
VOLVO XC90 2016 HYBRID -SAFETY ISSUES AND TERRIBLE CUSTOMER SERVICE. I STARTED THE CAR AND MY BRAKES SUDDENLY MADE THIS WEIRD NOISE AND I COULD FEEL A SHIFT IN THE BRAKE PEDAL. UP POPPED A NOTICE ON THE SCREEN BY THE ODOMETER SAYING "BRAKE PEDAL CHARACTERISTICS CHANGED SERVICE REQUIRED." I STARTED TO DRIVE MY KIDS HOME, THINKING IT WAS JUST A SERVICE NOTICE AND NOT A TOW SITUATION. AS I DROVE
... ON TOWN ROADS (NOT HWY), THE BRAKE MADE A GRINDING SOUND (COULD ALSO FEEL IT IN THE PEDAL) WHEN LIGHTLY DEPRESSED AND WHEN I FULLY PRESSED THE BRAKE TO SLOW OR STOP, IT WOULDN'T DO ANYTHING AT FIRST AND THEN IT WOULD SUDDENLY ENGAGE IN A JOLTING AND JERKY STOP MOTION IT WAS VERY SCARY TO DRIVE THE CAR LIKE THIS. I WASN'T SURE IF THE BRAKES WERE GOING TO WORK WELL ENOUGH TO GET ME AND MY TWO CHILDREN HOME. FORTUNATELY, WE DID MAKE IT HOME BUT THE CAR IS NOT SAFE TO DRIVE LIKE THIS. VOLVO TOWED THE CAR OUT OF MY DRIVEWAY THIS AM. THE WESTPORT SERVICE DEPT CLAIMED THEY HAVE "NEVER HEARD OF THE ISSUE," DESPITE MY FINDING OF COUNTLESS SIMILAR COMPLAINTS ONLINE AND A NOTATION ABOUT IT IN THE MANUAL. I'VE ONLY HAD THIS VEHICLE FOR 6MO. IT WAS NEW OFF THE LOT.Read more
Incident date: Apr 11, 2017
I LEASE A 2017 VOLVO S90 WITH AUTO-BRAKE AND START/STOP TECHNOLOGY. RECENTLY I WAS IN MY DRIVEWAY AND PUT THE VEHICLE IN DRIVE. I ROLLED FORWARD A FEW FEET AND REALIZED I NEEDED TO EXIT THE VEHICLE FOR SOMETHING. I BECAME DISTRACTED DUE TO AN ITEM ON MY DRIVERS SEAT AND SINCE THE VEHICLES ENGINE WAS NOT RUNNING DUE TO START-STOP TECHNOLOGY I DID NOT REALIZE THAT THE CAR WAS STILL IN DRIVE AND
... THAT THE IGNITION WAS IN THE ON POSITION. I EXITED THE VEHICLE AND CLOSED THE DRIVERS DOOR. WHEN I DID SO , THE START-STOP TECHNOLOGY ENGAGED AND THE CAR DROVE OFF WITHOUT ME. THE ONLY THING THAT STOPPED THE CAR WAS THAT IT RAN INTO MY HOME. I BELIEVE THIS IS A HUGE SAFETY FLAW THAT VOLVO NEEDS TO CORRECT IMMEDIATELY. THE AUTO BRAKE BUTTON WAS NOT ENGAGED.Read more
Crash
Incident date: May 12, 2017
FUEL PUMP CONTROL MODULE (PEM) FAILS DURING WET CONDITIONS. CAR WILL CRANK LIKE NORMAL BUT WILL NOT START. LET CAR DRY OUT FOR A FEW DAYS AND THEN THE CAR WILL RUN NORMAL AGAIN.
Incident date: May 12, 2017
FUEL PUMP CONTROL MODULE (PEM) FAILS DURING WET CONDITIONS. CAR WILL CRANK LIKE NORMAL BUT WILL NOT START. LET CAR DRY OUT FOR A FEW DAYS AND THEN THE CAR WILL RUN NORMAL AGAIN.
Incident date: Oct 15, 2016
SERIOUS ENGINE SPEED SURGING. JUMPS TO OVER 8000 RPM. HAPPENS WHEN STOPPING ON OCTANE, NOT ALWAYS. I COULD HAVE GOT KILLED WHILE BACKING INTO MY DRIVEWAY ON A HILL. I HAVE SEEN THIS AT LEAST 4 TIMES AND WILL NOT DRIVE IT. I INFORMED MY INSURER. AT DEALER NOW, THEY SAY THEY HAVE NEVER HEARD OF THIS AND CANNOT DUPLICATE. LOTS OF INFO ON WEB FROM OTHERS WHO HAVE SAME PROBLEM. IT SEEMS TO BE A THROTTL
... E CONTROL ISSUE AND CLASS ACTION SUIT HAS BEEN DONE ON YEARS JUST UP TO 2016. VOLVO HAVE EXTENDED WARRANTY FOR THE THROTTLE MODULE AND ECM. I ASKED THE DEALER TO RESEARCH ON THIS AND IF THEY CANNOT DUPLICATE THAN REPLACE THE LIKELY SUSPECT AND SOFTWARE AS WELL AS CONTACT VOLVO FOR HELP. IF THIS IS A KNOWN ISSUE, VOLVO NEEDS GET INFO OUT AS SOMEONE IS GOING TO GET HURT OR DIE DUE TO THIS KNOWN DEFECT AND SHOULD PAY FOR THE REPAIRS. I LOVE THE CARE BUT WILL NOT DRIVE IT AS IT IS. 63K MILES ON IT. PLEASE FEEL FREE TO CALL OR EMAIL. THANKS [XXX] [XXX] [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6).*JBRead more
Incident date: May 7, 2017
IMPROPER DRAINING ROUTE WHICH IN RESULT CAUSES MOLD AND DAMAGE TO FLOOR MATS AND SEAT CUSHIONS IN RAINY WEATHER. TRANSMISSION FLUID HAS HIGHER ACIDITY LEVELS. COOLANT REGULARLY FALLS BELOW MINIMUM LEVEL REQUIRED.
Incident date: May 7, 2017
IMPROPER DRAINING ROUTE WHICH IN RESULT CAUSES MOLD AND DAMAGE TO FLOOR MATS AND SEAT CUSHIONS IN RAINY WEATHER. TRANSMISSION FLUID HAS HIGHER ACIDITY LEVELS. COOLANT REGULARLY FALLS BELOW MINIMUM LEVEL REQUIRED.
Incident date: May 7, 2017
IMPROPER DRAINING ROUTE WHICH IN RESULT CAUSES MOLD AND DAMAGE TO FLOOR MATS AND SEAT CUSHIONS IN RAINY WEATHER. TRANSMISSION FLUID HAS HIGHER ACIDITY LEVELS. COOLANT REGULARLY FALLS BELOW MINIMUM LEVEL REQUIRED.
Incident date: May 4, 2017
1) ADAPTIVE CRUISE CONTROL SUDDENLY SHUTS OFF WHILE DRIVING ON THE HIGHWAY, ERROR MESSAGE APPEARS ON THE SCREEN: "WINDSCREEN SENSOR, SENSOR BLOCKED, SEE OWNER'S MANUAL", THE APPEARANCE OF THE SENSOR ON THE OUTSIDE OF THE CAR APPEARS CLEAN AND EVEN AFTER SCRUBBING THE SENSOR AREA THE ERROR STILL OCCURS. THE CAR HAS BEEN REPAIRED FOR THIS SAME PROBLEM OVER 5 TIMES INCLUDING TOTAL REPLACEMENT OF THE
... THE WINDSCREEN SENSORS, WITH THE PROBLEM STILL PERSISTING. 2) DASHBOARD WENT BLANK AND COMPUTER REBOOTED WHILE DRIVING.Read more
Incident date: May 4, 2017
1) ADAPTIVE CRUISE CONTROL SUDDENLY SHUTS OFF WHILE DRIVING ON THE HIGHWAY, ERROR MESSAGE APPEARS ON THE SCREEN: "WINDSCREEN SENSOR, SENSOR BLOCKED, SEE OWNER'S MANUAL", THE APPEARANCE OF THE SENSOR ON THE OUTSIDE OF THE CAR APPEARS CLEAN AND EVEN AFTER SCRUBBING THE SENSOR AREA THE ERROR STILL OCCURS. THE CAR HAS BEEN REPAIRED FOR THIS SAME PROBLEM OVER 5 TIMES INCLUDING TOTAL REPLACEMENT OF THE
... THE WINDSCREEN SENSORS, WITH THE PROBLEM STILL PERSISTING. 2) DASHBOARD WENT BLANK AND COMPUTER REBOOTED WHILE DRIVING.Read more
Incident date: May 4, 2017
1) ADAPTIVE CRUISE CONTROL SUDDENLY SHUTS OFF WHILE DRIVING ON THE HIGHWAY, ERROR MESSAGE APPEARS ON THE SCREEN: "WINDSCREEN SENSOR, SENSOR BLOCKED, SEE OWNER'S MANUAL", THE APPEARANCE OF THE SENSOR ON THE OUTSIDE OF THE CAR APPEARS CLEAN AND EVEN AFTER SCRUBBING THE SENSOR AREA THE ERROR STILL OCCURS. THE CAR HAS BEEN REPAIRED FOR THIS SAME PROBLEM OVER 5 TIMES INCLUDING TOTAL REPLACEMENT OF THE
... THE WINDSCREEN SENSORS, WITH THE PROBLEM STILL PERSISTING. 2) DASHBOARD WENT BLANK AND COMPUTER REBOOTED WHILE DRIVING.Read more
Incident date: May 1, 2017
TAKATA RECALL: A RECALL FAILURE OCCURRED MAY 1, 2017 ON A FAN CONTROL MODULE THAT WAS INSTALLED ON 7/22/2009-RCALL NUMBER 214. . THE RECALL WAS DONE BUT NOW THE RECALL PART HAS FAILED AGAIN. DEALERSHIP IS NOT WILLING TO PAY FOR IT AGAIN..
Incident date: Mar 30, 2017
ACCELERATING ON INTERSTATE AND ALL OF A SUDDEN COMPLETY LOST ENGINE POWER. ENGINE WOULD CONTINUE RUNNING, BUT WOULD NOT ACCELERATE. COULD HAVE EASILY GOTTEN INTO A WRECK IF THERE HAD BEEN MORE TRAFFIC ON THE INTERSTATE. ENDED UP GETTING TOWED AND HAVING TO REPLACE THE THROTTLE UNIT WHICH COST ALMOST $1000, THIS COULD HAVE BEEN A VERY DANGEROUS SITUATION WITH A VERY BAD OUTCOME IF TRAFFIC HAD B
... EEN HEAVIER.Read more
Incident date: Feb 3, 2017
ALUMINUM NUTS ON THE VALVE STEMS COMPLETELY DISINTEGRATE AND FALL APART CAUSING TIRES TO GO FLAT WHILE DRIVING. THIS HAPPENED ON TWO OCCASIONS (TWO TIRES) WHILE DRIVING DOWN THE HIGHWAY. LUCKILY WE WERE ABLE TO GET OFF THE ROAD QUICKLY WITHOUT INCIDENT. ALL 4 VALVE STEMS WERE INSPECTED
Incident date: Apr 25, 2017
DASHBOARD WENT BLACK AND COMPUTER REBOOTED THREE TIMES WHILE DRIVING. ENGINE WAS NOT AFFECTED. NO SPEEDOMETER AND GAUGES, AS THEY ARE ALL PART OF THE ELECTRONIC DASHBOARD.