Showing 6,583 complaints for SUZUKI
Incident date: Sep 25, 2013
THE MAGNETS ON THE FLYWHEEL CAME OFF AND SHATTERED CAUSING THE MOTORCYCLE TO DIE. *TR
Incident date: Sep 25, 2013
THE MAGNETS ON THE FLYWHEEL CAME OFF AND SHATTERED CAUSING THE MOTORCYCLE TO DIE. *TR
Incident date: Oct 3, 2013
TL* THE CONTACT OWNS A 2001 SUZUKI GRAND VITARA. THE CONTACT STATED THAT WHILE DRIVING 35 MPH, HE CRASHED INTO ANOTHER VEHICLE. THE AIR BAGS FAILED TO DEPLOY UNTIL AFTER IMPACT. THE CONTACT SUSTAINED INJURIES TO THE CHEST AND STERNUM WHILE THE PASSENGER SUSTAINED A FACIAL INJURY FROM STRIKING THE WINDSHIELD. THE CONTACT AND THE PASSENGER WERE BOTH TRANSPORTED TO A HOSPITAL. A POLICE REPORT WAS NOT
... FILED. THE VEHICLE WAS DESTROYED. THE CONTACT DID NOT CALL THE MANUFACTURER REGARDING THE AIR BAG FAILURE. THE FAILURE MILEAGE WAS 85,000.Read more
Crash
2 injured
Incident date: Oct 23, 2011
THE IGNITION ROTOR HAS A SERIES OF MAGNETS GLUED TO IT BUT THAT GLUE FAILED CAUSING THE MAGNETS TO COME LOOSE AND BREAK APART IN THE ENGINE CAUSE FRAGMENTS TO GO ALL OVER INSIDE THE ENGINE. WHAT I HAVE READ ON THE SUZUKI FORUMS THIS IS A COMMON OCCURRENCE. *TR
Incident date: Oct 23, 2011
THE IGNITION ROTOR HAS A SERIES OF MAGNETS GLUED TO IT BUT THAT GLUE FAILED CAUSING THE MAGNETS TO COME LOOSE AND BREAK APART IN THE ENGINE CAUSE FRAGMENTS TO GO ALL OVER INSIDE THE ENGINE. WHAT I HAVE READ ON THE SUZUKI FORUMS THIS IS A COMMON OCCURRENCE. *TR
Incident date: Oct 3, 2013
TL* THE CONTACT OWNS A 2001 SUZUKI GRAND VITARA. THE CONTACT WAS TRAVELING APPROXIMATELY 35 MPH AND CRASHED INTO ANOTHER VEHICLE. THE AIR BAGS FAILED TO DEPLOY UNTIL MOMENTS AFTER IMPACT. THE PASSENGER WAS PROPELLED INTO THE WINDSHIELD AND SUSTAINED INJURIES TO THE KNEE, FINGERS AND FACE. THE CONTACT SUSTAINED INJURIES TO THE STERNUM. A POLICE REPORT WAS FILED. THE VEHICLE WAS NEITHER DIAGNOSED NO
... R REPAIRED TO DETERMINE THE AIR BAG FAILURE. THE MANUFACTURER WAS CONTACTED ABOUT THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 85,000. THE VIN WAS UNAVAILABLE. UPDATED 12/24/13*CNRead more
Crash
2 injured
Incident date: Oct 4, 2013
TL* THE CONTACT OWNS A 2008 SUZUKI XL7. THE CONTACT STATED THAT WHILE DRIVING 40 MPH, THE POWER STEERING ASSIST FAILED AND THE STEERING WHEEL COULD NOT BE TURNED. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOT NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 64,000.
Incident date: Jan 1, 2012
TL* THE CONTACT OWNS A 2006 SUZUKI FORENZA. THE CONTACT STATED THAT THE TRANSMISSION WARNING LIGHT ILLUMINATED AND CAUSED THE GEARS TO ENGAGE WITH FORCE. AS A RESULT, THE ENGINE OVERHEATED. THE VEHICLE WAS TAKEN TO THE DEALER, WHO REPLACED THE TRANSMISSION RANGE SENSOR HOWEVER, THE FAILURE WAS NOT CORRECTED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE
... MILEAGE WAS 102,000 AND THE CURRENT MILEAGE WAS 145,000.Read more
Incident date: Oct 5, 2006
WE PURCHASED A 2006 SUZUKI GRAND VITARA LUXURY IN 2006. WE HAD THE CAR ABOUT 6 MONTHS AND NOTICED THE BACK TIRES WERE WEARING FASTER THAN NORMAL, ALSO THERE WAS THIS GRINDING SOUND WHEN YOU BRAKE, IT WAS SPORADIC. FROM 2006 TILL 2012 WE WERE GIVEN DOZENS OF REASONS WHY AND SOLUTIONS FOR A COST, NONE OF THEM FIXED THE PROBLEM. THE LAST COMPLAINT IN 2012 WE REFUSED TO LEAVE THE DEALERSHIP (ONE OF TH
... E TWO IN NORTHERN CALIFORNIA THAT WOULD STILL ALLOW YOU TO BRING IN A SUZUKI) UNTIL WE WERE GIVEN A ANSWER, WE WERE TOLD IT IS A INHERENT PROBLEM WITH THE CAR AND THERE IS NOTHING THAT COULD BE DONE? OVER THE YEARS THE BRAKES HAVE BEEN CHECKED SO MUCH I CANT COUNT. IS IT THE ESP SYSTEM? AS TIME HAS PASSED IT HAS ONLY GOTTEN LOUDER. WE DON'T KNOW WHERE ELSE TO TURN, WE JUST WANT A ANSWER! SUZUKI KNOWS WHAT IT IS AND THEY ARE NOT TELLING ANYONE, THIS IS NOT ONLY IRRESPONSIBLE IT IS POTENTIALLY DANGEROUS. *TRRead more
Incident date: Oct 5, 2006
WE PURCHASED A 2006 SUZUKI GRAND VITARA LUXURY IN 2006. WE HAD THE CAR ABOUT 6 MONTHS AND NOTICED THE BACK TIRES WERE WEARING FASTER THAN NORMAL, ALSO THERE WAS THIS GRINDING SOUND WHEN YOU BRAKE, IT WAS SPORADIC. FROM 2006 TILL 2012 WE WERE GIVEN DOZENS OF REASONS WHY AND SOLUTIONS FOR A COST, NONE OF THEM FIXED THE PROBLEM. THE LAST COMPLAINT IN 2012 WE REFUSED TO LEAVE THE DEALERSHIP (ONE OF TH
... E TWO IN NORTHERN CALIFORNIA THAT WOULD STILL ALLOW YOU TO BRING IN A SUZUKI) UNTIL WE WERE GIVEN A ANSWER, WE WERE TOLD IT IS A INHERENT PROBLEM WITH THE CAR AND THERE IS NOTHING THAT COULD BE DONE? OVER THE YEARS THE BRAKES HAVE BEEN CHECKED SO MUCH I CANT COUNT. IS IT THE ESP SYSTEM? AS TIME HAS PASSED IT HAS ONLY GOTTEN LOUDER. WE DON'T KNOW WHERE ELSE TO TURN, WE JUST WANT A ANSWER! SUZUKI KNOWS WHAT IT IS AND THEY ARE NOT TELLING ANYONE, THIS IS NOT ONLY IRRESPONSIBLE IT IS POTENTIALLY DANGEROUS. *TRRead more
Incident date: Jun 15, 2009
TL* THE CONTACT OWNS A 2005 SUZUKI XL7. THE CONTACT STATED THAT WHILE ENTERING THE VEHICLE, THE REAR MIDDLE ROW SEAT BELT FAILED TO RETRACT MAKING IT IMPOSSIBLE TO BUCKLE THE SEAT BELT. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSIS BUT THEY WERE UNABLE TO DUPLICATE THE PROBLEM. THE SEAT BELTS WERE REPLACED BUT THE PROBLEM PERSISTED. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAG
... E WAS 36,000. ...UPDATED 11-14-13 *BF THE CONSUMER STATED THE SEAT BELTS HAVE WORN OUT TWICE. HE TOOK THE VEHICLE TO THE DEALER AT APPROXIMATELY 36,000 AND THEY WERE REPLACED. NOW AT 50,000, THEY NEED TO BE REPLACED AGAIN. WHERE THE SEAT BELT RETRACTS INTO THE UNIT, THEY ARE BEING WORN THROUGH, AND THEY WILL NOT RETRACT OR EXTEND.Read more
Incident date: Sep 23, 2013
2009 SUZUKI SX4 64,000 AIR BAG LIGHT STAYS ON EVEN THOUGH NEVER IN AN ACCIDENT OR ACTIVATED. CONTACTED DEALERSHIP AND TOLD ME NOT UNDER WARRANTY. COSTS WAY OVER $1,000 TO FIX AND UNFORTUNATELY I DON'T HAVE THAT KIND OF MONEY. I DID SOME RESEARCH AND FOUND AN EXTREMELY HIGH VOLUME OF COMPLAINTS FOR THIS IDENTICAL DILEMMA. I BELIEVE THERE SHOULD BE A RECALL AND SUZUKI SHOULD RECTIFY THIS PROBLEM
... AT NO COST TO THE CONSUMER. WHAT IS IT GOING TO TAKE? SOMEBODY DYING IN AN ACCIDENT TO GET THEIR ATTENTION? PLEASE LET'S TAKE CARE OF THIS AND SAVE HUMAN LIVES! PLEASE LET'S NOT PUT MONEY OVER SAFETY. *TRRead more
Incident date: Nov 25, 2007
WAS HIT BY A PONTIAC ON THE PASSENGER SIDE OF THE VEHICLE AND THE AIR BAGS DID NOT GO OFF. THE MANUAL STATES THAT I HAVE AIR BAGS THAT ARE IN THE PASSENGER AND DRIVER SEATS THAT ARE SUPPOSED TO GO OFF IF AN ACCIDENT OCCURS. DUE TO THIS, MY PASSENGER AND I SUFFERED INJURIES THAT COULD HAVE BEEN FATAL, IF I HAD NOT TRIED TO AVOID THE ACCIDENT. ALSO, THE CENTER CONSOLE BROKE DURING THE ACCIDENT, CAU
... SING THE GEAR SHIFT TO STICK, AND WHEN YOU TURN THE ENGINE OFF, IT WON'T GO ALL THE WAY OFF UNTIL YOU JERK THE GEAR SHIFT TOWARD THE DRIVER SEAT. *TRRead more
Crash
2 injured
Incident date: Sep 2, 2013
THE MOTORCYCLE IS VERY HARD TO SHIFT INTO 2ND GEAR. TOOK IT TO THE DEALER AND THEY CLAIM THE CLUTCH IS ADJUSTED CORRECTLY. I WAS EVEN TOLD BY THE DEALER THAT IT IS COMMON PROBLEM WITH THE SUZUKI M109R CLUTCH/TRANSMISSION. BECAUSE OF THE SHIFTING PROBLEM SOMETIMES I AM AFRAID THAT A CAR BEHIND ME WILL REAR END ME AS IT IS SO HARD TO SHIFT FROM 1ST INTO 2ND GEAR AND THAN THE MOTORCYCLE WILL SLOW DOW
... N SIGNIFICANTLY. SEARCHING THE INTERNET FOR SOLUTION I DISCOVERED HUNDREDS IF NOT THOUSANDS OF SIMILAR COMPLAINTS. DOES SOMEBODY NEED TO DIE BEFORE THIS IS FIXED? *TRRead more
Incident date: Jan 9, 1996
TL* THE CONTACT OWNS A 2006 SUZUKI FORENZA. THE CONTACT STATED THAT THE AIR BAG AND ENGINE WARNING INDICATORS ILLUMINATED CONTINUOUSLY ON THE INSTRUMENT PANEL. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER AND AN INDEPENDENT MECHANIC FOR DIAGNOSIS. THE REPAIR CONSISTED OF APPLYING MECHANICAL TAPE TO THE FAULTY WIRING LOCATED UNDER THE DRIVER'S SIDE SEAT HOWEVER, THE REPAIR DID NOT CORRECT THE PROB
... LEM. THE FAILURE RECURRED AFTER THE REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 4,000. THE VIN WAS UNAVAILABLE.Read more
Incident date: Sep 9, 2013
TL* THE CONTACT OWNS A 2006 SUZUKI DR200SE MOTORCYCLE. THE CONTACT STATED THAT THE REAR FENDER WAS TOO CLOSE TO THE EXHAUST PIPE. AS A RESULT, WHILE DRIVING 20 MPH THE PLASTIC STARTED TO MELT AND SMOKE WAS EMITTED. THE VEHICLE WAS NOT TAKEN TO THE DEALER. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE MOTORCYCLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 769.
Fire
Incident date: Sep 12, 2013
I WAS DRIVING DOWN THE ROAD AT 50MPH AND TRIED TO CHANGE GEARS AND WAS NOT ABLE TO. MY CLUTCH CABLE WAS IN PERFECT ORDER BUT I COULD NOT ENGAGE THE CLUTCH. I ALMOST REAR ENDED A CAR BECAUSE I COULD NOT ENGAGE THE CLUTCH. I GOT THE BIKE INTO NEUTRAL FINALLY WHILE DODGING CARS ON A BUSY ROAD. I BELIEVE THE ONLY REASON I DID NOT CRASH OR GET KILLED IS BECAUSE OF MY 30 PLUS YEARS OF EXPERIENCE RIDI
... NG MOTORCYCLES. I GOT A FRIEND TO TOW ME HOME AND AFTER READING FORUMS SUCH AS WWW.M109RIDERS.COM I FOUND OUT THAT MY TUBULAR NUT BACKED OFF. THIS IS A NON SERVICEABLE PART ACCORDING TO SUZUKI. THERE IS A FIX FOR IT THAT IS DARN NEAR FREE JUST LOOK AT WWW.M109RIDERS.COM. I WILL BE DOING THIS FIX AS SOON AS MY NEW DRIVE PLATE AND WAVE WASHER GET DELIVERED. THIS SHOULD BE A RECALLED BEFORE SOMEONE GETS KILLED. I URGE ANY M109 RIDER TO SEARCH THAT WEBSITE AND RESEARCH THE COMMON PROBLEMS ON THIS BIKE.. OH AND SHAME ON YOU SUZUKI! *JSRead more
Incident date: Sep 8, 2013
SERVICE PASSENGER AIRBAG LIGHT CAME ON AND WON'T GO OFF. *LN UPDATED 1/9/2013 *JS
Incident date: Sep 30, 2012
TL* THE CONTACT OWNS A 2006 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE DRIVING UPHILL, THE VEHICLE FAILED TO ACCELERATE. THE CONTACT NOTICED THERE WAS A HESITATION BETWEEN GEARS AND ALSO AN ABNORMAL NOISE. THE VEHICLE WAS INSPECTED BY AN INDEPENDENT MECHANIC, WHERE UNKNOWN REPAIRS WERE MADE TO THE VEHICLE HOWEVER, THE FAILURE SOON RECURRED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NO
... TIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 32,000. UPDATED 11/15/13*CN THE CONSUMER STATED THE SWITCH ASSEMBLY WAS REPLACED TWICE. IT WAS ADVISED BY A SUZUKI REPAIR TECHNICIAN TO USE A PLASTIC CORD TO HOLD IT TOGETHER. THE SWITCH ASSEMBLY HAS NOT BEEN REPAIRED. UPDATED 11/26/2013 *JSRead more
Incident date: Sep 18, 2013
WAS DRIVING AND TRANSMISSION RANGE SENSOR WENT BAD AND CAR JUMPED OUT OF GEAR NO WARNING. TRAFFIC BEHIND ALMOST COLLIDED. MY 4 YEAR OLD WAS IN BACK SEAT. VERY SCARY. CALLED SUZUKI AND THEY SAID THIS IS AN EXTREMELY COMMON PROBLEM CONSIDERING MY MAKE, MODEL, MILEAGE. SO WHY AM I, A SINGLE DISABLED MOTHER, RESPONSIBLE FOR GETTING A WELL KNOWN, UNSAFE MANUFACTURER ISSUE REPAIRED..... I CAN'T AFFOR
... D THIS AND FROM WHAT I WAS TOLD MOST PEOPLE WITH SIMILAR ISSUE HAD THIS PROBLEM NOT ONLY ONCE BUT FEW MONTHS AFTER GETTING REPAIR DONE. THIS IS EXTREMELY UNSAFE! CAR SHIFTING AND STALLING WHILE AT FULL SPEED! ME AND MY SON COULD HAVE BEEN SERIOUSLY HURT! PLANNING TO CALL SUZUKI CUSTOMER RELATIONS TO SEE IF THEY CAN FIX ISSUE BECAUSE IT IS NOT FAIR THAT I HAVE TO COME UP WITH WAY TO REPAIR SUCH A DANGEROUS PROBLEM SO MANY SUZUKI OWNERS HAVE EXPERIENCED.Read more
Incident date: Sep 18, 2013
WAS DRIVING AND TRANSMISSION RANGE SENSOR WENT BAD AND CAR JUMPED OUT OF GEAR NO WARNING. TRAFFIC BEHIND ALMOST COLLIDED. MY 4 YEAR OLD WAS IN BACK SEAT. VERY SCARY. CALLED SUZUKI AND THEY SAID THIS IS AN EXTREMELY COMMON PROBLEM CONSIDERING MY MAKE, MODEL, MILEAGE. SO WHY AM I, A SINGLE DISABLED MOTHER, RESPONSIBLE FOR GETTING A WELL KNOWN, UNSAFE MANUFACTURER ISSUE REPAIRED..... I CAN'T AFFOR
... D THIS AND FROM WHAT I WAS TOLD MOST PEOPLE WITH SIMILAR ISSUE HAD THIS PROBLEM NOT ONLY ONCE BUT FEW MONTHS AFTER GETTING REPAIR DONE. THIS IS EXTREMELY UNSAFE! CAR SHIFTING AND STALLING WHILE AT FULL SPEED! ME AND MY SON COULD HAVE BEEN SERIOUSLY HURT! PLANNING TO CALL SUZUKI CUSTOMER RELATIONS TO SEE IF THEY CAN FIX ISSUE BECAUSE IT IS NOT FAIR THAT I HAVE TO COME UP WITH WAY TO REPAIR SUCH A DANGEROUS PROBLEM SO MANY SUZUKI OWNERS HAVE EXPERIENCED.Read more
Incident date: Sep 18, 2013
WAS DRIVING AND TRANSMISSION RANGE SENSOR WENT BAD AND CAR JUMPED OUT OF GEAR NO WARNING. TRAFFIC BEHIND ALMOST COLLIDED. MY 4 YEAR OLD WAS IN BACK SEAT. VERY SCARY. CALLED SUZUKI AND THEY SAID THIS IS AN EXTREMELY COMMON PROBLEM CONSIDERING MY MAKE, MODEL, MILEAGE. SO WHY AM I, A SINGLE DISABLED MOTHER, RESPONSIBLE FOR GETTING A WELL KNOWN, UNSAFE MANUFACTURER ISSUE REPAIRED..... I CAN'T AFFOR
... D THIS AND FROM WHAT I WAS TOLD MOST PEOPLE WITH SIMILAR ISSUE HAD THIS PROBLEM NOT ONLY ONCE BUT FEW MONTHS AFTER GETTING REPAIR DONE. THIS IS EXTREMELY UNSAFE! CAR SHIFTING AND STALLING WHILE AT FULL SPEED! ME AND MY SON COULD HAVE BEEN SERIOUSLY HURT! PLANNING TO CALL SUZUKI CUSTOMER RELATIONS TO SEE IF THEY CAN FIX ISSUE BECAUSE IT IS NOT FAIR THAT I HAVE TO COME UP WITH WAY TO REPAIR SUCH A DANGEROUS PROBLEM SO MANY SUZUKI OWNERS HAVE EXPERIENCED.Read more
Incident date: Sep 18, 2013
TL* THE CONTACT OWNS 2008 SUZUKI FORENZA. THE CONTACT STATED THAT THE VEHICLE BECAME UNRESPONSIVE WHILE ATTEMPTING TO ACCELERATE FROM A TRAFFIC STOP. THE CONTACT HEARD A LOUD BANG AS THE VEHICLE BEGAN TO ROLL AWAY IN REVERSE. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSIS WHERE THE TECHNICIAN STATED THE TRANSMISSION RANGE SENSOR WOULD NEED TO REPLACED. THE VEHICLE WAS REPAIRED. THE APPROXIMATE
... FAILURE MILEAGE WAS 15,000. *TRRead more
Incident date: Sep 20, 2011
TL* THE CONTACT OWNS A 2007 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE IN REVERSE, THE VEHICLE EMITTED A LOUD BANG AND BECAME UNRESPONSIVE TO ACCELERATION ATTEMPTS. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSIS. THE TECHNICIAN STATED THAT THE TRANSMISSION RANGE SENSOR WOULD HAVE TO BE REPLACED. THE VEHICLE WAS REPAIRED BUT THE FAILURE RECURRED. THE APPROXIMATE FAILURE MILEAGE WAS 30,000.
... *TRRead more
Incident date: Aug 12, 2013
AFTER MY DAYTIME RUNNING LIGHTS STAYED ON ALL NIGHT, MY BATTERY DIED AND I HAD TO HAVE THE ENGINE JUMPED. I WENT ALONG WITH MY DAY, PARKED MY CAR AT THE BUS LOT AND WENT TO WORK. AFTER RETURNING TO THE CAR, I SMELLED SMOKE. WHEN I TRIED TO POP MY HOOD, I NOTICED THE INTERIOR PANELING UNDER MY STEERING WHEEL WAS BLACK AND MELTED. THE HOOD WOULD NOT POP OPEN BECAUSE THE RELEASE LEVER WAS ALSO ME
... LTED. THERE WAS SMOKE DAMAGE ON MY WINDSHIELD NEAR THE AIR/DEFROST VENTS AND ON ANYTHING SITTING IN MY CAR. LUCKY FOR ME, I WAS NOT IN THE CAR WHEN THE FIRE OCCURRED AND IT WAS IN A PARKING LOT WHERE NO ONE WAS AROUND TO GET INJURED. AFTER HAVING THE TRANSMISSION SENSOR REPLACED ON THE CAR 4 TIMES BEFORE THEY REPLACED THE ENTIRE TRANSMISSION, I'VE REALIZED THERE WERE ELECTRICAL PROBLEMS WITH THIS CAR LONG BEFORE THE FIRE OCCURRED. MANY OTHERS HAVE COMPLAINED ABOUT A FIRE IN THIS EXACTLY MAKE/MODEL/YEAR CAR. SUZUKI SHOULD BE ASHAMED FOR MAKING SUCH TERRIBLE CARS AND FILING FOR BANKRUPTCY RIGHT BEFORE THE PROBLEM OCCURS SO THERE IS NOTHING TO BE DONE/NO ACCOUNTABILITY. *TRRead more
Fire
Incident date: Aug 12, 2013
AFTER MY DAYTIME RUNNING LIGHTS STAYED ON ALL NIGHT, MY BATTERY DIED AND I HAD TO HAVE THE ENGINE JUMPED. I WENT ALONG WITH MY DAY, PARKED MY CAR AT THE BUS LOT AND WENT TO WORK. AFTER RETURNING TO THE CAR, I SMELLED SMOKE. WHEN I TRIED TO POP MY HOOD, I NOTICED THE INTERIOR PANELING UNDER MY STEERING WHEEL WAS BLACK AND MELTED. THE HOOD WOULD NOT POP OPEN BECAUSE THE RELEASE LEVER WAS ALSO ME
... LTED. THERE WAS SMOKE DAMAGE ON MY WINDSHIELD NEAR THE AIR/DEFROST VENTS AND ON ANYTHING SITTING IN MY CAR. LUCKY FOR ME, I WAS NOT IN THE CAR WHEN THE FIRE OCCURRED AND IT WAS IN A PARKING LOT WHERE NO ONE WAS AROUND TO GET INJURED. AFTER HAVING THE TRANSMISSION SENSOR REPLACED ON THE CAR 4 TIMES BEFORE THEY REPLACED THE ENTIRE TRANSMISSION, I'VE REALIZED THERE WERE ELECTRICAL PROBLEMS WITH THIS CAR LONG BEFORE THE FIRE OCCURRED. MANY OTHERS HAVE COMPLAINED ABOUT A FIRE IN THIS EXACTLY MAKE/MODEL/YEAR CAR. SUZUKI SHOULD BE ASHAMED FOR MAKING SUCH TERRIBLE CARS AND FILING FOR BANKRUPTCY RIGHT BEFORE THE PROBLEM OCCURS SO THERE IS NOTHING TO BE DONE/NO ACCOUNTABILITY. *TRRead more
Fire
Incident date: Aug 20, 2013
THE SENSOR LIGHT FOR THE PASSENGER AIR BAG WENT ON AND WONT RESET THE MECHANIC CHECKED VIA DIAGNOSTIC COMPUTER THE LIGHT AND SAID ITS A FAULTY SENSOR BUT CHANGING IT WOULD REQUIRE $1,500 PASSENGER SEAT REPLACEMENT BECAUSE THE UNIT IS INTEGRAL MEANWHILE THE PASSENGER SEAT BELT LIGHT IS ON REGARDLESS IF BELT IS ENGAGED AND I DON'T KNOW THE IMPLICATIONS TO THE AIR BAG FUNCTIONALITY. *JB
Incident date: Aug 20, 2013
THE SENSOR LIGHT FOR THE PASSENGER AIR BAG WENT ON AND WONT RESET THE MECHANIC CHECKED VIA DIAGNOSTIC COMPUTER THE LIGHT AND SAID ITS A FAULTY SENSOR BUT CHANGING IT WOULD REQUIRE $1,500 PASSENGER SEAT REPLACEMENT BECAUSE THE UNIT IS INTEGRAL MEANWHILE THE PASSENGER SEAT BELT LIGHT IS ON REGARDLESS IF BELT IS ENGAGED AND I DON'T KNOW THE IMPLICATIONS TO THE AIR BAG FUNCTIONALITY. *JB
Incident date: Aug 20, 2013
THE SENSOR LIGHT FOR THE PASSENGER AIR BAG WENT ON AND WONT RESET THE MECHANIC CHECKED VIA DIAGNOSTIC COMPUTER THE LIGHT AND SAID ITS A FAULTY SENSOR BUT CHANGING IT WOULD REQUIRE $1,500 PASSENGER SEAT REPLACEMENT BECAUSE THE UNIT IS INTEGRAL MEANWHILE THE PASSENGER SEAT BELT LIGHT IS ON REGARDLESS IF BELT IS ENGAGED AND I DON'T KNOW THE IMPLICATIONS TO THE AIR BAG FUNCTIONALITY. *JB
Incident date: Jun 5, 2013
TL* THE CONTACT OWNS A 2008 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE STARTING THE IGNITION, THE AIR BAG WARNING INDICATOR ILLUMINATED CONTINUOUSLY UNTIL THE ENGINE WAS TURNED OFF. THE FAILURE RECURRED WHENEVER THE VEHICLE WAS IN OPERATION. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THERE WAS A RECALL ASSOCIATED WITH NHTSA CAMPAIGN ID NUMBER 13V405000 (AIR BAGS) THAT PERTAINED TO MODEL YEARS 2
... 006-2011 AND SX4 VEHICLES. THE MANUFACTURER WAS NOTIFIED OF THE DEFECT. THE APPROXIMATE FAILURE MILEAGE WAS 60,000.....UPDATED 10-21-13 *BF UPDATED 10/24/2013 *JSRead more
Incident date: Jun 1, 2011
I HAVE READ ABOUT THE RECALL ON SUZUKI VEHICLES DATED 09/17/2013 THAT ARE HAVING AN ISSUE WITH THE FRONT PASSENGER SEAT AIR BAG SENSOR NOT KNOWING IF A CHILD OR AN ADULT IS ON THE SEAT, THERE FORE CAUSING THE BAG TO DEPLOY EVEN IF A SMALL CHILD IS IN THE SEAT. I HAVE THE SAME ISSUE WITH MY VEHICLE EXCEPT IT IS A 2004 MODEL WHICH DID NOT QUALIFY FOR THE RECALL, THOUGH I DO NOT KNOW WHY. *TR
Incident date: Sep 16, 2013
TL* THE CONTACT OWNS A 2008 SUZUKI GRAND VITARA. THE CONTACT STATED THAT WHILE DRIVING 30 MPH, SHE CRASHED INTO THE REAR OF ANOTHER VEHICLE BUT THE AIR BAGS FAILED TO DEPLOY. A POLICE REPORT WAS FILED AND THE CONTACT SUSTAINED WHIPLASH AND MINOR BRUISING. THE VEHICLE WAS TOWED TO A BODY SHOP. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT
... MILEAGE WAS 40,000.Read more
Crash
1 injured
Incident date: Aug 16, 2013
THE AIR BAG SENSOR IN THE FRONT PASSENGER SEAT IS NO LONGER WORKING. A WARNING LIGHT ON THE DASH STAYS ON STATING THE PASSENGER-SIDE AIR BAG IS OFF EVEN WHEN SOMEONE IS SITTING IN THE FRONT PASSENGER SEAT. *TR
Incident date: Sep 2, 2013
TL* THE CONTACT OWNS A 2006 SUZUKI GRAND VITARA XL-7. THE CONTACT STATED THAT THREE YEARS AFTER HAVING THE VEHICLE SERVICED UNDER NHTSA CAMPAIGN I.D. 10V250000 (STEERING), THE STEERING PULLEY BECAME FRACTURED. THE VEHICLE BECAME VERY DIFFICULT TO STEER WHILE DRIVING. THE CONTACT TOOK THE VEHICLE TO A LOCAL MECHANIC TO HAVE THE PULLEY REPLACED. THE CONTACT CALLED THE MANUFACTURER REGARDING THE STEE
... RING PULLEY AND THE MANUFACTURER ADVISED HIM TO CALL A DEALER. THE FAILURE MILEAGE WAS 94,000.Read more
Incident date: Sep 3, 2013
THE LOW BEAM HEADLIGHTS IN OUR SUZUKI GRAND VITARA WENT OUT COMPLETELY. I HAVE HAD PROBLEMS BEFORE WITH A SINGLE BULB BURNING OUT WHICH I REPLACED. THEY ARE BURNING OUT MUCH MORE RAPIDLY NOW AND BECOMING A CONSTANT PROBLEM OF HAVING TO REPLACE THE LOW BEAM HEADLIGHTS. NOW, BOTH LOW BEAM HEADLIGHTS STOPPED WORKING THE OTHER DAY AS WE WERE DRIVING BACK AT NIGHT WHICH FORCED ME TO USE MY HIGH BEAM HE
... ADLIGHTS TO GET HOME SAFELY. I HAVE RESEARCHED ONLINE AND HAVE SEEN THAT THIS IS A COMMON PROBLEM MANY SUZUKI OWNERS ARE HAVING BUT SUZUKI IS REFUSING TO ACKNOWLEDGE IT AND PUT OUT A RECALL ON THE ISSUE. *TRRead more
Incident date: Sep 7, 2013
TL* THE CONTACT OWNS A 2009 SUZUKI BOULEVARD M109 MOTORCYCLE. THE CONTACT STATED THAT SMOKE EMITTED FROM THE VEHICLE. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS FOUND THAT THE VOLTAGE REGULATOR HAD FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED ABOUT THE FAILURE. THE FAILURE MILEAGE WAS 8,637.
Fire
Incident date: Sep 3, 2013
THE LOW BEAM HEADLIGHTS IN OUR SUZUKI GRAND VITARA WENT OUT COMPLETELY. I HAVE HAD PROBLEMS BEFORE WITH A SINGLE BULB BURNING OUT WHICH I REPLACED. THEY ARE BURNING OUT MUCH MORE RAPIDLY NOW AND BECOMING A CONSTANT PROBLEM OF HAVING TO REPLACE THE LOW BEAM HEADLIGHTS. NOW, BOTH LOW BEAM HEADLIGHTS STOPPED WORKING THE OTHER DAY AS WE WERE DRIVING BACK AT NIGHT WHICH FORCED ME TO USE MY HIGH BEAM HE
... ADLIGHTS TO GET HOME SAFELY. I HAVE RESEARCHED ONLINE AND HAVE SEEN THAT THIS IS A COMMON PROBLEM MANY SUZUKI OWNERS ARE HAVING BUT SUZUKI IS REFUSING TO ACKNOWLEDGE IT AND PUT OUT A RECALL ON THE ISSUE. *TRRead more
Incident date: Sep 30, 2010
WHILE MY CAR WAS UNDER WARRANTY, ON TWO DIFFERENT OCCASIONS I GOT THE AIRBAG SYMBOL. NOW THAT MY WARRANTY HAS EXPIRED NOW THE AIRBAG SYMBOL CAME BACK PLUS THE FRONT PASSENGER SEATBELT UNLOCK LIGHT SYMBOL, EVEN WITH THE SEATBELT SECURED. I WENT TO SUZUKI THEY TOLD ME THAT I HAD TO PAY TO GET MY CAR INSPECTED , I TOLD THEM THAT THIS IS NOT AN ISSUE OF WEAR AND TEAR THIS IS A SAFETY ISSUE. *
... TRRead more
Incident date: Jun 9, 2011
ENTERED VEHICLE TO GO TO SERVICE CENTER FOR OTHER SERVICE AND AIR BAG LIGHT REMAINED ON AND AFTER SEVERAL ATTEMPTS TO RESET, SHUTTING VEHICLE OFF GETTING OUT AND RE-SEATING MY SELF THE SYSTEM REMAINS INOPERATIVE TO THIS DATE. CODE SCANNER SAYS PASSENGER SEAT MUST BE REPLACED TO REMEDY PROBLEM. COST OF PARTS $2500.00 PLUS LABOR. AFTER DISCUSSION WITH SEVERAL OTHER SUZUKI OWNERS WE FEEL THAT THIS IS
... A CONSTANT PROBLEM WITH THE SUZUKI AND SHOULD BE RESOLVED BY THE MANUFACTURER. IT IS NOT SAFE TO HAVE A VEHICLE WITHOUT THE AIR BAGS BEING OPERATIONAL. WE HAVE OWNED THIS VEHICLE SINCE 2004, IT WAS NEW. *TRRead more
Incident date: Jan 8, 2009
WITHIN A FEW MONTHS OF PURCHASING THE VEHICLE, I HAD TO BEGIN REPLACING LOW BEAM HEAD LAMPS, SEEMINGLY DURING RANDOM STARTS THE BULB WOULD BLOW OUT ON EITHER THE PASSENGER OR DRIVERS SIDE, WITH VERY LITTLE USE BEHIND IT. SOME LAMPS LASTED AS LITTLE AS A FEW WEEKS, OTHERS LASTED MORE THAN A YEAR, BUT THE BULBS NEEDED A SIGNIFICANTLY HIGHER RATE OF REPLACEMENT THAN ANY OTHER VEHICLE I'VE EVER DRIVEN
... . I HAVE REPLACED MULTIPLE LOW BEAM LAMPS - 6 DRIVER SIDE LAMPS, AND 8 PASSENGER SIDE IN ONLY 5 YEARS OF OWNING THE VEHICLE AND LESS THAN 20K MILES DRIVER PER YEAR. NO HELP FROM SUZUKI ON THE MATTER. AND I ONLY BUY QUALITY BULBS FROM BRAND NAME MANUFACTURERS AT REPUTABLE PARTS STORES. *TRRead more
Incident date: Nov 15, 2011
TL* THE CONTACT OWNS A 2007 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE DRIVING 30 MPH, HE CRASHED INTO THE REAR OF ANOTHER VEHICLE. THE AIR BAGS FAILED TO DEPLOY. THE CONTACT SUSTAINED ANKLE INJURIES BUT A POLICE REPORT WAS NOT FILED. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSIS BUT THEY WERE UNABLE TO DUPLICATE THE PROBLEM. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOTIFIED. T
... HE APPROXIMATE FAILURE MILEAGE WAS 107,000.Read more
Crash
1 injured
Incident date: Sep 12, 2013
TL* THE CONTACT OWNS A 2005 SUZUKI VERONA. THE CONTACT STATED THAT WHILE THE VEHICLE WAS BEING INSPECTED AT THE DEALER, THE INSPECTOR NOTICED A HOLE IN THE CRADLE THAT HELD THE ENGINE. THE DEALER STATED THAT THE CRADLE NEEDED TO BE REPLACED. THE DEALER DID NOT REPLACE THE CRADLE. THE FAILURE MILEAGE WAS 45,000.
Incident date: Sep 13, 2013
TRANSMISSION RANGE SENSOR IS HORRIBLE THIS WILL BE THE SECOND TIME TIME TO CHANGE THIS. FIRST TIME WAS AT 45000. *TR
Incident date: Sep 13, 2013
TRANSMISSION RANGE SENSOR IS HORRIBLE THIS WILL BE THE SECOND TIME TIME TO CHANGE THIS. FIRST TIME WAS AT 45000. *TR
Incident date: Sep 10, 2013
BOUGHT THIS HORRIBLE CAR FOR $4,300 OF FINANCIAL AID MONEY WITH "AS IS, NO WARRANTY". OWNER SAID HE'D FIX THE PROBLEM BUT DID NOT EVEN THOUGH HE'S NOT OBLIGED TO, BUT HE WENT AGAINST HIS WORDS FOR FIXING THE CAR. HE SAID HIS MECHANIC WILL BUY THE NEW HOSE FOR THE ENGINE WHICH HE DID, BUT DID NOT PUT IN A FILTER AS SAID. THEN THEY DID NOT FIX THE OXYGEN SENSOR OR PUT ON NEW BRAKE PADS OR ROTORS AS
... SAID. THE BRAKES AND ROTORS ARE SEVERELY DAMAGE, AND THE OXYGEN SENSOR IS BUSTED. THE COOLANT & ANTI-FREEZE TUBE BURST, THE LEFT BLINKER BLINKS REALLY FAST, THE SMOG LIGHT BUTTON DOESN'T WORK, THE WHEEL ALIGNMENT IS OFF. IT IS JUST A TERRIBLE CAR I HAVE BOUGHT WRONGLY. *TRRead more
Incident date: Sep 10, 2013
BOUGHT THIS HORRIBLE CAR FOR $4,300 OF FINANCIAL AID MONEY WITH "AS IS, NO WARRANTY". OWNER SAID HE'D FIX THE PROBLEM BUT DID NOT EVEN THOUGH HE'S NOT OBLIGED TO, BUT HE WENT AGAINST HIS WORDS FOR FIXING THE CAR. HE SAID HIS MECHANIC WILL BUY THE NEW HOSE FOR THE ENGINE WHICH HE DID, BUT DID NOT PUT IN A FILTER AS SAID. THEN THEY DID NOT FIX THE OXYGEN SENSOR OR PUT ON NEW BRAKE PADS OR ROTORS AS
... SAID. THE BRAKES AND ROTORS ARE SEVERELY DAMAGE, AND THE OXYGEN SENSOR IS BUSTED. THE COOLANT & ANTI-FREEZE TUBE BURST, THE LEFT BLINKER BLINKS REALLY FAST, THE SMOG LIGHT BUTTON DOESN'T WORK, THE WHEEL ALIGNMENT IS OFF. IT IS JUST A TERRIBLE CAR I HAVE BOUGHT WRONGLY. *TRRead more
Incident date: Sep 10, 2013
BOUGHT THIS HORRIBLE CAR FOR $4,300 OF FINANCIAL AID MONEY WITH "AS IS, NO WARRANTY". OWNER SAID HE'D FIX THE PROBLEM BUT DID NOT EVEN THOUGH HE'S NOT OBLIGED TO, BUT HE WENT AGAINST HIS WORDS FOR FIXING THE CAR. HE SAID HIS MECHANIC WILL BUY THE NEW HOSE FOR THE ENGINE WHICH HE DID, BUT DID NOT PUT IN A FILTER AS SAID. THEN THEY DID NOT FIX THE OXYGEN SENSOR OR PUT ON NEW BRAKE PADS OR ROTORS AS
... SAID. THE BRAKES AND ROTORS ARE SEVERELY DAMAGE, AND THE OXYGEN SENSOR IS BUSTED. THE COOLANT & ANTI-FREEZE TUBE BURST, THE LEFT BLINKER BLINKS REALLY FAST, THE SMOG LIGHT BUTTON DOESN'T WORK, THE WHEEL ALIGNMENT IS OFF. IT IS JUST A TERRIBLE CAR I HAVE BOUGHT WRONGLY. *TRRead more
Incident date: Jul 16, 2012
THE CHECK ENGINE CAME ON, AND I HAD A DIAGNOSTIC DONE. IT SHOWED ONE O2 SENSOR WAS NOT GOOD. IT WAS REPLACED. AFTER ONE WEEK THE LIGHT CAME ON AGAIN, AND ANOTHER SENSOR NEEDED TO BE REPLACED. ABOUT TWO WEEKS LATER, THE LIGHT CAME ON AGAIN, AND THE TEST SHOWED THAT THE CATALYTIC CONVERTER NEEDED TO BE REPLACED. THIS WAS REPLACED. TWO MONTHS LATER THE LIGHT CAME ON AGAIN, AND IT SHOWS THAT BOTH
... THE O2 SENSOR AND CATALYTIC CONVERTER NEED TO BE REPLACED. NONETHELESS, THE CAR PASSED THE EMISSIONS TEST, BUT THE LIGHT IS STILL ON, AND THE DIAGNOSTICS STILL READ THE SAME; THE O2 SENSOR AND CATALYTIC CONVERTER NEED TO BE REPLACED. THE ACCELERATION NOW HAS PROBLEMS. SOMETIMES, THE CAR WILL HIT 3-4 RPM WHILE THE ACCELERATION IS AT 40 MPH AND WILL NOT GO HIGHER. SOMETIMES, I HAVE TO PULL OVER BECAUSE A "BURNING RUBBER SMELL" IS EMITTED FROM THE ENGINE AND COMES INTO THE CAR THROUGH THE VENTS. THE MILEAGE NOW IS ABOUT 96500. *TRRead more
Incident date: Jul 16, 2012
THE CHECK ENGINE CAME ON, AND I HAD A DIAGNOSTIC DONE. IT SHOWED ONE O2 SENSOR WAS NOT GOOD. IT WAS REPLACED. AFTER ONE WEEK THE LIGHT CAME ON AGAIN, AND ANOTHER SENSOR NEEDED TO BE REPLACED. ABOUT TWO WEEKS LATER, THE LIGHT CAME ON AGAIN, AND THE TEST SHOWED THAT THE CATALYTIC CONVERTER NEEDED TO BE REPLACED. THIS WAS REPLACED. TWO MONTHS LATER THE LIGHT CAME ON AGAIN, AND IT SHOWS THAT BOTH
... THE O2 SENSOR AND CATALYTIC CONVERTER NEED TO BE REPLACED. NONETHELESS, THE CAR PASSED THE EMISSIONS TEST, BUT THE LIGHT IS STILL ON, AND THE DIAGNOSTICS STILL READ THE SAME; THE O2 SENSOR AND CATALYTIC CONVERTER NEED TO BE REPLACED. THE ACCELERATION NOW HAS PROBLEMS. SOMETIMES, THE CAR WILL HIT 3-4 RPM WHILE THE ACCELERATION IS AT 40 MPH AND WILL NOT GO HIGHER. SOMETIMES, I HAVE TO PULL OVER BECAUSE A "BURNING RUBBER SMELL" IS EMITTED FROM THE ENGINE AND COMES INTO THE CAR THROUGH THE VENTS. THE MILEAGE NOW IS ABOUT 96500. *TRRead more
Incident date: May 15, 2013
TL* THE CONTACT OWNS A 2008 SUZUKI FORENZA. THE CONTACT WAS DRIVING APPROXIMATELY 50 MPH WHEN THE VEHICLE STALLED AS THE CONTACT DOWN SHIFTED. THE ENGINE RPM'S THEN DECREASED ABNORMALLY LOW. THE VEHICLE WAS TAKEN TO THE DEALER AND DIAGNOSED THAT THERE WAS NOTHING WRONG WITH THE VEHICLE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE PROBLEM. THE FAILURE MILEAGE WAS 55,000.