Showing 6,583 complaints for SUZUKI
Incident date: Feb 25, 2016
BOUGHT THIS IN APRIL 2014 WITH 30K MILES, HAVE REPLACED BOTH LOW BEAM HEADLIGHTS 4-5 TIMES EACH, ALSO BEAMS ARE LOW VISIBILITY
Incident date: Feb 25, 2016
BOUGHT THIS IN APRIL 2014 WITH 30K MILES, HAVE REPLACED BOTH LOW BEAM HEADLIGHTS 4-5 TIMES EACH, ALSO BEAMS ARE LOW VISIBILITY
Incident date: Feb 19, 2016
DRIVE GEAR (CLUTCH GEAR) FOR OIL PUMP, CAMS ETC. BROKE SPIDER WASHER (RETAINER CLIP) AND CAME LOOSE STRIKING BACK OF CLUTCH BASKET WHICH KEPT IT FROM COMING COMPLETELY OFF WHICH WOULD HAVE CAUSED ENGINE DESTRUCTION. GEAR SHOULD HAVE HAD MORE TORQUE APPLIED AT FACTORY TO NUT AND RED LOCK-TITE APPLIED TO THREADS. SHOULD HAVE BEEN RECALL. REMAINING 1/3 OF BROKEN SPIDER WASHER COULD NOT BE FOUND IN OI
... L SUMP. REMAINING LO PIECE COULD ENTER TRANSMISSION WITH POSSIBLE LOCK UP. PROBLEM WAS NOTICED BY NOISE WHILE RIDING 02/19/16. REPAIRED BY MSP CYCLES, DECATUR, GA AT A COST TO ME OF $343.22. SINCE I CAN'T AFFORD ANOTHER MOTORCYCLE I'LL CONTINUE TO RIDE THIS SV WITH A QUESTION AS TO WHETHER THE MISSING PIECE WILL CAUSE PROBLEMS. THANKSRead more
Incident date: May 22, 2015
TL* THE CONTACT OWNS A 2009 SUZUKI AN650K9. WHILE DRIVING VARIOUS SPEEDS, THE ENGINE STALLED AND THE ELECTRICAL LIGHT ILLUMINATED ON THE INSTRUMENT PANEL. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE RECTIFIER REGULATOR FAILED AND WOULD NEED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 1,400. UPDATED 04/20/
... 16*LJ UPDATED 6/7/18*JBRead more
Incident date: Jan 26, 2016
TL* THE CONTACT OWNS A 2007 SUZUKI GSX-R600. WHILE DRIVING AT APPROXIMATELY 20 MPH, THE ENGINE STALLED WITHOUT WARNING. THE FAILURE RECURRED TWICE. THE ENGINE RESTARTED AFTER RECEIVING A JUMP FROM ANOTHER VEHICLE. THE SECOND TIME THE FAILURE RECURRED, THE VEHICLE DID NOT RESTART. THE VEHICLE WAS TOWED TO A DEALER WHERE IT WAS DIAGNOSED THAT THE STARTER AND REGULATOR RECTIFIER FAILED AND NEEDED TO
... BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURES. THE FAILURE MILEAGE WAS APPROXIMATELY 11,000.Read more
Incident date: Mar 1, 2013
TL* THE CONTACT OWNS A 2011 (NA) SUZUKI HAYABUSA MOTORCYCLE. THE CONTACT STATED THAT THE MOTORCYCLE WAS INOPERABLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE BATTERY HAD BEEN OVERCHARGED AND LEAKED SULPHURIC ACID. AS A RESULT, THE BATTERY AND RECTIFIER NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT R
... ECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 16V018000 (ELECTRICAL SYSTEM); HOWEVER, THE PART TO DO THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 100,000. PARTS DISTRIBUTION DISCONNECT. UPDATED 04/14/16*LJ UPDATED 6/6/18*JBRead more
Incident date: Feb 18, 2016
MY 2008 XL7 SERIVCE STABILITY CONTROL AND ABS LIGHT STAYS ON AND IT'S VERY DIFFICULT TO TURN.
Incident date: Feb 18, 2016
MY 2008 XL7 SERIVCE STABILITY CONTROL AND ABS LIGHT STAYS ON AND IT'S VERY DIFFICULT TO TURN.
Incident date: Dec 1, 2008
RADIO CHANGED OUT 2X AFTER ELECTRICAL PROBLEMS, LIGHT FOR AIR BAG HAS BEEN ON FOR 3 YRS. BRAKES HAVE HAD TO GET WORKED ON 2X BEFORE IT HIT 50,000, CLIP ON DRIVERSIDE MAT BROKE AFTER 2 MONTHS OF HAVING CAR, DOOR PANELS ON BOTH FRONT AND BACK PASSANGER SIDE KEPT FALLING OFF AND KEPT TAKING CAR BACK TO FIX TILL THEY HAD NO REPLACEMENT PARTS THIS CAR SHOULD NOT BE ON THE ROAD THERE ARE MANY SAFETY ISS
... UES BLIND SPOTS BECAUSE OF THE DESIGN, AND ALL THE LITTLE ISSUES FROM 2 BATTERIES REPLACED TO 2 SETS OF BRAKE JOBS TO ELECTRICALS TO 3 SETS OF TIRES, AND THE CAR ONLY HAS 80,OOO MILES OR LESS. I'VE HAD IT 9 YRS MOSTLY AS A SECOND CAR AND ALWAYS PROBLEMS INCLUDING PAINT. BUT THE SAFETY ISSUES AND THE CRAP CAR WE WERE SOLD KEPT IT CAUSE NOBODY IN THERE RIGHT MIND WANTS IT I AM 1ST YR OWNER THIS CAR SUCKS FFFFFFF IS WHAT IT SHOULD RATE THE CAR DEALERS WONT FIX IT THEY MAKE YOU COME BACK AGAIN AND AGAIN THAT THE PARTS HAVE TO BE FOUND BECAUSE THE PLANT GOT WASHED AWAY AND THE PARTS WITH IT. AND THAT COMPANY WONT LET THEM HOLD PARTS IN THERE SHOPS SO HURRY UP AND WAIT IT IS THE TRAINSHAF IS CRACKED BUT HEY ITS A SECOND CAR THAT COST TOO MUCH AND GIVES TOO LITTLE JUST FOUND THIS WEBSITE THANK TO CONSUMERREPORT MAGAZINE, THIS CAR WAS CRAP FROM DAY ONE WHEN IT ROLLED OF THE TRUCK IN 2008Read more
Incident date: Dec 1, 2008
RADIO CHANGED OUT 2X AFTER ELECTRICAL PROBLEMS, LIGHT FOR AIR BAG HAS BEEN ON FOR 3 YRS. BRAKES HAVE HAD TO GET WORKED ON 2X BEFORE IT HIT 50,000, CLIP ON DRIVERSIDE MAT BROKE AFTER 2 MONTHS OF HAVING CAR, DOOR PANELS ON BOTH FRONT AND BACK PASSANGER SIDE KEPT FALLING OFF AND KEPT TAKING CAR BACK TO FIX TILL THEY HAD NO REPLACEMENT PARTS THIS CAR SHOULD NOT BE ON THE ROAD THERE ARE MANY SAFETY ISS
... UES BLIND SPOTS BECAUSE OF THE DESIGN, AND ALL THE LITTLE ISSUES FROM 2 BATTERIES REPLACED TO 2 SETS OF BRAKE JOBS TO ELECTRICALS TO 3 SETS OF TIRES, AND THE CAR ONLY HAS 80,OOO MILES OR LESS. I'VE HAD IT 9 YRS MOSTLY AS A SECOND CAR AND ALWAYS PROBLEMS INCLUDING PAINT. BUT THE SAFETY ISSUES AND THE CRAP CAR WE WERE SOLD KEPT IT CAUSE NOBODY IN THERE RIGHT MIND WANTS IT I AM 1ST YR OWNER THIS CAR SUCKS FFFFFFF IS WHAT IT SHOULD RATE THE CAR DEALERS WONT FIX IT THEY MAKE YOU COME BACK AGAIN AND AGAIN THAT THE PARTS HAVE TO BE FOUND BECAUSE THE PLANT GOT WASHED AWAY AND THE PARTS WITH IT. AND THAT COMPANY WONT LET THEM HOLD PARTS IN THERE SHOPS SO HURRY UP AND WAIT IT IS THE TRAINSHAF IS CRACKED BUT HEY ITS A SECOND CAR THAT COST TOO MUCH AND GIVES TOO LITTLE JUST FOUND THIS WEBSITE THANK TO CONSUMERREPORT MAGAZINE, THIS CAR WAS CRAP FROM DAY ONE WHEN IT ROLLED OF THE TRUCK IN 2008Read more
Incident date: Dec 1, 2008
RADIO CHANGED OUT 2X AFTER ELECTRICAL PROBLEMS, LIGHT FOR AIR BAG HAS BEEN ON FOR 3 YRS. BRAKES HAVE HAD TO GET WORKED ON 2X BEFORE IT HIT 50,000, CLIP ON DRIVERSIDE MAT BROKE AFTER 2 MONTHS OF HAVING CAR, DOOR PANELS ON BOTH FRONT AND BACK PASSANGER SIDE KEPT FALLING OFF AND KEPT TAKING CAR BACK TO FIX TILL THEY HAD NO REPLACEMENT PARTS THIS CAR SHOULD NOT BE ON THE ROAD THERE ARE MANY SAFETY ISS
... UES BLIND SPOTS BECAUSE OF THE DESIGN, AND ALL THE LITTLE ISSUES FROM 2 BATTERIES REPLACED TO 2 SETS OF BRAKE JOBS TO ELECTRICALS TO 3 SETS OF TIRES, AND THE CAR ONLY HAS 80,OOO MILES OR LESS. I'VE HAD IT 9 YRS MOSTLY AS A SECOND CAR AND ALWAYS PROBLEMS INCLUDING PAINT. BUT THE SAFETY ISSUES AND THE CRAP CAR WE WERE SOLD KEPT IT CAUSE NOBODY IN THERE RIGHT MIND WANTS IT I AM 1ST YR OWNER THIS CAR SUCKS FFFFFFF IS WHAT IT SHOULD RATE THE CAR DEALERS WONT FIX IT THEY MAKE YOU COME BACK AGAIN AND AGAIN THAT THE PARTS HAVE TO BE FOUND BECAUSE THE PLANT GOT WASHED AWAY AND THE PARTS WITH IT. AND THAT COMPANY WONT LET THEM HOLD PARTS IN THERE SHOPS SO HURRY UP AND WAIT IT IS THE TRAINSHAF IS CRACKED BUT HEY ITS A SECOND CAR THAT COST TOO MUCH AND GIVES TOO LITTLE JUST FOUND THIS WEBSITE THANK TO CONSUMERREPORT MAGAZINE, THIS CAR WAS CRAP FROM DAY ONE WHEN IT ROLLED OF THE TRUCK IN 2008Read more
Incident date: Feb 15, 2016
THE HEAD LIGHTS KEEP BLOWING OUT, ESPECIALLY THE LEFT FRONT. I FIND MYSELF CHANGING THIS BULB EVERY 3-5 MONTHS. NOW THE HIGH BEAMS DO NOT TURN ON FROM THE FORWARD POSITION AT THE STEERING WHEEL, THEY WILL WORK WHEN THE ARM IS PULLED BACK WITH THE HIGH BEAM LIGHT INDICATING THEY ARE WORKING, NOT THE SAME IN THE FORWARD POSITION. I HAVE CHECKED THE FUSES AND BULB. I AM TIRED OF THESE PROBLEMS
... AND IT IS A DEFINITE SAFETY HAZARD. SUZUKI SHOULD GET ON BOARD TO FIX THESE REOCCURRING PROBLEMS FOR EVERY OWNER. BUT SINCE SUZUKI NO LONGER EXISTS IN THE UNITED STATES, IT WILL BE UP TO NHTSA.Read more
Incident date: Jan 15, 2016
THE PASSENGER SIDE AIRBAG SENSING UNIT IS NOT RECOGNIZING THE PRESENCE OF A PASSENGER. THE AIRBAG REMAINS OFF EVEN THOUGH THE FRONT PASSENGER SEAT IS OCCUPIED BY AN ADULT.
Incident date: Dec 14, 2015
I HAD BEEN PROBLEMS WITH THE FRONT HEADLIGHTS, I HAD TWO TICKETS AS RESULTS OF THIS PROBLEMS. I HAD REPLACED THEM AT LEAST 6 TIMES A YEAR. ALSO A LOT OF PROBLEMS WITH THE HEAT AND COOLING. I RECENTLY REPLACE ALL THE COMPONENTS FROM PUMP, RADIATOR,THERMOSTAT AND THE LAST ONE HEATING CORD MORE $4000.00 FOR A 2010. MAKE NO SENSE AT ALL. AND THE WORST IS THAT WE DO NOT HAVE ANY SUPPORT FROM THE ZUSUKI
... . BAD PURCHASES ON THIS CAR.Read more
Incident date: Dec 28, 2015
CVT BOLT AND PULLEY GRINDS; WHICH MAY CAUSE BELT TO BREAK. IF RIDER IS AT A HIGH SPEED, THIS COULD CAUSE A THREATENING ACCIDENT. SUZUKIBURGMAN USA FOREM SUGGESTS THIS IS A HUGE ISSUE WITH 2003-2013 SUZUKI BURGMAN 650'S. OUR BURGMAN IS UNSAFE AND NOW NOT DRIVABLE DUE TO CVT BOLT "MUSHROOMING" WHERE IT CONNECTS TO BEARING, CAUSING A HIGH PITCH WINDING NOISE. IT ALSO HAS A GRINDING NOISE.
Incident date: Dec 28, 2015
CVT BOLT AND PULLEY GRINDS; WHICH MAY CAUSE BELT TO BREAK. IF RIDER IS AT A HIGH SPEED, THIS COULD CAUSE A THREATENING ACCIDENT. SUZUKIBURGMAN USA FOREM SUGGESTS THIS IS A HUGE ISSUE WITH 2003-2013 SUZUKI BURGMAN 650'S. OUR BURGMAN IS UNSAFE AND NOW NOT DRIVABLE DUE TO CVT BOLT "MUSHROOMING" WHERE IT CONNECTS TO BEARING, CAUSING A HIGH PITCH WINDING NOISE. IT ALSO HAS A GRINDING NOISE.
Incident date: Jun 20, 2009
TRANSMISSION RANGE SENSOR FAILURE.
Incident date: Feb 19, 2014
TL* THE CONTACT OWNS A 2006 SUZUKI AN650 BURGMAN SCOOTER. WHILE DRIVING APPROXIMATELY 40 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE RESTARTED A FEW MOMENTS LATER. THE CONTACT REPLACED THE IGNITION SWITCH HIMSELF, BUT THE FAILURE RECURRED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER ISSUED NHTSA CAMPAIGN NUMBER: 05V372000 (ELECTRICAL SYSTEM) FOR THE 2003 AND 2004 MODEL YEARS. THE MANU
... FACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 60,000.Read more
Incident date: Jun 20, 2009
TRANSMISSION RANGE SENSOR FAILURE.
Incident date: Feb 2, 2016
TL* THE CONTACT OWNS A 2014 SUZUKI DL1000. THE CONTACT STATED THAT THAT THE MOTORCYCLE WOULD STALL. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS INFORMED THAT THE PARTS NEEDED TO ORDERED AND NO FURTHER INFORMATION WAS AVAILABLE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 1,900.
Incident date: Apr 1, 2015
TAKATA RECALL: THE STEERING WHEEL LIGHT KEEP COMING ON AND OFF. IM NOT SURE WHY, I KEEP FLUID IN THE TUBE. THE ENGINE LIGHT NEVER GOES OFF. THIS ALL HAPPENEDES IN APRIL 2015 AT THE HOUSE ADDRESS THE CAR FIRST PURCHASED.
Incident date: Apr 1, 2015
TAKATA RECALL: THE STEERING WHEEL LIGHT KEEP COMING ON AND OFF. IM NOT SURE WHY, I KEEP FLUID IN THE TUBE. THE ENGINE LIGHT NEVER GOES OFF. THIS ALL HAPPENEDES IN APRIL 2015 AT THE HOUSE ADDRESS THE CAR FIRST PURCHASED.
Incident date: Apr 1, 2015
TAKATA RECALL: THE STEERING WHEEL LIGHT KEEP COMING ON AND OFF. IM NOT SURE WHY, I KEEP FLUID IN THE TUBE. THE ENGINE LIGHT NEVER GOES OFF. THIS ALL HAPPENEDES IN APRIL 2015 AT THE HOUSE ADDRESS THE CAR FIRST PURCHASED.
Incident date: Jan 21, 2016
TL* THE CONTACT OWNS A 2006 SUZUKI FORENZA. WHILE THE VEHICLE WAS PARKED IN THE DRIVEWAY, A FIRE STARTED ON THE REAR DRIVER SIDE PASSENGER DOOR WITHOUT WARNING. THE FIRE CONSUMED THE REAR SEATS AND EXTENDED FROM THE REAR TO THE FRONT FLOOR. THE CONTACT WAS ABLE TO EXIT THE VEHICLE AND EXTINGUISH THE FLAMES. A FIRE INSPECTION REPORT WAS NOT PROCESSED BY A FIRE DEPARTMENT AND THE VEHICLE HAD NOT BEE
... N DIAGNOSED YET TO DETERMINE THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT WAS WAITING ON A RESPONSE TO HAVE THE VEHICLE TOWED TO A DEALER FOR DIAGNOSTIC TESTING AND REPAIR. THE FAILURE MILEAGE WAS NOT AVAILABLE.Read more
Fire
Incident date: Jan 21, 2016
TL* THE CONTACT OWNS A 2006 SUZUKI FORENZA. WHILE THE VEHICLE WAS PARKED IN THE DRIVEWAY, A FIRE STARTED ON THE REAR DRIVER SIDE PASSENGER DOOR WITHOUT WARNING. THE FIRE CONSUMED THE REAR SEATS AND EXTENDED FROM THE REAR TO THE FRONT FLOOR. THE CONTACT WAS ABLE TO EXIT THE VEHICLE AND EXTINGUISH THE FLAMES. A FIRE INSPECTION REPORT WAS NOT PROCESSED BY A FIRE DEPARTMENT AND THE VEHICLE HAD NOT BEE
... N DIAGNOSED YET TO DETERMINE THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT WAS WAITING ON A RESPONSE TO HAVE THE VEHICLE TOWED TO A DEALER FOR DIAGNOSTIC TESTING AND REPAIR. THE FAILURE MILEAGE WAS NOT AVAILABLE.Read more
Fire
Incident date: Dec 16, 2015
SINCE 2012 I HAVE PURCHASED THIS SUV ITS GIVING ME TROUBLE RELATED TO LOW BEAM LIGHT. I HAVE REPLACED THIS LIGHT FOR AT LEAST 5 TIMES. MANY PEOPLE ON DIFFERENT WEBSITE HAVE REGISTERED THE SAME PROBLEM AND ARE HAVING SAME KIND OF PROBLEM. PLEASE HELP US TO GET A PERMANENT SOLUTION TO THIS ISSUE.
Incident date: Jan 28, 2016
TL* THE CONTACT OWNS A 2012 SUZUKI SX4. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V587000 (STEERING) HOWEVER, THE PART NEEDED TO REPAIR THE VEHICLE WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. THE VIN WAS UNAVAILABLE
... .Read more
Incident date: Jan 20, 2016
UPLOAD FORWARDED
Incident date: Jan 20, 2016
UPLOAD FORWARDED
Incident date: Nov 17, 2015
THE "TRANS RANGE SWITCH" IS CAUSING MY CAR TO JUMP TO 2 GEAR RANDOMLY. THE CAR SEEMS TO RUN FINE AFTER O START IT. AND OUT OF NO WERE THE ENGINE JUMPS AND THE "ENGINE LIGHT" COMES ON THE CAR ACTS LIKES ITS NOT IN 1ST GEAR. IT CAN'T GET IT TO GO INTO GEAR (DRIVE OR REVERSE) WITHOUT IT JUMPING. THEN AFTER THE CAR SITS FOR A DAY IT ACTS FINE FOR THE FIRST TRIP AND THEN IT STARTS THE SAME PROBLEM AGAI
... N AFTERWARDS. I CAN'T GO UPHILL EITHER WITHOUT IT REAVING HIGH LIKE ITS IN NEUTRAL. I THINK THIS IS THE "TRANS RANGE SWITCH" GOING BAD.Read more
Incident date: Feb 15, 2004
I FACE THE HEAT ENGINE AND ELECTRICAL PROBLEMS LIKE THE OTHER SUZUKI CARS OF SIMILAR MODELS DRIVING IN THE HIGHWAY.
Incident date: Feb 15, 2004
I FACE THE HEAT ENGINE AND ELECTRICAL PROBLEMS LIKE THE OTHER SUZUKI CARS OF SIMILAR MODELS DRIVING IN THE HIGHWAY.
Incident date: Feb 15, 2004
I FACE THE HEAT ENGINE AND ELECTRICAL PROBLEMS LIKE THE OTHER SUZUKI CARS OF SIMILAR MODELS DRIVING IN THE HIGHWAY.
Incident date: Jun 6, 2015
THERE IS A VIOLENT SHUDDER WHEN TAKING OFF IN FIRST GEAR WHICH IS VERY DANGEROUS ON A MOTORCYCLE WHEN PULLING OUT INTO TRAFFIC. TALKING TO OTHER OWNERS AND MECHANIC...IT SEEMS TO BE A PROBLEM WITH THE CLUTCH AND SPRINGS AND APPARENTLY A PROBLEM WITH SEVERAL OF THESE BIKES.
Incident date: Jan 7, 2016
TL* THE CONTACT OWNED A 2005 SUZUKI FORENZA. WHILE DRIVING 50 MPH, THE CONTACT'S VEHICLE REAR ENDED ANOTHER VEHICLE. THE AIR BAGS FAILED TO DEPLOY. THE VEHICLE WAS DESTROYED AND TOWED FROM THE SCENE. A POLICE REPORT WAS FILED. THE CONTACT SUSTAINED INJURIES TO THE THROAT, LEFT WRIST, AND KNEE. MEDICAL ATTENTION WAS REQUIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VIN WAS UNKNOWN. TH
... E FAILURE MILEAGE WAS APPROXIMATELY 120,000.Read more
Crash
1 injured
Incident date: Jan 15, 2013
I HAVE HAD ISSUES WITH THE STEERING ON MY 2012 SUZUKI KIZASHI, IT WANTS TO PULL ON BOH SIDES OF THE HIGHWAY, AND THE SUSPENSION IS REALLY ROUGH. MY MAIN CONCLUSION IS THAT I GOT THIS CAR BECAUSE I LIKED IT, NOW I EXPECTED NO SUCH PROBLEMS AS IM HAVING AND NOBODY WILL FIX IT THEY JUST KEEP TELLING ME TO GET AN ALIGNMENT AND IVE HAD MANY ALIGNMENTS DONE, I AM NOT THREATENING ANYBODY, I WANT MY CAR F
... IXED I RELY ON THIS CAR AND CANT AFFORD TO GET ANOTHER ONE, SO IF YA COULD HELP GET IT FIXED IT WOULD MUCH APPRECIATED.Read more
Incident date: Jan 15, 2013
I HAVE HAD ISSUES WITH THE STEERING ON MY 2012 SUZUKI KIZASHI, IT WANTS TO PULL ON BOH SIDES OF THE HIGHWAY, AND THE SUSPENSION IS REALLY ROUGH. MY MAIN CONCLUSION IS THAT I GOT THIS CAR BECAUSE I LIKED IT, NOW I EXPECTED NO SUCH PROBLEMS AS IM HAVING AND NOBODY WILL FIX IT THEY JUST KEEP TELLING ME TO GET AN ALIGNMENT AND IVE HAD MANY ALIGNMENTS DONE, I AM NOT THREATENING ANYBODY, I WANT MY CAR F
... IXED I RELY ON THIS CAR AND CANT AFFORD TO GET ANOTHER ONE, SO IF YA COULD HELP GET IT FIXED IT WOULD MUCH APPRECIATED.Read more
Incident date: Jan 18, 2012
AIRBAG LIGHT HAS BEEN ON IN THE INSTRUMENT CLUSTER FOR FOUR YEARS. AFTER RECIEVED RECALL NOTIFICATION VIA MAIL (1 YEAR AGO). SUBMITTED REQUEST TO FIX PASSENGER SEAT TO THE ONLY SUZUKI DEALERSHIP ON OHAU, HAWAII AND THEY STATED, "MY VEHICLE DIDN'T FALL UNDER THE RECALL" AND THAT THEY NEEDED TO REPAIR THE ENTIRE AIRBAG SYSTEM. THEY COULDN'T PIN POINT THE PROBLEM AND REFUSED TO CONTACT SUZUKI TECH
... NICAL REPRESENTATIVES. AS THE SECOND OWNER AND ACTIVE DUTY MILITARY, I CANNOT GO BACK TO THE STATE IN WHICH I BOUGHT THE VEHICLE DUE TO MILITARY ORDERS TO HAVE ANY OTHER SUZUKI DEALERSHIP FIX THIS. ADDITIONALLY, WITH THE SAFTEY INSPECTION LAWS IN HAWAII, I CANNOT REGISTER THIS CAR IN THIS STATE UNLESS PAY FOR THE ENTIRE REPLACEMENT OF THE AIRBAG SYSTEM OR WAIT TILL THE DEALERSHIP CHANGES THIER MIND ABOUT DOING THE RECALL ON MY CAR. THIS SITUATION I AM IN NOW IS UNSATISFACTORY AND PUTS MY FAMILY AND MY SELF AT RISK.Read more
Incident date: Dec 31, 2015
12/31/15 -- OUTSIDE TEMP APPROX 8 DEG F, VEHICLE DEFROSTER FAILED TO ACTUATE, WINDSHIELD FROZE OVER INTERNALLY WORSE & WORSE, FINALLY RESORTED TO USE ICE SCRAPER ON INSIDE OF WINDSHIELD WHILE DRIVER CONTINUED ON STATE HWY. HEATED AIR WAS COMING OUT DASH VENTS, FLOOR, BUT NOT A WHIFF FROM DEFROSTER. WAS ON THE WAY TO A HOSPITAL, KEPT DRIVING TIL ABOUT 12 MILES ALONG SUDDENLY DEFROSTER VENTS ACTUA
... TED, BLOWING HEATED AIR LIKE CRAZY. BUT HAD I NOT BEEN ALONG, SPOUSE WOULD HAVE BEEN HARD-PRESSED TO SAFELY PULL OFF OR GET TO SURGERY APPOINTMENT. SINCE HEAT WAS BLOWING OUT OF OTHER VENTS, INDICATES ACTUATOR FAULT. PROBLEM NOT DIAGNOSED, NOT SURE IF TEMP.-RELATED OR INTERMITTENT FAULT. IN SNOWSTORM OR AT NIGHT COULD HAVE BECOME REALLY SERIOUS EVENT (RECENTLY PURCHASED USED, NOT SURE OF HISTORY) 124000 MILESRead more
Incident date: Dec 28, 2015
TL* THE CONTACT OWNS A 2010 SUZUKI EQUATOR. THE CONTACT STATED THAT THE AIR BAG WARNING LIGHT REMAINED ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER, BUT IT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 72,000.
Incident date: Jan 12, 2009
MY LIGHTS ARE ALWAYS GOING OUT ITS HARD TO SEE AT NIGHT WHEN THEY ARE ON AND I CONSIDERED VERY DANGEROUS AND WENT DEALER WHERE I BOUGHT IT AND THEY TELL ME THEY CAN'T FIX IT JUST KEEP CHANGING LIGHTS WHEN THEY GO OUT NOT GOOD
Incident date: Dec 9, 2015
TL* THE CONTACT OWNS A 2008 SUZUKI FORENZA. THE CONTACT STATED THAT THE DRIVER SIDE AIR BAG WARNING LIGHT ILLUMINATED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 78,125.
Incident date: Dec 17, 2015
TL* THE CONTACT OWNS A 2010 SUZUKI EQUATOR. WHILE DRIVING 40 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE COOLANT MIXED IN WITH THE TRANSMISSION FLUID. AS A RESULT, THE TRANSMISSION NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 83,000.
Incident date: Dec 17, 2015
TL* THE CONTACT OWNS A 2010 SUZUKI EQUATOR. WHILE DRIVING 40 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE COOLANT MIXED IN WITH THE TRANSMISSION FLUID. AS A RESULT, THE TRANSMISSION NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 83,000.
Incident date: May 1, 2007
STARTING AT ABOUT 30,000 MILES, THE CAR BEGAN BLOWING LOW BEAM/DRIVING LIGHT BULBS EVERY 3 TO 5 MONTHS. SOMETIMES THE DRIVER-SIDE, SOMETIMES THE PASSENGER SIDE, SOMETIMES BOTH. THE BLOWN BULBS SEEM TO BLOW OUT DURING THE DAYTIME, WHEN THEY ARE ACTING AS DAYTIME RUNNING LIGHTS, BUT AREN'T NOTICED UNTIL NIGHT. THE DATE BELOW IS THE APPROXIMATE DATE OF THE FIRST OCCURRENCE.
Incident date: Jun 12, 2014
THE VEHICLE WOULD RANDOMLY PERFORMING IN VERY ODD MANNERS SUCH AS STALLING WHILE DRIVING DOWN THE HIGHWAY, ELECTRICAL SYSTEMS (LIGHTS, STEREO, ETC) TURNING OFF AND ON RANDOMLY, REDUCING SPEED IGNORING ACCELERATOR POSITION AS WELL AS MANY OTHERS. SEVERAL VISITS TO DIFFERENT MECHANICS FOUND NO ISSUES WITH THE VEHICLE. WHILE SITTING ON THE SIDE OF THE ROAD AT ONE POINT WAITING FOR A TOW TRUCK I NOT
... ICED THAT THE PASSENGER FLOOR WAS SOAKING WET AND WE HAD NOT HAD RAIN FOR MANY DAYS. AFTER DOING MY OWN INVESTIGATING I FOUND THAT THE DRAIN PAN FOR THE A/C CONDENSER IS LOCATED INSIDE THE CAR BEHIND THE STEREO JUST TO THE LEFT OF THE GLOVE BOX. THE DRAIN PAN HAS A HOSE THAT ROUTES THROUGH THE FIREWALL AND DRAINS ONTO THE GROUND FROM UNDER THE HOOD. THIS DRAIN HOSE BECAME CLOGGED AND AS A RESULT ALL OF THE WATER FROM THE A/C CONDENSATION WAS OVERFLOWING AND DRAINING DIRECTLY ONTO THE ECU AND THEN ONTO THE PASSENGER FLOOR. THIS WATER WAS CAUSING THE ECU TO MISBEHAVE WHICH WAS CREATING A DANGEROUS SITUATION BUT BY TIME THE VEHICLE WAS TAKEN TO A MECHANIC THE WATER HAD DRIED AND THE CAR WAS BEHAVING PROPERLY. ONCE THE DRAIN HOSE WAS CLEARED THERE WERE NO FURTHER PROBLEMS. AFTER CHECKING ON SOME SUZUKI FORUMS I FOUND A COUPLE OTHERS THAT HAD THE SAME SITUATION ARISE. IT'S A FIX THAT TAKES LESS THAN A HALF HOUR AND REQUIRES NO PARTS BUT NOT ONE THAT MECHANICS KNOW ABOUT AND CREATES A DANGEROUS SITUATION WITH THE COMPUTER ACTING UNPREDICTABLY AND FREQUENTLY CAUSING THE CAR TO STALL IN THE MIDDLE OF THE ROADWAY.Read more
Incident date: Jun 12, 2014
THE VEHICLE WOULD RANDOMLY PERFORMING IN VERY ODD MANNERS SUCH AS STALLING WHILE DRIVING DOWN THE HIGHWAY, ELECTRICAL SYSTEMS (LIGHTS, STEREO, ETC) TURNING OFF AND ON RANDOMLY, REDUCING SPEED IGNORING ACCELERATOR POSITION AS WELL AS MANY OTHERS. SEVERAL VISITS TO DIFFERENT MECHANICS FOUND NO ISSUES WITH THE VEHICLE. WHILE SITTING ON THE SIDE OF THE ROAD AT ONE POINT WAITING FOR A TOW TRUCK I NOT
... ICED THAT THE PASSENGER FLOOR WAS SOAKING WET AND WE HAD NOT HAD RAIN FOR MANY DAYS. AFTER DOING MY OWN INVESTIGATING I FOUND THAT THE DRAIN PAN FOR THE A/C CONDENSER IS LOCATED INSIDE THE CAR BEHIND THE STEREO JUST TO THE LEFT OF THE GLOVE BOX. THE DRAIN PAN HAS A HOSE THAT ROUTES THROUGH THE FIREWALL AND DRAINS ONTO THE GROUND FROM UNDER THE HOOD. THIS DRAIN HOSE BECAME CLOGGED AND AS A RESULT ALL OF THE WATER FROM THE A/C CONDENSATION WAS OVERFLOWING AND DRAINING DIRECTLY ONTO THE ECU AND THEN ONTO THE PASSENGER FLOOR. THIS WATER WAS CAUSING THE ECU TO MISBEHAVE WHICH WAS CREATING A DANGEROUS SITUATION BUT BY TIME THE VEHICLE WAS TAKEN TO A MECHANIC THE WATER HAD DRIED AND THE CAR WAS BEHAVING PROPERLY. ONCE THE DRAIN HOSE WAS CLEARED THERE WERE NO FURTHER PROBLEMS. AFTER CHECKING ON SOME SUZUKI FORUMS I FOUND A COUPLE OTHERS THAT HAD THE SAME SITUATION ARISE. IT'S A FIX THAT TAKES LESS THAN A HALF HOUR AND REQUIRES NO PARTS BUT NOT ONE THAT MECHANICS KNOW ABOUT AND CREATES A DANGEROUS SITUATION WITH THE COMPUTER ACTING UNPREDICTABLY AND FREQUENTLY CAUSING THE CAR TO STALL IN THE MIDDLE OF THE ROADWAY.Read more
Incident date: Dec 2, 2015
HEADLIGHT BULBS BURN OUT MUCH TOO OFTEN. SINCE 2010, I HAVE TAKEN THE CAR INTO THE DEALER ELEVEN TIMES TO REPLACE ONE OR SEVERAL BURNED OUT LIGHT BULBS. ON ONE OCCASION ALL FOUR PRIMARY BULBS BURNED OUT AT ONE TIME. I HAVE RECEIPTS OF EVERY VISIT. DURING THE LAST CHANGE ON 12/2/15 THE DEALER INFORMS ME THAT SUZUKI WOULD NO LONGER COVER THE BULB REPLACEMENT AND LABOR . THE BUMPER NEEDS TO BE R
... EMOVED TO REPLACE BULBS, SO THIS IS NOT A CHEAP EXERCISE, NOT TO MENTION THE SAFETY PROBLEMS OF BULBS BURNING OUT SO OFTEN.Read more
Incident date: Dec 7, 2015
TL* THE CONTACT OWNS A 2008 SUZUKI FORENZA. THE CONTACT STATED THAT THE PASSENGER SIDE AIR BAG IN THE SEAT INADVERTENTLY DEPLOYED CAUSING SIGNIFICANT INJURY TO THE CONTACTS EARDRUM AND THE SEAT WAS DESTROYED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 100,000. THE VIN WAS NOT AVAILABLE.
Incident date: Oct 2, 2015
TL* THE CONTACT OWNS A 2007 SUZUKI XL7. WHILE DRIVING AT VARIOUS SPEEDS, THE PASSENGER SIDE AIR BAG WARNING INDICATOR ILLUMINATED ON THE INSTRUMENT PANEL. THE CONTACT STATED THAT THE FAILURE WOULD OCCUR INTERMITTENTLY. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE FLEXIBILITY OF THE SENSOR WOULD MAKE THE SENSOR READ THE PASSENGER'S WEIGHT INTERMITTENTLY. THE VEHI
... CLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 125,225.Read more