Showing 6,583 complaints for SUZUKI
Incident date: Dec 13, 2013
MY SV1000 HAS EXPERIENCED PROBLEMS WITH ITS CHARGING SYSTEM THAT AFFECTS THE ENTIRE ENGINE. I CAME TO FIND IT WAS A HEAVILY DOCUMENTED ON PUBLIC ONLINE FORUMS SUCH AS SV-PORTAL.COM AND HAS AFFECTED ALMOST ALL SV1000 OWNERS. THE MAGNETS, WHICH ARE GLUED TO THE INTERIOR OF THE STATOR ROTOR, BREAK FREE OF THEIR EPOXY BOND AND SHATTER INTO PIECES INSIDE THE ENGINE CASE. THIS IS A MAJOR SAFETY ISSU
... E AS DAMAGE TO THE STATOR/ALTERNATOR IS CERTAIN AND FRAGMENTED MAGNETS ENTER THE TRANSMISSION, OIL PAN, CLUTCH AND OTHER ENGINE SYSTEMS. WHEN ANY OF THESE SYSTEMS ARE CAUSED TO FAIL BY THE BROKEN MAGNET PIECES OR CHARGING SYSTEM FAILURE AT DRIVING SPEED THE RIDER AND ALL NEAR BY MOTORISTS ARE AT SERIOUS RISK. THIS PROBLEM IS WIDESPREAD AND AFFECTS ALL YEARS OF THE SV1000. THE SAFETY ISSUE OCCURS AT VARYING MILEAGE BUT IT IS CERTAIN THAT VEHICLES WITH MORE THAN 15,000 TO 18,000 MILES WILL HAVE THIS ISSUE. *TRRead more
Incident date: Dec 13, 2013
MY SV1000 HAS EXPERIENCED PROBLEMS WITH ITS CHARGING SYSTEM THAT AFFECTS THE ENTIRE ENGINE. I CAME TO FIND IT WAS A HEAVILY DOCUMENTED ON PUBLIC ONLINE FORUMS SUCH AS SV-PORTAL.COM AND HAS AFFECTED ALMOST ALL SV1000 OWNERS. THE MAGNETS, WHICH ARE GLUED TO THE INTERIOR OF THE STATOR ROTOR, BREAK FREE OF THEIR EPOXY BOND AND SHATTER INTO PIECES INSIDE THE ENGINE CASE. THIS IS A MAJOR SAFETY ISSU
... E AS DAMAGE TO THE STATOR/ALTERNATOR IS CERTAIN AND FRAGMENTED MAGNETS ENTER THE TRANSMISSION, OIL PAN, CLUTCH AND OTHER ENGINE SYSTEMS. WHEN ANY OF THESE SYSTEMS ARE CAUSED TO FAIL BY THE BROKEN MAGNET PIECES OR CHARGING SYSTEM FAILURE AT DRIVING SPEED THE RIDER AND ALL NEAR BY MOTORISTS ARE AT SERIOUS RISK. THIS PROBLEM IS WIDESPREAD AND AFFECTS ALL YEARS OF THE SV1000. THE SAFETY ISSUE OCCURS AT VARYING MILEAGE BUT IT IS CERTAIN THAT VEHICLES WITH MORE THAN 15,000 TO 18,000 MILES WILL HAVE THIS ISSUE. *TRRead more
Incident date: Dec 13, 2013
MY SV1000 HAS EXPERIENCED PROBLEMS WITH ITS CHARGING SYSTEM THAT AFFECTS THE ENTIRE ENGINE. I CAME TO FIND IT WAS A HEAVILY DOCUMENTED ON PUBLIC ONLINE FORUMS SUCH AS SV-PORTAL.COM AND HAS AFFECTED ALMOST ALL SV1000 OWNERS. THE MAGNETS, WHICH ARE GLUED TO THE INTERIOR OF THE STATOR ROTOR, BREAK FREE OF THEIR EPOXY BOND AND SHATTER INTO PIECES INSIDE THE ENGINE CASE. THIS IS A MAJOR SAFETY ISSU
... E AS DAMAGE TO THE STATOR/ALTERNATOR IS CERTAIN AND FRAGMENTED MAGNETS ENTER THE TRANSMISSION, OIL PAN, CLUTCH AND OTHER ENGINE SYSTEMS. WHEN ANY OF THESE SYSTEMS ARE CAUSED TO FAIL BY THE BROKEN MAGNET PIECES OR CHARGING SYSTEM FAILURE AT DRIVING SPEED THE RIDER AND ALL NEAR BY MOTORISTS ARE AT SERIOUS RISK. THIS PROBLEM IS WIDESPREAD AND AFFECTS ALL YEARS OF THE SV1000. THE SAFETY ISSUE OCCURS AT VARYING MILEAGE BUT IT IS CERTAIN THAT VEHICLES WITH MORE THAN 15,000 TO 18,000 MILES WILL HAVE THIS ISSUE. *TRRead more
Incident date: Jun 12, 2014
TL* THE CONTACT OWNS A 2004 SUZUKI VERONA. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS, THE VEHICLE ACCELERATED WITHOUT WARNING CAUSING THE CONTACT TO CRASH. A POLICE REPORT WAS FILED AND NO INJURIES WERE SUSTAINED. THE VEHICLE WAS DESTROYED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS UNKNOWN. UPDATED 08/19/14*LJ UPDATED 08/23/2017*CT
Crash
Incident date: May 6, 2012
2008 SUZUKI GSX-R1000. CONSUMER WRITES IN REGARDS TO BRAKING SYSTEM DEFECT RECALL. *SMD THE CONSUMER STATED A YEAR PRIOR TO RECEIVING THE RECALL NOTICE, HER HUSBAND WAS KILLED ON HIS MOTORCYCLE. THE CONSUMER VISITED THE SHOP THAT WAS SOLD THE BIKE SHE WAS INFORMED THE BRAKES WERE THE CAUSE OF HER HUSBAND'S FATAL ACCIDENT. ACCORDING TO WITNESS OF THE ACCIDENT, HER HUSBAND TOOK OFF FROM THE STOP
... SIGN, GOT HIS SPEED UP AND THE BIKE APPEARED TO BE WOBBLING AND HE COULD NOT SLOW IT DOWN. RECALL # 13V449000. *JBRead more
Crash
1 deaths
Incident date: Sep 16, 2008
FROM DAY ONE, MY ENGINE LIGHT HAS COME ON AND I HAVE BEEN DEALING WITH DIFFERENT ISSUES IE, IT'S THE GAS CAP, THE MAN WHO SOLD ME THE CAR, (THE DEALER) TOOK THE CAR TO THE DEALERSHIP TO BE REPAIRED,SO MUCH, THEN HE TOOK OFF, AND LEFT MASSACHUSETTS AFTER SELLING ME A LEMON. ETC. HOW MANY GAS CAPS DO I HAVE TO BUY? NOW AT YEAR 2014, THE ENGINE AND TRANSMISSION HAS BEEN REPLACED, THE ENGINE BELT SNAP
... PED, THE TRANSMISSION IS ACTING UP, (IN JULY OF 2010), AND THE SENSOR HAS GONE COMPLETELY WILD, IE, COMES ON AND GOES OFF STEADILY, HAD THAT REPAIRED, AND WHEN I DRIVE THE ENGINE LIGHT STILL COMES ON AND GOES OFF, OFF, AND ON, AND NOW THE AIR BAG LIGHT STEADILY DOES THE SAME, AFTER HAVING IT REPAIRED TWICE. THE WEBSITE WWW.TOPIX.COM/FORUM/CITY/FLORENCE/AL HAS HUNDREDS OF COMPLAINTS ON ALL OF THE SUZUKI VEHICLES FROM 2005-2012. HOW MANY COMPLAINTS DO YOU HAVE TO HAVE IN ORDER TO DO SOMETHING ABOUT THESE SUZUKI VEHICLES? I DON'T THINK IT'S FAIR TO HAVE TO PAY FOR THESE KIND OF REPAIRS, STILL MAKING CAR NOTES, ON THIS CAR, AND I HAVE TO HAVE TOP NOTCH INSURANCE. I WOULD LIKE TO KNOW WHAT SOMEONE IS GOING TO DO ABOUT THESE VEHICLES. I AM HOPING IT DOESN'T HAVE TO TAKE SOMEONE TO BE KILLED IN ORDER FOR SOMETHING TO HAPPEN FOR A RECALL. THE WARRANTY WAS ONLY FOR 90 DAYS, AND THOUGH I EXERCISED IT. I GOT THE RUN AROUND BECAUSE THE DEALER, AND THE DEALERSHIP DIDN'T DO THE RIGHTFUL REPAIRS ON THIS VEHICLE IN THE TIME ALLOWED. THE FAULT IS ON BOTH. *TRRead more
Incident date: Sep 16, 2008
FROM DAY ONE, MY ENGINE LIGHT HAS COME ON AND I HAVE BEEN DEALING WITH DIFFERENT ISSUES IE, IT'S THE GAS CAP, THE MAN WHO SOLD ME THE CAR, (THE DEALER) TOOK THE CAR TO THE DEALERSHIP TO BE REPAIRED,SO MUCH, THEN HE TOOK OFF, AND LEFT MASSACHUSETTS AFTER SELLING ME A LEMON. ETC. HOW MANY GAS CAPS DO I HAVE TO BUY? NOW AT YEAR 2014, THE ENGINE AND TRANSMISSION HAS BEEN REPLACED, THE ENGINE BELT SNAP
... PED, THE TRANSMISSION IS ACTING UP, (IN JULY OF 2010), AND THE SENSOR HAS GONE COMPLETELY WILD, IE, COMES ON AND GOES OFF STEADILY, HAD THAT REPAIRED, AND WHEN I DRIVE THE ENGINE LIGHT STILL COMES ON AND GOES OFF, OFF, AND ON, AND NOW THE AIR BAG LIGHT STEADILY DOES THE SAME, AFTER HAVING IT REPAIRED TWICE. THE WEBSITE WWW.TOPIX.COM/FORUM/CITY/FLORENCE/AL HAS HUNDREDS OF COMPLAINTS ON ALL OF THE SUZUKI VEHICLES FROM 2005-2012. HOW MANY COMPLAINTS DO YOU HAVE TO HAVE IN ORDER TO DO SOMETHING ABOUT THESE SUZUKI VEHICLES? I DON'T THINK IT'S FAIR TO HAVE TO PAY FOR THESE KIND OF REPAIRS, STILL MAKING CAR NOTES, ON THIS CAR, AND I HAVE TO HAVE TOP NOTCH INSURANCE. I WOULD LIKE TO KNOW WHAT SOMEONE IS GOING TO DO ABOUT THESE VEHICLES. I AM HOPING IT DOESN'T HAVE TO TAKE SOMEONE TO BE KILLED IN ORDER FOR SOMETHING TO HAPPEN FOR A RECALL. THE WARRANTY WAS ONLY FOR 90 DAYS, AND THOUGH I EXERCISED IT. I GOT THE RUN AROUND BECAUSE THE DEALER, AND THE DEALERSHIP DIDN'T DO THE RIGHTFUL REPAIRS ON THIS VEHICLE IN THE TIME ALLOWED. THE FAULT IS ON BOTH. *TRRead more
Incident date: Sep 16, 2008
FROM DAY ONE, MY ENGINE LIGHT HAS COME ON AND I HAVE BEEN DEALING WITH DIFFERENT ISSUES IE, IT'S THE GAS CAP, THE MAN WHO SOLD ME THE CAR, (THE DEALER) TOOK THE CAR TO THE DEALERSHIP TO BE REPAIRED,SO MUCH, THEN HE TOOK OFF, AND LEFT MASSACHUSETTS AFTER SELLING ME A LEMON. ETC. HOW MANY GAS CAPS DO I HAVE TO BUY? NOW AT YEAR 2014, THE ENGINE AND TRANSMISSION HAS BEEN REPLACED, THE ENGINE BELT SNAP
... PED, THE TRANSMISSION IS ACTING UP, (IN JULY OF 2010), AND THE SENSOR HAS GONE COMPLETELY WILD, IE, COMES ON AND GOES OFF STEADILY, HAD THAT REPAIRED, AND WHEN I DRIVE THE ENGINE LIGHT STILL COMES ON AND GOES OFF, OFF, AND ON, AND NOW THE AIR BAG LIGHT STEADILY DOES THE SAME, AFTER HAVING IT REPAIRED TWICE. THE WEBSITE WWW.TOPIX.COM/FORUM/CITY/FLORENCE/AL HAS HUNDREDS OF COMPLAINTS ON ALL OF THE SUZUKI VEHICLES FROM 2005-2012. HOW MANY COMPLAINTS DO YOU HAVE TO HAVE IN ORDER TO DO SOMETHING ABOUT THESE SUZUKI VEHICLES? I DON'T THINK IT'S FAIR TO HAVE TO PAY FOR THESE KIND OF REPAIRS, STILL MAKING CAR NOTES, ON THIS CAR, AND I HAVE TO HAVE TOP NOTCH INSURANCE. I WOULD LIKE TO KNOW WHAT SOMEONE IS GOING TO DO ABOUT THESE VEHICLES. I AM HOPING IT DOESN'T HAVE TO TAKE SOMEONE TO BE KILLED IN ORDER FOR SOMETHING TO HAPPEN FOR A RECALL. THE WARRANTY WAS ONLY FOR 90 DAYS, AND THOUGH I EXERCISED IT. I GOT THE RUN AROUND BECAUSE THE DEALER, AND THE DEALERSHIP DIDN'T DO THE RIGHTFUL REPAIRS ON THIS VEHICLE IN THE TIME ALLOWED. THE FAULT IS ON BOTH. *TRRead more
Incident date: Mar 4, 2008
I AM THE OWNER OF A 2007 SUZUKI FORENZA WITH A RECURRING TRANSMISSION RANGE SENSOR FAILURE. OUT OF THE 7 YEARS I HAVE OWNED THE VEHICLE, I HAVE HAD TO REPLACE THE TRANSMISSION RANGE SENSOR EVERY 14 MONTHS LIKE CLOCKWORK. NO OTHER DEALER OTHER THAN AN AUTHORIZED SUZUKI DEALER IS ABLE TO REPLACE THE RANGE SENSOR. THE FAILURE CAUSES THE VEHICLE TO ABRUPTLY ENGAGE INTO NEUTRAL WITHOUT WARNING. ON SEVE
... RAL OCCASIONS, I HAVE ATTEMPTED TO ACCELERATE FROM A COMPLETE STOP AND THE VEHICLE WOULD DRAG OR WOULD NOT ACCELERATE OVER 10 MPH. ON ONE INSTANCE, I WAS REAR-ENDED DUE TO THE FAILURE BUT LUCKILY NO ONE WAS INJURED. I BELIEVE THAT SUZUKI KNOWS THERE IS AN ISSUE WITH THE SENSOR, WHICH IS A MAJOR PROBLEM FOR AN SUCH AN IMPORTANT COMPONENT ON THE VEHICLE. THIS COULD COST SOMEONE THEIR LIFE! PLEASE DO SOMETHING OR AT LEAST HAVE SUZUKI STOP REPLACING THE FAILURE PART WITH A DEFECTIVE PART THAT THEY KNOW IS GOING TO FAIL WITHIN 14 MONTHS. THE FAILURE MILEAGE WAS 14,000 AND THE CURRENT MILEAGE WAS 92,000. *JSRead more
Crash
Incident date: May 29, 2014
MY CAR HAD A FIRE ON 5/29/2014. I DROVE IN LOW SPEED 30 MPH IN TEMPE CITY, BUT I SMELLED LITTLE SMOKE COMING OUT. I PARKED THE CAR. THE FIRE STARTED FROM SOME CABLES AT THE LEFT SIDE COLUMN UNDER STEERING WHEEL IN FRONT OF DRIVER'S SEAT. THERE WAS NO COLLISION. SOME WIRES, PARTS AND THE PLASTIC COVER UNDER THE STEERING WHEEL HAVE BEEN BURNT DOWN. THE CAR WAS TOWED TO BILL LUKE SUZUKI IN TEMP
... E, AZ AT THE SAME DATE 5/29/2014. THE DEALER BILL LUKE ASKED ME TO REPORT THIS ISSUE TO SUZUKI. I CALLED SUZUKI CUSTOMER SERVICE IN CA ON 5/30/2014. ALREADY 2 WEEKS PAST, I HAVE NOT RECEIVED A RESPONSE FROM SUZUKI. SUZUKI HAS NOT TAKEN ANY ACTION. NOW THE CAR IS STILL IN BILL LUKE IN TEMPE. WOULD YOU PLEASE HELP ME? I APPRECIATE YOU VERY MUCH IF YOU CAN HELP. *TRRead more
Fire
Incident date: Apr 30, 2014
TL* THE CONTACT OWNS A 2007 SUZUKI FORENZA. WHILE DRIVING 40 MPH, THE CONTACT NOTICED THAT THE AIR BAG INDICATOR WAS OFF WHILE A PASSENGER WAS OCCUPYING THE SEAT. THE CONTACT WAS UNABLE TO FIND A DEALER TO REPAIR THE VEHICLE BECAUSE ALL THE SUZUKI DEALERS IN THE AREA WERE NO LONGER IN BUSINESS. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 76,579.
Incident date: Mar 1, 2013
TL* THE CONTACT OWNS A 2007 SUZUKI RENO. THE CONTACT STATED THAT THE VEHICLE SHOOK, HESITATED, AND LOST ACCELERATION INTERMITTENTLY. THE FAILURE OCCURRED AT VARIOUS SPEEDS. THE VEHICLE WAS TAKEN TO THE DEALER WHO STATED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE VIN WAS UNAVAILABLE. THE FAILURE MILEAGE WAS 78,000.
Incident date: Jun 3, 2013
FRONT PASSENGER SIDE FLOOR HOLDS WATER WHEN AIR CONDITIONER IS ON AND THE INSIDE FLOOR IS STARTING TO RUST THIS IS OF NO FAULT OF MY OWN THIS IS A DEFECT. *TR
Incident date: Oct 28, 2013
TL* THE CONTACT OWNS A 2002 SUZUKI GRAND VITARA XL7. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 45 MPH, HE LOST CONSCIOUSNESS AND CRASHED INTO A POLE. THE AIR BAGS FAILED TO DEPLOY. THE CONTACT'S HEAD STRUCK THE STEERING WHEEL COLUMN AND FRONT WINDSHIELD. THE CONTACT SUSTAINED BRUISES TO THE CHEST AREA AND A SLIGHT CONCUSSION THAT REQUIRED MEDICAL ATTENTION. A POLICE REPORT WAS FILED. THE
... VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 230,000.Read more
Crash
1 injured
Incident date: Oct 27, 2013
TL* THE CONTACT OWNS A 2004 SUZUKI GSXR600 MOTORCYCLE. THE CONTACT STATED THAT WHILE DRIVING 45 MPH, HE ATTEMPTED TO ENGAGE THE BRAKES BUT THE VEHICLE FAILED TO STOP. AS A RESULT, THE VEHICLE CRASHED INTO A GUARD RAIL. A POLICE REPORT WAS FILED AND THE DRIVER SUSTAINED A BROKEN FEMUR AND SHATTERED PELVIS. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND
... CURRENT MILEAGE WAS 40,000.Read more
Crash
1 injured
Incident date: Jun 1, 2010
HAVE REPLACED THE DRIVERS SIDE LOW BEAM BULB AT LEAST 7 TIMES AND HAVE CHANGED THE PASSENGER SIDE APPROXIMATELY 6 TIMES SO FAR EVEN REPLACED WITH BEST BULB BRANDS. *TR
Incident date: Jun 1, 2010
HAVE REPLACED THE DRIVERS SIDE LOW BEAM BULB AT LEAST 7 TIMES AND HAVE CHANGED THE PASSENGER SIDE APPROXIMATELY 6 TIMES SO FAR EVEN REPLACED WITH BEST BULB BRANDS. *TR
Incident date: Jun 27, 2013
THE MAGNETS WHICH ARE SUPPOSED TO BE AN INTEGRAL PART OF THE ALTERNATOR ROTOR CAME LOOSE. THEY ARE APPARENTLY HELD IN PLACE WITH GLUE, WHICH FAILED. THIS ALLOWED THE MAGNETS TO BREAK APART AND DESTROY THE ALTERNATOR STATOR AS WELL. THIS WAS AN EXPENSIVE REPAIR INVOLVING NEW PARTS (ROTOR, STATOR, GASKET, OIL) LABOR AND MUCH INCONVENIENCE. *TR
Incident date: Jun 27, 2013
THE MAGNETS WHICH ARE SUPPOSED TO BE AN INTEGRAL PART OF THE ALTERNATOR ROTOR CAME LOOSE. THEY ARE APPARENTLY HELD IN PLACE WITH GLUE, WHICH FAILED. THIS ALLOWED THE MAGNETS TO BREAK APART AND DESTROY THE ALTERNATOR STATOR AS WELL. THIS WAS AN EXPENSIVE REPAIR INVOLVING NEW PARTS (ROTOR, STATOR, GASKET, OIL) LABOR AND MUCH INCONVENIENCE. *TR
Incident date: Mar 28, 2014
THE AIR BAG SENSOR TURNED ON AND WOULDN'T TURN OFF. THERE WAS NO ACCIDENT OR REASON FOR THE SENSOR TO TURN ON. TOOK IT TO THE DEALERSHIP AND HAD TO HAVE THE SENSOR SYSTEM REPLACED. CONTACTED THE SUZUKI CUSTOMER SERVICE AND WAS NOT GIVEN ANY INFORMATION WHY THE SENSOR WOULD SUDDENLY FAIL OTHER THAN THAT IT WAS NO LONGER UNDER WARRANTY AND SO THEY WERE NOT RESPONSIBLE. THE CAR WAS RECALLED IN 2012 F
... OR ELECTRICAL ISSUES DUE TO THE HEADLIGHTS. *TRRead more
Incident date: Mar 28, 2014
THE AIR BAG SENSOR TURNED ON AND WOULDN'T TURN OFF. THERE WAS NO ACCIDENT OR REASON FOR THE SENSOR TO TURN ON. TOOK IT TO THE DEALERSHIP AND HAD TO HAVE THE SENSOR SYSTEM REPLACED. CONTACTED THE SUZUKI CUSTOMER SERVICE AND WAS NOT GIVEN ANY INFORMATION WHY THE SENSOR WOULD SUDDENLY FAIL OTHER THAN THAT IT WAS NO LONGER UNDER WARRANTY AND SO THEY WERE NOT RESPONSIBLE. THE CAR WAS RECALLED IN 2012 F
... OR ELECTRICAL ISSUES DUE TO THE HEADLIGHTS. *TRRead more
Incident date: Jun 6, 2007
TL* THE CONTACT OWNS A 2004 SUZUKI VERONA. THE CONTACT STATED THAT THE CHECK ENGINE LIGHT WOULD SUDDENLY ILLUMINATE AND THE VEHICLE WOULD BECOME RESISTANT TO ACCELERATION. THE VEHICLE WAS TAKEN TO THE DEALER, WHO WAS UNABLE TO DIAGNOSE THE DEFECT. THE MANUFACTURER WAS NOT NOTIFIED OF THE DEFECT. THE FAILURE MILEAGE WAS 45,000. UPDATED 10/7/14*CN THE CONSUMER STATED WHILE DRIVING THE VEHICLE W
... OULD SUDDENLY POWER OFF. THE POWER STEERING WOULD BECOME VERY STIFF. UPDATED 3/11/2015 *JSRead more
Incident date: Feb 28, 2014
I OWN A 2007 SUZUKI XL7 THE SERVICE AIRBAG LIGHT CAME ON AND AFTER SPENDING A GOOD SUM OF MONEY TO FIND OUT WHY BY A LOCAL CERTIFIED MECHANIC I WAS TOLD THAT THE PASSENGER SEAT SENSOR WAS BAD ??? I CALLED THE LOCAL DEALER AND WAS TOLD THAT THE CONNECTOR WAS UNDER RECALL AND THE SEAT SENSOR HAD ALOT OF BULLETINS TO BRING IT UP AND THEY SHOULD HANDLE IT LEAVING THE VEHICLE WITH THEM I WAITED FOR TH
... E CALL THEY CALLED THE AFTERNOON AND SAID IT WOULD BE $1056 FOR A NEW BOTTOM SEAT AND THE AIRBAG WOULD NOT WORK.SO AT THIS POINT SUZUKI AND ITS PARTNER GM WOULD BE RESPONSIBLE FOR YET MORE INJURIES AND POSSIBLE DEATHS FOR FAILING TO RECALL THE PASSENGER SEAT SENSOR !!!! SHOWING ONCE MORE JUST LIKE THE IGNITION SWITCH THAT MONEY IT COST FOR RECALLS IS MORE IMPORTANT THAT HUMAN INJURIES AND LIVES !!! AS WELL AS CUSTOMER LOYALTY.... I MY SELF HAVE DONE SIMPLE SEARCHES AND FOUND MORE THAN A FEW OUTSIDE OF THIS NHTSA SITE AND THE DEALER ARE AWARE OF THE PROBLEM WITH OUT HAVING TO RESEARCH SO MUCH SO THAT THEY KNEW WHAT I WAS TALKING ABOUT AT THE FIRST MENTION OF IT. ... COME ON THIS IS A AIRBAG ISSUE NOT A BROKEN DOOR HANDLE OR A RATTLE THIS IS SERIOUS !!! *TRRead more
Incident date: Feb 28, 2014
I OWN A 2007 SUZUKI XL7 THE SERVICE AIRBAG LIGHT CAME ON AND AFTER SPENDING A GOOD SUM OF MONEY TO FIND OUT WHY BY A LOCAL CERTIFIED MECHANIC I WAS TOLD THAT THE PASSENGER SEAT SENSOR WAS BAD ??? I CALLED THE LOCAL DEALER AND WAS TOLD THAT THE CONNECTOR WAS UNDER RECALL AND THE SEAT SENSOR HAD ALOT OF BULLETINS TO BRING IT UP AND THEY SHOULD HANDLE IT LEAVING THE VEHICLE WITH THEM I WAITED FOR TH
... E CALL THEY CALLED THE AFTERNOON AND SAID IT WOULD BE $1056 FOR A NEW BOTTOM SEAT AND THE AIRBAG WOULD NOT WORK.SO AT THIS POINT SUZUKI AND ITS PARTNER GM WOULD BE RESPONSIBLE FOR YET MORE INJURIES AND POSSIBLE DEATHS FOR FAILING TO RECALL THE PASSENGER SEAT SENSOR !!!! SHOWING ONCE MORE JUST LIKE THE IGNITION SWITCH THAT MONEY IT COST FOR RECALLS IS MORE IMPORTANT THAT HUMAN INJURIES AND LIVES !!! AS WELL AS CUSTOMER LOYALTY.... I MY SELF HAVE DONE SIMPLE SEARCHES AND FOUND MORE THAN A FEW OUTSIDE OF THIS NHTSA SITE AND THE DEALER ARE AWARE OF THE PROBLEM WITH OUT HAVING TO RESEARCH SO MUCH SO THAT THEY KNEW WHAT I WAS TALKING ABOUT AT THE FIRST MENTION OF IT. ... COME ON THIS IS A AIRBAG ISSUE NOT A BROKEN DOOR HANDLE OR A RATTLE THIS IS SERIOUS !!! *TRRead more
Incident date: Feb 28, 2014
THE SUZUKI WINDSHIELD IS LEAKING AND CAUSING THE CAR INTERIOR TO MILDEW AND MOLD THE WINDSHIELD IS A RECALL ITEM BUT WHAT ABOUT THE SMELL AND HEALTH CONCERNS BREATHING PROBLEMS CONSTANT UPPER LUNG INFECTIONS FROM A CAR DEFECT THIS IS A ISSUE. CAR CAN NOT BE SOLD BECAUSE OF SMELL ???? MONEY IS NOT AS BIG OF CONCERN AS HEALTH OF ME AND MY FAMILY ??? SUZUKI SHOULD BUY BACK OR FIX PROBLEM. *TR
Incident date: Feb 28, 2014
THE SUZUKI WINDSHIELD IS LEAKING AND CAUSING THE CAR INTERIOR TO MILDEW AND MOLD THE WINDSHIELD IS A RECALL ITEM BUT WHAT ABOUT THE SMELL AND HEALTH CONCERNS BREATHING PROBLEMS CONSTANT UPPER LUNG INFECTIONS FROM A CAR DEFECT THIS IS A ISSUE. CAR CAN NOT BE SOLD BECAUSE OF SMELL ???? MONEY IS NOT AS BIG OF CONCERN AS HEALTH OF ME AND MY FAMILY ??? SUZUKI SHOULD BUY BACK OR FIX PROBLEM. *TR
Incident date: Feb 28, 2014
I OWN A 2007 SUZUKI XL7 THE SERVICE AIRBAG LIGHT CAME ON AND AFTER SPENDING A GOOD SUM OF MONEY TO FIND OUT WHY BY A LOCAL CERTIFIED MECHANIC I WAS TOLD THAT THE PASSENGER SEAT SENSOR WAS BAD ??? I CALLED THE LOCAL DEALER AND WAS TOLD THAT THE CONNECTOR WAS UNDER RECALL AND THE SEAT SENSOR HAD ALOT OF BULLETINS TO BRING IT UP AND THEY SHOULD HANDLE IT LEAVING THE VEHICLE WITH THEM I WAITED FOR TH
... E CALL THEY CALLED THE AFTERNOON AND SAID IT WOULD BE $1056 FOR A NEW BOTTOM SEAT AND THE AIRBAG WOULD NOT WORK.SO AT THIS POINT SUZUKI AND ITS PARTNER GM WOULD BE RESPONSIBLE FOR YET MORE INJURIES AND POSSIBLE DEATHS FOR FAILING TO RECALL THE PASSENGER SEAT SENSOR !!!! SHOWING ONCE MORE JUST LIKE THE IGNITION SWITCH THAT MONEY IT COST FOR RECALLS IS MORE IMPORTANT THAT HUMAN INJURIES AND LIVES !!! AS WELL AS CUSTOMER LOYALTY.... I MY SELF HAVE DONE SIMPLE SEARCHES AND FOUND MORE THAN A FEW OUTSIDE OF THIS NHTSA SITE AND THE DEALER ARE AWARE OF THE PROBLEM WITH OUT HAVING TO RESEARCH SO MUCH SO THAT THEY KNEW WHAT I WAS TALKING ABOUT AT THE FIRST MENTION OF IT. ... COME ON THIS IS A AIRBAG ISSUE NOT A BROKEN DOOR HANDLE OR A RATTLE THIS IS SERIOUS !!! *TRRead more
Incident date: Feb 28, 2014
I OWN A 2007 SUZUKI XL7 THE SERVICE AIRBAG LIGHT CAME ON AND AFTER SPENDING A GOOD SUM OF MONEY TO FIND OUT WHY BY A LOCAL CERTIFIED MECHANIC I WAS TOLD THAT THE PASSENGER SEAT SENSOR WAS BAD ??? I CALLED THE LOCAL DEALER AND WAS TOLD THAT THE CONNECTOR WAS UNDER RECALL AND THE SEAT SENSOR HAD ALOT OF BULLETINS TO BRING IT UP AND THEY SHOULD HANDLE IT LEAVING THE VEHICLE WITH THEM I WAITED FOR TH
... E CALL THEY CALLED THE AFTERNOON AND SAID IT WOULD BE $1056 FOR A NEW BOTTOM SEAT AND THE AIRBAG WOULD NOT WORK.SO AT THIS POINT SUZUKI AND ITS PARTNER GM WOULD BE RESPONSIBLE FOR YET MORE INJURIES AND POSSIBLE DEATHS FOR FAILING TO RECALL THE PASSENGER SEAT SENSOR !!!! SHOWING ONCE MORE JUST LIKE THE IGNITION SWITCH THAT MONEY IT COST FOR RECALLS IS MORE IMPORTANT THAT HUMAN INJURIES AND LIVES !!! AS WELL AS CUSTOMER LOYALTY.... I MY SELF HAVE DONE SIMPLE SEARCHES AND FOUND MORE THAN A FEW OUTSIDE OF THIS NHTSA SITE AND THE DEALER ARE AWARE OF THE PROBLEM WITH OUT HAVING TO RESEARCH SO MUCH SO THAT THEY KNEW WHAT I WAS TALKING ABOUT AT THE FIRST MENTION OF IT. ... COME ON THIS IS A AIRBAG ISSUE NOT A BROKEN DOOR HANDLE OR A RATTLE THIS IS SERIOUS !!! *TRRead more
Incident date: Jul 1, 2013
BECAUSE OF FAULTY PRIMER, THE PAINT ON MY 2008 XL7 IS NOW PEELING OFF AND BUBBLING. SUZUKI REFUSES TO DO ANYTHING ABOUT IT. IT IS TOO EXPENSIVE TO FIX SO WHEN I GO TO TRADE IT IN, IT WILL BE WORTH LITTLE TO NOTHING. I WILL NEVER BUY ANOTHER SUZUKI AGAIN SIMPLY BASED ON THE LACK OF CUSTOMER SERVICE. MINE IS NOT THE ONLY WHITE XL7 THIS HAS HAPPENED TO. THERE ARE MANY MORE COMPLAINTS WHEN YOU SE
... ARCH THE INTERNET WHERE SUZUKI HAS DONE NOTHING. IT'S SAD BECAUSE IT WAS A REALLY CLASSY VEHICLE AND NOT IT LOOKS LIKE A HOT MESS! IT DOESN'T SEEM LIKE SUZUKI WOULD WANT THEIR BRAND BEING REPRESENTED LIKE THIS AS YOU CAN CLEARLY TELL THE PAINT PROBLEM WAS NOT CAUSED BY AN ACCIDENT BUT IS A TRUE DEFECT. *TRRead more
Incident date: Nov 15, 2013
TL* THE CONTACT OWNS A 2008 SUZUKI GRAND VITARA. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN ID NUMBER: 13V405000 (AIR BAGS) AND STATED THAT THE PARTS WERE NOT AVAILABLE. THE DEALER DID NOT GIVE A SPECIFIC DATE WHEN THE PARTS WOULD BECOME AVAILABLE. THE MANUFACTURER COULD NOT PROVIDE AN ESTIMATED DATE FOR WHEN THE CONTACTS VEHICLE WOULD RECEIVE THE RECALL REPAIRS. THE CONTACT HAD NOT EXPER
... IENCED A FAILURE. UPDATED 08/28/14*LJ THE CONSUMER STATED THE MANUFACTURER REFUSED TO ALLOW A LOCAL SHOP TO COMPLETE THE REPAIRS. THE DEALER WAS TOO FAR AND COSTLY TO TRAVEL. UPDATED 09/1/2014 *JSRead more
Incident date: Apr 9, 2012
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 5 EPOXIED IN THE CORRECT PLACE. THE OTHER 1 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: Apr 9, 2012
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 5 EPOXIED IN THE CORRECT PLACE. THE OTHER 1 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: Sep 3, 2013
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 4 EPOXIED IN THE CORRECT PLACE. THE OTHER 2 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: Sep 3, 2013
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 4 EPOXIED IN THE CORRECT PLACE. THE OTHER 2 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: Sep 21, 2013
THIS IS A SECOND FAILURE. MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 3 EPOXIED IN THE CORRECT PLACE. THE OTHER 3 HAD BROKEN THE BOND AND WERE SLIDING ARO
... UND CAUSING DAMAGE AND WERE ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. THIS IS THE SECOND FAILURE IN THE SAME BIKE OF AN OEM SUZUKI PART. FIRST FAILURE ODI 10594978. *TRRead more
Incident date: Sep 21, 2013
THIS IS A SECOND FAILURE. MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 3 EPOXIED IN THE CORRECT PLACE. THE OTHER 3 HAD BROKEN THE BOND AND WERE SLIDING ARO
... UND CAUSING DAMAGE AND WERE ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. THIS IS THE SECOND FAILURE IN THE SAME BIKE OF AN OEM SUZUKI PART. FIRST FAILURE ODI 10594978. *TRRead more
Incident date: Aug 23, 2010
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 1 EPOXIED IN THE CORRECT PLACE. THE OTHER 5 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: Aug 23, 2010
MOTORCYCLE STARTED TO VIBRATE MORE AT HANDLE BARS AND BECAME UNCOMFORTABLE TO RIDE. ELECTRICAL OUTPUT FROM THE MAGNETO WAS ALSO STARTING TO DROP IN DC OUTPUT. SELF INVESTIGATION INTO ISSUE REVEALED THAT THE INTERNAL MAGNETO ROTOR THAT NORMALLY HAS 6 MAGNETS EPOXIED TO IT, NOW ONLY HAD 1 EPOXIED IN THE CORRECT PLACE. THE OTHER 5 HAD BROKEN THE BOND AND WERE SLIDING AROUND CAUSING DAMAGE AND WERE
... ALL BUNCHED UP CAUSING THE VIBRATION ISSUE ALONG WITH THE LOW VOLTAGE OUTPUT TO THE ELECTRICAL SYSTEM. ENGINE WAS CLEANED OUT, AND PART REPLACED WITH NEW SUZUKI OEM PART. *TRRead more
Incident date: May 1, 2014
OCS SENSOR MAT INSTALLED IN THE FRONT PASSENGER SEAT MAY FAIL DUE TO REPEATED FLEXING OF THE MAT FROM USE OF THE SEAT. AS A RESULT, DURING A CRASH NECESSITATING DEPLOYMENT, THE AIR BAG WILL DEPLOY REGARDLESS OF WHETHER THE FRONT SEAT OCCUPANT IS AN ADULT OR A CHILD. * WILL NOT DETECT PASSENGER IN SEAT AT WEIGHTS OF 150 LBS OR BELOW. *TR
Incident date: Apr 25, 2014
HUSBAND WAS DRIVING VEHICLE WHEN THE FRONT TIRE GAVE WAY AND BENT IN FROM FRAME. TOOK TO THE REPAIR SHOP AND WAS INFORMED THAT THE ENTIRE FRAME WAS ROTTED OUT. THE VEHICLE COULD NOT BE REPAIRED AS THE PART IS NOT AVAILABLE. THE CAR ONLY HAD 129,000 MILES ON IT. THIS IS A COMMON PROBLEM WITH THE CAR AND IT SHOULD HAVE BEEN RECALLED. FORTUNATELY, NO ACCIDENT OCCURRED AND NO INJURIES WERE SUSTAIN
... ED. SHAME ON SUZUKI FOR PRODUCING INFERIOR CARS. THIS IS A SERIOUS SAFELY ISSUE! *TRRead more
Incident date: Apr 25, 2014
HUSBAND WAS DRIVING VEHICLE WHEN THE FRONT TIRE GAVE WAY AND BENT IN FROM FRAME. TOOK TO THE REPAIR SHOP AND WAS INFORMED THAT THE ENTIRE FRAME WAS ROTTED OUT. THE VEHICLE COULD NOT BE REPAIRED AS THE PART IS NOT AVAILABLE. THE CAR ONLY HAD 129,000 MILES ON IT. THIS IS A COMMON PROBLEM WITH THE CAR AND IT SHOULD HAVE BEEN RECALLED. FORTUNATELY, NO ACCIDENT OCCURRED AND NO INJURIES WERE SUSTAIN
... ED. SHAME ON SUZUKI FOR PRODUCING INFERIOR CARS. THIS IS A SERIOUS SAFELY ISSUE! *TRRead more
Incident date: Nov 20, 2013
TL* THE CONTACT OWNS A 2007 SUZUKI SX4. THE CONTACT STATED THAT NHTSA CAMPAIGN NUMBER: 10V513000 (VISIBILITY) AND NHTSA CAMPAIGN NUMBER: 13V405000 (AIR BAGS) HAD EXCEEDED A REASONABLE AMOUNT OF TIME FOR REPAIRS. THE DEALER STATED THE PARTS WERE NOT AVAILABLE FOR REPAIRS. THE MANUFACTURER WAS NOT MADE AWARE OF THE DELAY. THE VEHICLE WAS NOT REPAIRED. THE CONTACT DID NOT EXPERIENCE ANY FAILURE.
... UPDATED 8/12/14*CN UPDATED 09/5/2014 *JSRead more
Incident date: Nov 20, 2013
TL* THE CONTACT OWNS A 2007 SUZUKI SX4. THE CONTACT STATED THAT NHTSA CAMPAIGN NUMBER: 10V513000 (VISIBILITY) AND NHTSA CAMPAIGN NUMBER: 13V405000 (AIR BAGS) HAD EXCEEDED A REASONABLE AMOUNT OF TIME FOR REPAIRS. THE DEALER STATED THE PARTS WERE NOT AVAILABLE FOR REPAIRS. THE MANUFACTURER WAS NOT MADE AWARE OF THE DELAY. THE VEHICLE WAS NOT REPAIRED. THE CONTACT DID NOT EXPERIENCE ANY FAILURE.
... UPDATED 8/12/14*CN UPDATED 09/5/2014 *JSRead more
Incident date: Feb 2, 2012
TL* THE CONTACT OWNS A 2008 SUZUKI SX4. THE CONTACT STATED THAT THE AIR BAG SENSOR ILLUMINATED INTERMITTENTLY. THE CONTACT MENTIONED THAT A PASSENGER WAS SEATED IN THE PASSENGER SEAT BUT THE WARNING LAMP STILL INDICATED THAT THE AIR BAG WAS OFF. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER. THE TECHNICIAN EXPLAINED THAT THE PARTS WERE NOT AVAILABLE IN ORDER TO DO REPAIRS FOR RECALL NHTSA CAMPAIGN
... ID NUMBER: 13V405000 (AIR BAGS) AND WAS NOT ABLE TO PROVIDE A SPECIFIC DATE WHEN THE PARTS WOULD BECOME AVAILABLE. THE MANUFACTURER WAS NOT ABLE TO BE REACHED AFTER NUMEROUS ATTEMPTS. THE VEHICLE FAILURE AND CURRENT MILEAGE WAS 36,000.Read more
Incident date: Dec 14, 2011
I WAS DRIVING DOWN A BUSY STREET IN STOP AND GO TRAFFIC. WHILE STOPPED AT A STOP LIGHT, MY VEHICLE MADE A VERY LOUD "CLUNK" NOISE, LURCHED FORWARD AND THE CHECK ENGINE LIGHT CAME ON. WHEN I ATTEMPTED TO ACCELERATE AFTER THE LIGHT TURNED GREEN, I HAD TO PUSH THE GAS PEDAL ALMOST TO THE FLOOR TO GET THE VEHICLE TO MOVE FORWARD. I PULLED OVER AND PARKED, TURNED THE VEHICLE OFF, WAITED ABOUT A MINU
... TE, TURNED THE VEHICLE BACK ON, AND THE PROBLEM HAD GONE AWAY ALTHOUGH THE CHECK ENGINE LIGHT WAS STILL ON. A DAY OR SO LATER, WHILE I WAS DRIVING ON THE HIGHWAY GOING APPROXIMATELY 65 MILES PER HOUR, THE VEHICLE MADE THE "CLUNK" NOISE, LURCHED FORWARD AND THE CHECK ENGINE LIGHT CAME ON AGAIN. THIS TIME, BECAUSE I WAS ALREADY IN MOTION, THE RPMS JUMPED UP ABOVE 3000, WHICH IS VERY HIGH FOR A 4 CYLINDER ENGINE ONLY GOING 65 MILES PER HOUR. AGAIN, I PULLED OVER, TURNED THE VEHICLE OFF, WAITED ABOUT A MINUTE, TURNED THE CAR ON AND WAS ABLE TO DRIVE THE VEHICLE NORMALLY AGAIN ALTHOUGH THE CHECK ENGINE LIGHT REMAINED ILLUMINATED. THIS ISSUE HAS BEEN HAPPENING RANDOMLY ABOUT 20 TIMES A YEAR OVER THE COURSE OF THE LAST 2 1/2 - 3 YEARS. *TRRead more
Incident date: Dec 14, 2011
I WAS DRIVING DOWN A BUSY STREET IN STOP AND GO TRAFFIC. WHILE STOPPED AT A STOP LIGHT, MY VEHICLE MADE A VERY LOUD "CLUNK" NOISE, LURCHED FORWARD AND THE CHECK ENGINE LIGHT CAME ON. WHEN I ATTEMPTED TO ACCELERATE AFTER THE LIGHT TURNED GREEN, I HAD TO PUSH THE GAS PEDAL ALMOST TO THE FLOOR TO GET THE VEHICLE TO MOVE FORWARD. I PULLED OVER AND PARKED, TURNED THE VEHICLE OFF, WAITED ABOUT A MINU
... TE, TURNED THE VEHICLE BACK ON, AND THE PROBLEM HAD GONE AWAY ALTHOUGH THE CHECK ENGINE LIGHT WAS STILL ON. A DAY OR SO LATER, WHILE I WAS DRIVING ON THE HIGHWAY GOING APPROXIMATELY 65 MILES PER HOUR, THE VEHICLE MADE THE "CLUNK" NOISE, LURCHED FORWARD AND THE CHECK ENGINE LIGHT CAME ON AGAIN. THIS TIME, BECAUSE I WAS ALREADY IN MOTION, THE RPMS JUMPED UP ABOVE 3000, WHICH IS VERY HIGH FOR A 4 CYLINDER ENGINE ONLY GOING 65 MILES PER HOUR. AGAIN, I PULLED OVER, TURNED THE VEHICLE OFF, WAITED ABOUT A MINUTE, TURNED THE CAR ON AND WAS ABLE TO DRIVE THE VEHICLE NORMALLY AGAIN ALTHOUGH THE CHECK ENGINE LIGHT REMAINED ILLUMINATED. THIS ISSUE HAS BEEN HAPPENING RANDOMLY ABOUT 20 TIMES A YEAR OVER THE COURSE OF THE LAST 2 1/2 - 3 YEARS. *TRRead more
Incident date: May 1, 2014
I STARTED THE CAR. LET IT IDLE FOR A MINUTE TO BRING THE RPM DOWN. I TRIED TO SHIFT IT TO REVERSE BUT IT WOULD NOT GO. IT HAD AN ENGINE WARNING LIGHT ON. I SHIFTED BACK TO PARK AND TURNED THE CAR OFF. I LET IT SET FOR A MINUTE THEN RESTARTED IT. WHEN I SHIFTED AGAIN, IT CLUNKED AND WOULD BARELY MOVE. I SHIFTED TO DRIVE AND IT CLUNKED AND WOULD BARELY MOVE. I AM A SINGLE 55 YEAR OLD WOMAN. I WORK 2
... JOBS AND LIVE 8 MILES OUT OF TOWN. I CAN'T AFFORD TO HAVE THIS CAR DOWN. I BOUGHT IT BECAUSE OF THE LOW MILEAGE. IT ONLY HAS 39,000 MILES. *TRRead more
Incident date: Jun 1, 2009
I HAVE REPLACED THE TRANSMISSION RANGE SENSOR TWICE SINCE PURCHASING MY CAR NEW IN 2008 AND JUST LAST WEEK I STARTED HAVING THE SAME ISSUE! SO I WILL BE REPLACING THIS SAME PART FOR THE 3RD TIME SINCE PURCHASINGIT NEW 6 YEARS AGO. *TR
Incident date: May 6, 2014
WHEN I FILL UP MY TANK MY VEHICLE HAS TROUBLE STARTING AND ALSO MAKES A NOISE WHILE STARTING.THE TEMPERATURE GAGE NO LONGER WORKS AND THE BLINKER HANDLE HAS TO BE MANUALLY TURN OFF AFTER TURNING.PLEASE LET ME KNOW WHATS GOING ON.THIS SUV NOW HAS 95,000 MILES LOVE IT BUT AM CONCERNED IS THIS A PRICEY REPAIR.NEED TO KNOW IF THERE'S ANY RECALLS FOR MY VEHICLE.A CONCERNED OWNER. *TR
Incident date: Sep 4, 2013
THE AIR BAG DASH LITE CAME ON, WHEN TAKEN IN FOR REPAIR THE DEALER TOLD ME THAT THEY HAVE SEEN SEVERAL LIKE THIS AND THAT IT WAS A DEFECTIVE PASSENGER SEAT SENSOR, THE FIX IS TO REPLACE THE ENTIRE SEAT? IF THIS IS HAPPENING TO SEVERAL PEOPLE WHY NOT A RECALL? THE COST T REPLACE THE SEAT OVER $2000. *TR