Showing 2,833 complaints for SCION
Incident date: Jan 2, 2017
EXCESSIVE OIL CONSUMPTION BETWEEN OIL CHANGES, I NEED TO CHECK THE LEVEL EVERY MONTH AND ADD OIL IF NEEDED. WHEN I TURN ON THE VEHICLE, THE RADIO TURNS ON ALONE OR TURNS ITSELF OFF, WITHOUT PRESSING THE BUTTON. THESE 2 COMPLAINTS HAVE BEEN GOING ON FOR MORE THAN TWO YEARS.
Incident date: Jan 2, 2017
EXCESSIVE OIL CONSUMPTION BETWEEN OIL CHANGES, I NEED TO CHECK THE LEVEL EVERY MONTH AND ADD OIL IF NEEDED. WHEN I TURN ON THE VEHICLE, THE RADIO TURNS ON ALONE OR TURNS ITSELF OFF, WITHOUT PRESSING THE BUTTON. THESE 2 COMPLAINTS HAVE BEEN GOING ON FOR MORE THAN TWO YEARS.
Incident date: Mar 2, 2019
BEFORE I TOOK MY CAR IN FOR RECALL I MADE SURE IT WAS IN TIP TOP SHAPE NO LEAKS OR NOISES OF ANY KIND, NO ISSUES WHATSOEVER! POST J02 VALVE SPRING RECALL CAR WAS RETURNED WITH A 1/2' HOLE IN EXHAUST MANIFOLD DEALER SAYS IT WAS MY FAULT ALTHOUGH IT HAPPENED WHILE IN THEIR POSSESSION IT WAS AT THAT TIME THE SHOP FOREMAN DECIDED NOT TO ADDRESS THE ENGINE SQUALLING AROUND 5K RPM AND INSTRUCTED ME TO F
... IX THE EXHAUST AND DRIVE IT. 3K MILES LATER I'M DRIVING DOWN THE ROAD 55MPH NORMALLY THE CARS STARTS BOGGING DOWN AND LESS THAN A MILE LATER STARTS KNOCKING VIOLENTLY AS I TURN AT AN INTERSECTION THE VEHICLE JUST DIES LEAVING ME QUICKLY EXITING THE VEHICLE TRYING TO PUSH IT OUT OF THE ROAD WITH THE HELP OF PASSING MOTORIST I FINALLY SUCCEEDED AFTER MY CAR HALF IN THE INTERSECTION SAT FOR 15 MIN BLOCKING TRAFFIC AND POTENTIALLY CAUSING ACCIDENTS. DEALER WANTED ME TO PAY FOR INVESTIGATION IF THEY DETERMINED I WAS AT FAULT. I DECIDED NOT TO LET THEM CONTINUE AND CHOOSE TO HAVE A PRIVATE REPAIR FACILITY INVESTIGATE WHAT CAUSED THE FAILURE. THEY DETERMINED THAT SEALANT HAD BEEN SUCKED INTO THE OIL PICKUP TUBE CLOGGING THE SCREEN ESSENTIALLY STARVING MY ENGINE OF OIL LEADING TO CATASTROPHIC FAILURE. THIS RECALL IS THE FIRST AND ONLY TIME MY VEHICLES ENGINE HAS BEEN WORKED ON LEADING THE PRIVATE REPAIR FACILITY TO DETERMINE THE DEALER AT FAULT WITH A PROBABLE CAUSE BEING CARELESSNESS REMOVING OLD SEALANT FROM ENGINE AND TIMING COVER. CURRENTLY BEING TREATED AS A LIAR BY DEALER WHILE PROVIDING THE FINDINGS FROM PRIVATE REPAIR FACILITY TRYING TO GET THEM TO FIX MY CAR.Read more
Incident date: Apr 22, 2019
FOLLOWING THE J02 RECALL WORK MY 2013 FRS WAS PICKED UP AND BROUGHT TO ME 4.1 MILES AWAY WHEN I GOT OFF WORK AND STARTED MY VEHICLE I NOTICED A TICKING SOUND COMING FROM THE BACK PASSENGER SIDE OF THE ENGINE. UPON ACCELERATION THERE IS A DISTINCT KNOCKING COMING FROM THE ENGINE, SINCE THEN I HAVE DRIVEN 12.7 MILES INCLUDING THE DISTANCE BACK TO THE DEALER WHERE THE VEHICLE IS ONCE AGAIN. THERE ALS
... O APPEARS TO BE WAY TOO MUCH SEALANT APPLIED TO THE ENGINE WHEN THEY PUT IT BACK TOGETHER.Read more
Incident date: Apr 18, 2019
RECEIVED VAVLE SPRING RECALL NOTICE IN NOVEMBER AND READ UP ON THE RECALL, REALIZED IN JANUARY THERE WERE TONS OF FAILURES AFTER RECALL. HELD OFF UNTIL MARCH 1 WHEN I SAW NEW TRAINING HAD BEEN DONE. TOOK CAR IN FOR RECALL SERVICE TO NORTHRIDGE TOYOTA AT 100,1XX MILES. MARCH 12TH GOT THE CAR BACK. DROVE IT UNTIL APRIL 18TH NOTICED LIGHT KNOCKING NOISE, APRIL 19TH CAR STARTED SHAKING VIOLENTLY AT A
... STOP LIGHT. UPON ACCELERATING CAR STARTED HORRENDOUSLY KNOCKING AND SCREECHING. HAD CAR TOWED BACK TO DEALER WITH 101,0XX MILES (LESS THAN THE MANDATORY 1200 MILE WARRANTY ON SERVICES TOYOTA HAS). TOYOTA STATES NOT RELATED TO RECALL, AND REQUESTS $2700 TO JUST TAKE THE ENGINE OUT AND LOOK AT IT. REP STATED MIGHT BE OIL RELATED AND SENT PHOTO OF OIL PAN WITH GOLDEN OIL IN IT (FROM RECALL) AND ABOUT A POUND OF METAL FLAKES. CONTACTED CORPORATE FILED A CLAIM AND AM AWAITING RESPONSE. ABSOLUTELY ABSURD THEY STILL HAVE THE NERVE TO SAY THIS ISNT RELATED WHEN SO MANY PEOPLE ARE HAVING THE SAME ISSUE.Read more
Incident date: Apr 21, 2019
THE PASSAGER REAR CALIPER MALFUNCTION CAUSE THE BRAKE PAD FLY AWAY FROM THE RIGHT REAR BRAKE
Incident date: Apr 8, 2019
I TOOK MY CAR IN FOR A RECALL REPAIR REGARDING REPLACEMENT OF THE ENGINE VALVE SPRINGS ON 1/8/19. THE CAR WAS READY FOR PICKUP TWO AND A HALF WEEKS LATER ON 1/25/19. AFTER EXACTLY TWO MONTHS, ON MARCH 8TH MY CAR BEGAN SHAKING AND WOBBLING WHILE I WAS DRIVING ON THE FREEWAY. WHEN THE CHECK ENGINE LIGHT TURNED ON AND I NOTICED MY CAR BEGAN SLOWING DOWN, I IMMEDIATELY PULLED OVER TO THE SIDE RIGHT SI
... DE OF THE HIGHWAY AS THE CAR SHUT OFF. AFTER I TRIED TURNING IT BACK ON, THE CAR WOULD TURN OFF AFTER A COUPLE SECONDS. I GOT THE CAR TOWED BACK HOME AND CONTACTED TOYOTA. THEY DID NOT PROVIDE A TOW TRUCK SO I HAD TO TOW IT IN FOR THEM TO INSPECT IT. IN THE FIRST UPDATE, THEY TOLD ME IT HAD SOMETHING TO DO WITH THE LUBRICATION ON THE SIDES OF THE ENGINE. DURING THE SECOND AND FINAL UPDATE THEY HAD A SECOND TECH COME IN FOR INSPECTION AND CONCLUDED IT WAS AN INTERNAL ENGINE FAILURE. I AM NOW IN WORSE SITUATION THAN BEFORE AND I FEEL LIKE I AM BEING CHARGED TO FIX SOMETHING THAT WAS NOT BROKEN IN THE FIRST PLACE. NOT TO MENTION THE ESTIMATE TO FIX AND INSTALL A BRAND NEW ENGINE WILL COST UP TO $11,000. I AM CURRENTLY AWAITING FOR A RESPONSES FROM CORPORATE.Read more
Incident date: Apr 8, 2019
I TOOK MY CAR IN FOR A RECALL REPAIR REGARDING REPLACEMENT OF THE ENGINE VALVE SPRINGS ON 1/8/19. THE CAR WAS READY FOR PICKUP TWO AND A HALF WEEKS LATER ON 1/25/19. AFTER EXACTLY TWO MONTHS, ON MARCH 8TH MY CAR BEGAN SHAKING AND WOBBLING WHILE I WAS DRIVING ON THE FREEWAY. WHEN THE CHECK ENGINE LIGHT TURNED ON AND I NOTICED MY CAR BEGAN SLOWING DOWN, I IMMEDIATELY PULLED OVER TO THE SIDE RIGHT SI
... DE OF THE HIGHWAY AS THE CAR SHUT OFF. AFTER I TRIED TURNING IT BACK ON, THE CAR WOULD TURN OFF AFTER A COUPLE SECONDS. I GOT THE CAR TOWED BACK HOME AND CONTACTED TOYOTA. THEY DID NOT PROVIDE A TOW TRUCK SO I HAD TO TOW IT IN FOR THEM TO INSPECT IT. IN THE FIRST UPDATE, THEY TOLD ME IT HAD SOMETHING TO DO WITH THE LUBRICATION ON THE SIDES OF THE ENGINE. DURING THE SECOND AND FINAL UPDATE THEY HAD A SECOND TECH COME IN FOR INSPECTION AND CONCLUDED IT WAS AN INTERNAL ENGINE FAILURE. I AM NOW IN WORSE SITUATION THAN BEFORE AND I FEEL LIKE I AM BEING CHARGED TO FIX SOMETHING THAT WAS NOT BROKEN IN THE FIRST PLACE. NOT TO MENTION THE ESTIMATE TO FIX AND INSTALL A BRAND NEW ENGINE WILL COST UP TO $11,000. I AM CURRENTLY AWAITING FOR A RESPONSES FROM CORPORATE.Read more
Incident date: Apr 12, 2019
ON HIGHWAY, VEHICLE @ 3400-4000 RPM, 70-75 MPH, A HEAVY KNOCKING NOISE STARTED FROM THE ENGINE, MOMENTS LATER SAME KNOCKING CAN BE HEARD AT 2000 RPM, HAD TO PULL OVER ON HIGHWAY. AS SOON AS THE CAR FULLY STOPPED (WHILE STILL IN DRIVE) THE ENGINE STALLED OUT AND COULD NOT TURN BACK ON. HAD THE VEHICLE TOWED BACK TO THE DEALERSHIP THAT PERFORMED THE RECALL WORK FOR THE SPRING VALVES REPLACEMENT. TH
... EY TORE DOWN THE MOTOR AND ADVISED ME THE ISSUE WAS A SPUN ROD.Read more
Incident date: Apr 5, 2019
MY CAR WAS BROUGHT IN FOR THE RECALL FOR THE FAULTY VALVE SPRINGS. AFTER ABOUT A MONTH AND A HALF THE ENGINE BEGAN KNOCKING. I TOOK IT BACK TO THE DEALER AND AFTER LOOKING AT THE ENGINE THEY WANTED RECORDS OF REGULAR VEHICLE MAINTENANCE. THEY WANTED THIS TO MAKE SURE MAINTENANCE WAS DONE BECAUSE TOYOTA CORPORATE SUGGESTED TO REPLACE THE WHOLE ENGINE . I CHANGE MY OWN OIL BUT KEEP TRACK OF THE MILE
... AGE AND DATE I CHANGED IT AND GAVE THAT TO THE DEALERSHIP TO SEND TO TOYOTA CORPORATE. THEY DENIED THE ENGINE WITH NO REASONING.Read more
Incident date: Oct 15, 2018
THE AIRBAG INDICATOR LIGHT CAME ON AND WILL NOT GO OFF
Incident date: Apr 15, 2019
"OIL COMP RECALL" WENT TO MY LOCAL TOYOTA DEALERSHIP TALKED TO THE ASSTI SERVICE MANAGER AND WAS TOLD I COULD NOT DO THE RECALL THERE THAT I WOULD HAVE TO GO BACK TO THE PLACE THAT FIRST TESTED IT. I BOUGHT THE CAR AND IT WAS TESTED IN ALABAMA I LIVE IN FL. WENT TO THE TOYOTA DEALERSHIP AND THEY SAID IT WAS IN FINAL STAGES THAT THEY JUAT HAVE TO PREFORM THE RECALL THE FINAL STEP. WHICH IS THE WORK
... . THE ASSTI MANAGER WAS VERY VERY RUDE AND TOLD ME ID HAVE TO GO TO ALABAMA TO GET IT DONE. I AM LOSIBG ATLEAAT 2 QTS OR MORE OF OIL EVERY 2 WEEKS. THIS IS CAUSING ALOT OF ISSUES RUNNING WISE. MY CAT CONVERTER WENT OUT DUE TO THIS AS WELL. I WANT TO GET IT DONE AS SOON AS POSSIBLE CAUSE I HAVE A LITTLE GIRL AND ITS MY DAILY AND I DONT WANT SOMETHING TO HAPPEN.Read more
Incident date: Feb 1, 2019
TL* THE CONTACT OWNS A 2013 SCION FR-S. AFTER THE VEHICLE WAS SERVICED PER NHTSA CAMPAIGN NUMBER: 18V772000 (ENGINE), IT IMMEDIATELY EXPERIENCED LOSS OF POWER AND SPUTTERING. THE VEHICLE WAS TAKEN BACK TO HAMER TOYOTA (11041 SEPULVEDA BLVD, MISSION HILLS, CA) WHERE IT WAS DIAGNOSED THAT THE ENGINE GASKET AND CAMSHAFT WERE FAULTY AND NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE
... RECURRED APPROXIMATELY TWO MONTHS LATER. THE VEHICLE WAS TAKEN BACK TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE ENGINE ROD BEARING WAS FAULTY. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT INDICATED THAT THE FAILURES WERE NOT PRESENT PRIOR TO THE RECALL REPAIR. THE FAILURE MILEAGE WAS 92,400.Read more
Incident date: Mar 26, 2019
I BROUGHT MY 2013 SCION FRS IN FOR A J02 VALVE SPRING REPLACE AND NOT EVEN 1,100 MILES LATER I HAD ENGINE PROBLEMS THAT LED TO THE DAMAGE TO MY "ROCKER ARM , CAMSHAFT " TWO WEEKS LATER THE DEALERSHIP SAYS THEY WILL NOT REPAIR THE DAMAGE 100% DUE TO THE DAMAGE WASNT CAUSED FROM THE INITIAL RECALL. AND MY WARRANTY IS VOIDED BECAUSE THEY DID THE RECALL. MY VEHICLE HAS BEEN AT THE HENDRICK TOYOTA FOR
... A MONTH NOW AND I DONT KNOW HOW I'M GOING TO GET IT BACK.Read more
Incident date: Jan 26, 2019
I JUST PURCHASED MY SCION XB IN JANUARY 2019 AND WITHIN THREE WEEKS I HAD THE OIL LIGHT FLASHING SO I TOOK IT TO GET AN OIL CHANGE AT MIDTOWN TOYOTA IN CHICAGO. WITHIN A FEW WEEKS I NOTICED THAT MY OIL LIGHT STARTED FLASHING AGAIN SO I CHECKED MOTOR OIL AND CAME TO FIND OUT THAT I DIDN'T HAVE ANY OIL. I CALLED MIDTOWN TOYOTA WHERE I HAD MY CAR SERVICED AND ASKED HIM IF MY VEHICLE HAD A RECALL AS
... FAR AS THE OIL PROBLEM THAT I WAS HAVING? HE SAID YES THERE WAS A RECALL ON MY VEHICLE, HOWEVER THE RECALL HAD EXPIRED IN JANUARY 2018. NOW I'VE HAD THE CAR. NOW I'VE ONLY HAD THE CAR FOR TWO MONTHS WHICH I'M FINANCING AND THE SERVICE DEPARTMENT TOLD ME THAT I WILL HAVE TO PAY OUT-OF-POCKET FOR THIS CAR TO GET THAT RECALL FIXED. I DO NOT FEEL THAT IT'S FAIR FOR ANY DEALER I DO NOT FEEL THAT IT'S FAIR FOR ANY DEALERSHIP TO SELL A VEHICLE THAT HAS RECALLS AND THAT HAVE NOT BEEN TAKEN CARE OF BY THE PREVIOUS OWNERS IN THE PAST. IS THERE ANYTHING THAT TOYOTA CAN DO FOR ME TO GET THIS RE-CAR FIXED FREE OF CHARGE AS I AM DONE NEW OWNER OF THIS VEHICLE?Read more
Incident date: Mar 15, 2019
I WAS NOTIFIED BY MAIL THAT THEY'RE WAS A SAFETY RECALL FOR MY 2013 ACIOM FRS WHICH WAS TO REPLACE MY ENGINE SPRING VALVE AT NO COST. I TOOK IN MY CAR JANUARY 18 TO HAVE THE WORK DONE IT TOOK AROUND 2 WEEKS TO GET A RESPOND BACK THAT MY CAR WAS READY FOR PICK UP. I TOOK IT OUT AND DROVE IT FOR ABOUT 5 MILE TO GET GAS AND WHEN I TURNED ON MY CAR IT WAS STRUGGLING TO TURN ON AND ONCE IT TURNED ON IT
... WAS IT WAS SHAKING VIOLENTLY , 3 ENGINE CODES CAME UP P0017 P0300P219A. I TOOK IT IMMEDIATELY TO TOYOTA AND ALL THEY DID WAS CLEAR MY ENGINE CODES DROVE MY CAR FOR ABOUT 30 MILES AND HANDED IT BACK TO ME SAYING IT WAS SAFE TO DRIVE. I HAD MY CAR FOR ABOUT 2,000 MILES I WAS DRIVING BACK HOME AT NIGHT AND I HEARD A LOUD POP INSIDE MY ENGINE SO I PARKED THE CAR. THE NEXT DAY I WAS GOING TO MY FRIEND HOUSE TO CHANGE MY BRAKES AND WHILE I WAS ON THE FREEWAY I HEAD A SOFT ENGINE KNOCKING AND IT BECAME LOUDER AND LOUDER UNTIL THE ENGINE COMPLETLY DIED ON ME AND I WAS STRANDED. TOYOTA SEND A TOW TRUCK TO PICK UP MY CAR AND WHEN THEY INSPECTED THE ENGINE THEY SAID I HAD A CYLINDER THAT WAS DESTROYED AND A ROD BEARING DESTROYED AND THEY SAID IT WAS DUE TO 'OIL STARTVATION'. I'VE OWNED THAT CAR FOR A YEAR AND I HAVE NEVER HAD A SINGLE ISSUE WITH IT, UNTIL NOW THAT THEY WORKED ON MY ENGINE. THEY ARE TELLING ME I GOTTA PAY $8,600 OUT OF POCKET FOR A WHOLE NEW SHORT BLOCK AND THEY DON'T WANT TO TAKE RESPONSIBILITY FOR THE DAMAGES OCCUR AFTER THEIR WORK.Read more
Incident date: Mar 15, 2019
I WAS NOTIFIED BY MAIL THAT THEY'RE WAS A SAFETY RECALL FOR MY 2013 ACIOM FRS WHICH WAS TO REPLACE MY ENGINE SPRING VALVE AT NO COST. I TOOK IN MY CAR JANUARY 18 TO HAVE THE WORK DONE IT TOOK AROUND 2 WEEKS TO GET A RESPOND BACK THAT MY CAR WAS READY FOR PICK UP. I TOOK IT OUT AND DROVE IT FOR ABOUT 5 MILE TO GET GAS AND WHEN I TURNED ON MY CAR IT WAS STRUGGLING TO TURN ON AND ONCE IT TURNED ON IT
... WAS IT WAS SHAKING VIOLENTLY , 3 ENGINE CODES CAME UP P0017 P0300P219A. I TOOK IT IMMEDIATELY TO TOYOTA AND ALL THEY DID WAS CLEAR MY ENGINE CODES DROVE MY CAR FOR ABOUT 30 MILES AND HANDED IT BACK TO ME SAYING IT WAS SAFE TO DRIVE. I HAD MY CAR FOR ABOUT 2,000 MILES I WAS DRIVING BACK HOME AT NIGHT AND I HEARD A LOUD POP INSIDE MY ENGINE SO I PARKED THE CAR. THE NEXT DAY I WAS GOING TO MY FRIEND HOUSE TO CHANGE MY BRAKES AND WHILE I WAS ON THE FREEWAY I HEAD A SOFT ENGINE KNOCKING AND IT BECAME LOUDER AND LOUDER UNTIL THE ENGINE COMPLETLY DIED ON ME AND I WAS STRANDED. TOYOTA SEND A TOW TRUCK TO PICK UP MY CAR AND WHEN THEY INSPECTED THE ENGINE THEY SAID I HAD A CYLINDER THAT WAS DESTROYED AND A ROD BEARING DESTROYED AND THEY SAID IT WAS DUE TO 'OIL STARTVATION'. I'VE OWNED THAT CAR FOR A YEAR AND I HAVE NEVER HAD A SINGLE ISSUE WITH IT, UNTIL NOW THAT THEY WORKED ON MY ENGINE. THEY ARE TELLING ME I GOTTA PAY $8,600 OUT OF POCKET FOR A WHOLE NEW SHORT BLOCK AND THEY DON'T WANT TO TAKE RESPONSIBILITY FOR THE DAMAGES OCCUR AFTER THEIR WORK.Read more
Incident date: Mar 15, 2019
I WAS NOTIFIED BY MAIL THAT THEY'RE WAS A SAFETY RECALL FOR MY 2013 ACIOM FRS WHICH WAS TO REPLACE MY ENGINE SPRING VALVE AT NO COST. I TOOK IN MY CAR JANUARY 18 TO HAVE THE WORK DONE IT TOOK AROUND 2 WEEKS TO GET A RESPOND BACK THAT MY CAR WAS READY FOR PICK UP. I TOOK IT OUT AND DROVE IT FOR ABOUT 5 MILE TO GET GAS AND WHEN I TURNED ON MY CAR IT WAS STRUGGLING TO TURN ON AND ONCE IT TURNED ON IT
... WAS IT WAS SHAKING VIOLENTLY , 3 ENGINE CODES CAME UP P0017 P0300P219A. I TOOK IT IMMEDIATELY TO TOYOTA AND ALL THEY DID WAS CLEAR MY ENGINE CODES DROVE MY CAR FOR ABOUT 30 MILES AND HANDED IT BACK TO ME SAYING IT WAS SAFE TO DRIVE. I HAD MY CAR FOR ABOUT 2,000 MILES I WAS DRIVING BACK HOME AT NIGHT AND I HEARD A LOUD POP INSIDE MY ENGINE SO I PARKED THE CAR. THE NEXT DAY I WAS GOING TO MY FRIEND HOUSE TO CHANGE MY BRAKES AND WHILE I WAS ON THE FREEWAY I HEAD A SOFT ENGINE KNOCKING AND IT BECAME LOUDER AND LOUDER UNTIL THE ENGINE COMPLETLY DIED ON ME AND I WAS STRANDED. TOYOTA SEND A TOW TRUCK TO PICK UP MY CAR AND WHEN THEY INSPECTED THE ENGINE THEY SAID I HAD A CYLINDER THAT WAS DESTROYED AND A ROD BEARING DESTROYED AND THEY SAID IT WAS DUE TO 'OIL STARTVATION'. I'VE OWNED THAT CAR FOR A YEAR AND I HAVE NEVER HAD A SINGLE ISSUE WITH IT, UNTIL NOW THAT THEY WORKED ON MY ENGINE. THEY ARE TELLING ME I GOTTA PAY $8,600 OUT OF POCKET FOR A WHOLE NEW SHORT BLOCK AND THEY DON'T WANT TO TAKE RESPONSIBILITY FOR THE DAMAGES OCCUR AFTER THEIR WORK.Read more
Incident date: Jun 15, 2018
CANT HANDLE A INSTANT BRAKE.
Crash
Incident date: Feb 1, 2019
TL* THE CONTACT OWNS A 2006 SCION XB. THE CONTACT STATED THAT THE FUSE BOX UNDERNEATH THE STEERING WHEEL WAS MALFUNCTIONING AND THE WIRE WAS HOT, WHICH CREATED A POSSIBLE FIRE HAZARD. THE FAILURE ALSO CAUSED THE LIGHT SWITCH, MIRROR SWITCH, TRACTION CONTROL SWITCH, AIR BAGS, AND DOOR LOCKS NOT TO WORK AFTER THE FAILURE. THE DEALER AND MANUFACTURER WERE NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED
... OR REPAIRED. THE FAILURE MILEAGE WAS 174,000.Read more
Incident date: Apr 6, 2019
I GOT A RECALL NOTICE FROM TOYOTA, AND TOOK IT IN FEBRUARY 2, 2019 FOR THE VALVE SPRING REPLACEMENT. I GOT MY CAR BACK FEBRUARY 12TH 2019 & AFTER LEAVE THE DEALER THAT DAY IT STARTED BOGGING, SO I RETURNED IT TO ELIMINATE THE SOUND THAT VERY NIGHT. AFTER RETURNING IT, I GOT MY CAR BACK FEBRUARY 13TH 2019 EVERYTHING APPEARED TO BE FINE UNTIL THIS PAST WEEKEND, APRIL 6TH I HEARD A POP IN THE ENGINE.
... I BEGAN TO HEAR KNOCKING COMING FROM THE MOTOR AND LOST POWER IMMEDIATELY WHILE ON THE FREEWAY, I TRIED TURNING IT ON BUT THE MOTOR WAS DEAD ALL LIGHTS ON THE DASH WERE ON. I WENT IN, IN ATTEMPT TO "FIX" MY CAR DUE TO THE RECALL NOTICE, WHICH HAS LEAD ME TO HAVE A COMPLETELY INOPERABLE CAR.Read more
Incident date: Apr 5, 2019
DURING NORMAL DRIVING OF THE VEHICLE, THERE HAS BEEN RANDOM LOSS OF POWER STEERING ON THE CAR. A LIGHT APPEARS ON THE DASH AND A SHORT WARNING SIGNAL SOUNDS. MANUAL STEERING TAKES OVER ON THE CAR. LOSS OF POWER STEERING OCCURRED DURING NORMAL DRIVING AT RANDOM TIMES AND HAS OCCURRED WITH INCREASING FREQUENCY, AS MUCH AS 5 TIMES AN HOUR, MAKING THE CAR UNSAFE TO OPERATE. THE CUT OUT APPEARS TO BE
... COMPLETELY RANDOM AS IT HAPPENED ON BOTH SIDE STREETS MAIN ROADS, AFTER THE ENGINE WAS WARMED UP, AND BOTH IN MOTION AND STATIONARY. IT HAS OCCURRED APPROXIMATELY 12-15 TIMES OVER THE PAST FIVE MONTHS WITH INCREASING FREQUENCY. THE MANUAL STEERING REMAINS ENGAGED UNTIL THE CAR IS TURNED OFF AND ON AGAIN, ALTHOUGH WHEN THE POWER STEERING CUTS OUT AGAIN AFTER RESTARTING IS RANDOM, IT HAPPENED BOTH IMMEDIATELY, SEVERAL MINUTES AFTER, 30 MINUTES AFTER, AND NOT AT ALL.Read more
Incident date: Mar 22, 2019
LESS THAN 1000 MILES AFTER BRINGING MY CAR TO TOYOTA TO HAVE MANDATORY RECALL WORK PERFOMED INVOKVING VALVE SPRINGS, MY ENGINE DIED. THE ENGINE HAS A SPUN BEARING, LIKELY DUE TO OIL STARVATION. I WAS DRIVING ALONG THE HIGHWAY, AND WHEN I STOPPED FOR FUEL, I NOTICED A TICK THAT SOON BECAME A KNOCK. THE CAR WAS BOGGING DOWN ON IDLE AND ALMOST STALLED NUMEROUS TIMES. I DROVE IT TO A TOYOTA SERVICE CE
... NTER THAT HAPPENED TO BE LESS THAN 2 MILES AWAY.Read more
Incident date: Feb 20, 2019
AIR BAG LIGHT CAME ON AM WHILE DRIVING DOWN A BUMPY COUNTY ROAD. NO ERROR CODE. UNABLE TO RESET. VEHICLE MILEAGE RIGHT AT 150K.
Incident date: Mar 18, 2019
EXPERIENCE SUDDEN LOSS OF POWER AND ENGINE FAILURE 37 MILES AFTER THE J02 RECALL WAS PERFORMED. I WAS DRIVING FOR ABOUT 10 MINUTES WHEN SUDDENLY FELT THE ENGINE HAD LOST POWER, TURNED THE ENGINE OFF AND COASTED TO GET OUT OF THE WAY OF TRAFFIC. NOTICED A LOT OF SMOKE COMING OUT OF THE HOOD AND A OIL LEAKING FROM UNDER THE ENGINE. -DROPPED OFF THE CAR FOR THE J02 RECALL TO BE DONE ON 11 MARCH 2019
... WITH 42,581 MILES. -RECALL DONE, CAR PICKED UP ON 16 MARCH 2019. -ENGINE FAILED ON 18 MARCH 2019, MILLAGE 42,618. THE DEALER TECHNICIAN EXPLAINED THAT A RIGHT SIDE INTAKE ROCKER HAD COME LOOSE AND SUBSEQUENTLY WAS PINCHED BY THE EXHAUST CAM, EJECTING IT THROUGH THE VALVE COVER. THE ROCKER BLEW A WHOLE THROUGH THE VALVE COVER CAUSING A LARGE AMOUNT OF OIL TO POUR ON TO THE HOT EXHAUST MANIFOLD. SINCE THEN, THE DEALERSHIP ASSUMED THE COST OF THE REPAIRS BUT DO NOT ACCEPT RESPONSIBILITY FOR THE FAILURE.Read more
Incident date: Apr 2, 2019
ON MARCH 19TH 2019 I HAD THE J02 VALVE SPRING RECALL PERFORMED ON MY 2013 SCION FRS WITH 74,502 MILES ON THE ODOMETER. WORK WAS DONE BY WYATT JOHNSON TOYOTA OF CLARKSVILLE TN. I CHOSE THIS DEALER BECAUSE THE ALSO OWN A SUBARU DEALERSHIP. THEY ASSURED ME THAT THIS WAS THE 12TH FRS THAT THEY HAD PERFORMED THE RECALL ON WITH NO HISTORY OF PROBLEMS. I PICKED UP MY CAR 3 DAYS LATER WITH 74,505 MILES. I
... DROVE THE 100 MILES TO MY HOME VIA INTERSTATE 24, RUNNING AT 70-80 MPH. I NOTICED A TICKING NOISE AFTER AN HOUR OF DRIVING. BY DESTINATIONS END I HAD SEVERE RATTLING NOISE FROM DRIVERS SIDE OF ENGINE AND ROUGH IDLE. NOW WITH 294 MILES TOTAL SINCE REPAIR AFTER THE ENGINE IS RUNNING ROUGHER AND EMITTING SQUEALING AND RATTLING, ROUGH IDLE AND TRYING TO DIE. IT WAS SUGGESTED BY WYATT JOHNSON TOYOTA THAT I NOT DRIVE THE CAR TO THEM FOR INSPECTION RATHER TAKE IT TO MY LOCAL DEALER. I DELIVERED THE CAR TO COAD TOYOTA OF PADUCAH KY TODAY, APRIL 2ND 2019 WITH 74,801 MILES. I AWAIT THIER INSPECTION. THIS WAS A GREAT RUNNING ENGINE. NOW I SUSPECT IT IS ON THE VERGE OF FAILURE. I HAVE SUGGESTED DRAINING AND INSPECTING THE OIL FOR EVIDENCE OF UNUSUAL WEAR.Read more
Incident date: Feb 19, 2019
I HAD THE J02 VALVE SPRING RECALL DONE AND 2 WEEKS AND ROUGHLY 80 MILES LATER MY ENGUNE DEVELOPED A KNOCKING NOISE AND STARTED LOSING POWER THE DEALERSHIP THAT PERFORMED THE RECALL DENIED RESPONSIBILITY EVEN AFTER FINDING FIPG SEALENT IN MY OIL PICKUP
Incident date: Feb 19, 2019
I HAD THE J02 VALVE SPRING RECALL DONE AND 2 WEEKS AND ROUGHLY 80 MILES LATER MY ENGUNE DEVELOPED A KNOCKING NOISE AND STARTED LOSING POWER THE DEALERSHIP THAT PERFORMED THE RECALL DENIED RESPONSIBILITY EVEN AFTER FINDING FIPG SEALENT IN MY OIL PICKUP
Incident date: Jan 31, 2018
TL* THE CONTACT OWNS A 2013 SCION FR-S. THE CONTACT STATED THAT THE CHECK ENGINE INDICATOR ILLUMINATED. THE VEHICLE WAS SERVICED PER NHTSA CAMPAIGN NUMBER: 18V772000 (ENGINE AND ENGINE COOLING) BY AUTONATION TOYOTA LAS VEGAS (6300 W SAHARA AVE, LAS VEGAS, NV 89146, (702) 605-5801); HOWEVER, THE CHECK ENGINE WARNING INDICATOR REMAINED ILLUMINATED AFTER THE RECALL REPAIR. THE MANUFACTURER WAS MADE A
... WARE OF THE FAILURE AND DID NOT ASSIST. THE FAILURE MILEAGE WAS 69,449.Read more
Incident date: Feb 11, 2019
AFTER RECEIVING MY CAR AFTER THE RECALL WAS PERFORMED, 15 MILES INTO DRIVING IT HOME MY ENGINE BEGAN TO KNOCK AND SLOW DOWN ON THE FREEWAY. THIS SAFETY RECALL PUT ME AT RISK. THE DEALERSHIP STATED THAT THEY WILL NOT COMPENSATE FOR THE PRICE OF A NEW ENGINE AND TRIED TO BLAME IT ON ME, COMPLETELY DISREGARDING ALL OF THE OTHER VEHICLES JUST LIKE ME AFTER THIS RECALL. I PURCHASED AN ENGINE ON MY OWN
... EXPENSE AFTER THAT OCCURRED, AND THAT ENGINE IS BAD. I CANNOT BELIEVE THIS TOYOTA DEALERSHIP ISN'T COMPENSATING LIKE OTHERS DID.Read more
Incident date: Mar 17, 2019
VALVE SPRINGS RECALL: WAS GETTING OFF THE FREEWAY, AND WENT TO TURN AND REALIZED MY CAR SHUT OFF (ALL LIGHTS ON), AND WOULDN'T TURN BACK ON (LIGHTS DISAPPEARED) , BUT GOT IT TO START AGAIN AFTER A COUPLE OF MINUTES, AND DIED AGAIN, AND HAPPENED 3 OR 4 TIMES AND IT WAS SPUTTERING / SHAKING AS IF IT WAS OUT OF GAS BUT MY GAGE WAS A LITTLE ABOVE A QUARTER AND PULLED INTO A GAS STATION 50 FT IN FRONT
... OF ME FILLED UP AND TURNED THE CAR ON, AND ABOVE 2000 RPM'S STARTS MAKING A HORRIBLE NOISE. I HAD THE RECALL DONE ON IT LAST MONTH (VALVE SPRINGS) , WHILE MY CAR WAS THERE MY VACUUM PUMP WENT OUT AND THE TECHNICIAN ONLY REALIZED AFTER PUTTING THE ENGINE BACK IN, AND ENDED UP TAKING THE WHOLE ENGINE APART AGAIN AND PUT BACK TOGETHER AND REALIZED IT WAS THE VACUUM PUMP, TRIED TO SEND ME ON MY WAY BUT ENDED UP TALKING TO A MANAGER WHO ATE THE COST AND OFF I WENT 3 OR 4 DAYS LATER DUE TO GETTING THE PART, NO ISSUES SINCE THEN UNTIL NOW. WENT AND DID SOME RESEARCH AND COME TO FIND OUT OVER 40 OTHER HAVE HAD THE SAME ISSUE AS I HAVE AFTER THE RECALL AND IT TURNED OUT THAT TOYOTA HAD USED THE WRONG SEALANT OF SOME SORT AND NOW MY ENGINE HAS THROWN A ROD, AND THEY'RE MAKING ME PAY FOR IT! $5000-$7500 FOR THEIR MISTAKE!!! THE DEALERSHIP TOLD ME I HAVE TO REPLACE THE WHOLE SHORT BLOCK, OR REBUILD MY ENTIRE ENGINE. THEY SENT OUT ONE OF THEIR GM'S AND HE SAID THEY DID EVERYTHING RIGHT OBVIOUSLY NOT! I HAVE A SPREADSHEET OF 40 OTHERS THAT THIS HAS HAPPENED TO AS WELL AS 4 DIFFERENT NEWS ARTICLES REGARDING THE SAME ISSUES. I HAVE SPENT OVER 8 HOURS ON THE PHONE WITH EITHER TOYOTA OR THE DEALERSHIP ITSELF. NO HELP. HTTPS://WWW.FT86CLUB.COM/FORUMS/SHOWTHREAD.PHP?T=133521 HTTPS://WWW.THEDRIVE.COM/NEWS/26848/SCION-FR-S-SUBARU-BRZ-OWNERS-SAY-VALVE-SPRING-RECALL-FIX-IS-DESTROYING-THEIR-ENGINES HTTPS://DOCS.GOOGLE.COM/SPREADSHEETS/D/1SEL4X84CY_YNRKCWS9GNOIYNTWLJDOTGQZU1J4RLZOW/EDIT#GID=0Read more
Incident date: Feb 17, 2019
ON JAN 26, 2019, I SEND MY 2013 FRS TO DO THE VALVE SPRING RECALL BY TOYOTA, WHICH LASTS ABOUT TWO WEEKS. AFTER ABOUT 200 MILES ADDED, I HEARD A COUPLE OF TIMES OF ABNORMAL NOISE FROM THE ENGINE, IT WAS LIKE RHYTHMIC KNOCKING. THEY HAPPENED RIGHT AFTER I STARTED THE ENGINE AND CAN BE CLEARLY NOTICED. THE NOISE BECAME WEAK IN ABOUT 1 MINUTE. IN ADDITION, I DROVE IT FOR ANOTHER 200 MILES AND THE AVE
... RAGE MPG DECREASED FROM 34 TO 30.Read more
Incident date: Mar 14, 2019
I HAD THE J02 RECALL WORK COMPLETED AT WALSER TOYOTA IN BLOOMINGTON, MN IN EARLY FEBRUARY 2019. 800 MILES LATER, I NOTE A TICKING NOISE WHILE EXITING THE FREEWAY. THE CAR STALLED REPEATEDLY AS I LIMPED THE CAR TO SAFETY AND HAD THE CAR TOWED TO THE DEALERSHIP. SIMILAR TO DOZENS OF OTHER OWNERS REPORTING ISSUE WITH ENGINE FAILURE AFTER THE J02 RECALL ON THE FT86CLUB.COM MESSAGE BOARDS, MY ENGI
... NE SPUN A BEARING DUE TO OIL STARVATION. IT IS UNKNOWN IF THE ENGINE FAILURE IS POOR WORKMANSHIP OR A FAILURE WITH THE RECALL PROCEDURE/PARTS.Read more
Incident date: Mar 26, 2019
2008 - SCION - TOYOTA - BURNING OIL, BURNING A QUART OF OIL IN LESS THAN EVERY 800 MILES. CAR IS UP TO DATE WITH ALL MAINTENANCE. MECHANIC REFERRED US TO DEALERSHIP. TOYOTA ISSUED A TSB - 'SOME 2006 ' 2011 MODEL YEAR VEHICLES EQUIPPED WITH THE 2AZ-FE ENGINE MAY EXHIBIT ENGINE OIL CONSUMPTION. THE PISTON ASSEMBLY HAS BEEN CHANGED TO MINIMIZE OIL CONSUMPTION.' AND THAT 'P030# (CYLINDER # MISFIRE DET
... ECTED) DTC MAY ALSO BE SET AS A RESULT OF OIL CONSUMPTION.' HOWEVER DEALERSHIP REFUSES TO EVEN TEST OR REPAIR THE VEHICLE. SAYING WE ONLY HAD UNTIL AUG 2017. WE WERE NEVER NOTIFIED OF SUCH ISSUES, NO LETTERS OR ANYTHING WERE SENT TO US. CAR HAS ALWAYS BEEN REGISTERED AND OUR OWNER INFO HAS ALWAYS BEEN AVAILABLE TO TOYOTA. SO NOW WE ARE STUCK WITH DEFECTIVE VEHICLE.Read more
Incident date: Aug 25, 2013
I WAS IN A CAR ACCIDENT I WAS THE PASSENGER .WE WERE ON CAR ACCIDENT WE ROLLED SEVERAL TIMES IN THE AIRBAGS NEVER COME OFF. I'M A QUADRIPLEGIC I BROKED C6. I FLEW OUT OFF THE SUN ROOF.THE CAR WAS ON MOTION ON A STREE. I WAS FOUND 62 FEET FROM THE CAR
Crash
1 injured
Incident date: Mar 1, 2018
WHITE PAINT. THE PAINT STARTING FLAKING OFF IN LARGE SHEETS ON IT'S OWN, NO CONNECTION TO VEHICLE DAMAGE, WEATHER, ETC. PAINT IS NOW GONE FROM MY ENTIRE ROOF, HALF THE HOOD, MULTIPLE OTHER PLACES. CONTINUES CHIPPING AND FLAKING, CAR IS ONLY 8 YEARS OLD AND THIS IS AN OBVIOUS DEFECT. BEEN HAPPENING FOR OVER A YEAR, ABOUT 1/3 OF THE PAINT ON MY CAR IS NOW GONE. CAN PROVIDE LOTS OF PICTURES.
Incident date: Feb 12, 2019
CAR BURNING OIL, 128000 MILES. OIL LIGHT CAN ON BEFORE OIL CHANGE WAS NEEDED. CHECKED OIL LEVEL IT WAS REALLY LOW. NO VISIBLE LEAKS. I HAD TO ADD 1 QUART OF OIL 1 MONTH GETTING OIL CHANGED. I HAVE READ THAT SCION XB HAS HAD A PROBLEM WITH OIL CONSUMPTION BECAUSE OF THE PISTON RINGS IN PREVIOUS MODELS.WONDERING IF MY CAR IS HAVING THE SAME PROBLEM
Incident date: Mar 20, 2019
WHEN AT A STOP THE ENGINE STARTS TO SHAKE LIKE IT'S ABOUT TO TURN OFF WE BOUGHT IT WITH 29000 MILES NOTICED IT A WEEK AFTER WE BOUGHT IT AND IT HAS DONE IT A FEW TIMES THE TOYOTA DEALERSHIP COULDN'T FIND ANY CODES TO REMEDY IT. THE CHECK ENGINE DOES NOT COME ON BUT IT DOES SHAKE VIOLENTLY.IT HAS 35000 MILES NOW.I HAD THE THROTTLE BODY CLEANED AND IT STILL PUTTERS AT THE LIGHT. MOSTLY WITH THE A/C
... OFFRead more
Incident date: Jul 4, 2015
ENGINE IS BURNING AT LEAST 1 QUART OF OIL PER WEEK AND ESTIMATED DRIVING MILES PER WEEK IS BETWEEN 200 MILES TO 300 MILES. THERE IS NO MAJOR OIL LEAKS ANYWHERE THAT I CAN SEE AND THERE IS NO OIL ON THE FLOOR WHERE THE CAR IS PARKED.
Incident date: Mar 12, 2009
OIL CONSUMPTION
Incident date: Jan 15, 2019
TL* THE CONTACT OWNS A 2014 SCION XB. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 19V005000 (AIR BAGS). THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. MIKE ERDMAN TOYOTA (4650 FL-520, COCOA, FL 32926, (321) 453-1313) WAS CONTACTED AND CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT MAD
... E AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT. CONSUMER STATED ALL ISSUES WERE RESOLVED.*JBRead more
Incident date: Mar 12, 2019
SECOND TIME THIS HAPPENED...FIRST THEY SAID BATTERY...WHILE DRIVING, INDICATING WARNING LIGHTS ON DASH START BLINKING (ABS, CHECK ENGINE, TRACTION, AND OTHERS), THEN THE ENGINE GOES INTO LOW HEAR AND STAYS UNTIL THE VEHICLE IS TURNED OFF AND BACK ON. DURING THESE EPISODES THE SPEED ODOMETER IS ERRATIC. ALSO WHEN IN THIS STATE, THE REVERSE GEAR DOES NOT ENGAGE. WHEN THIS STARTED IT WAS A ONCE A MON
... TH PROBLEM, THEN WEEKLY, NOW IT HAPPENS DAILY/HOURLY. IT STARTED AT APPROXIMATELY 40,000 MILES. THIS HAPPENS WHILE DRIVING ON CITY STREETS AND HIGHWAY, MOST OF THE TIME AT STOPS AND LOWER SPEEDS BUT DOES HAPPEN ON FREEWAY TOO.Read more
Incident date: Mar 12, 2019
SECOND TIME THIS HAPPENED...FIRST THEY SAID BATTERY...WHILE DRIVING, INDICATING WARNING LIGHTS ON DASH START BLINKING (ABS, CHECK ENGINE, TRACTION, AND OTHERS), THEN THE ENGINE GOES INTO LOW HEAR AND STAYS UNTIL THE VEHICLE IS TURNED OFF AND BACK ON. DURING THESE EPISODES THE SPEED ODOMETER IS ERRATIC. ALSO WHEN IN THIS STATE, THE REVERSE GEAR DOES NOT ENGAGE. WHEN THIS STARTED IT WAS A ONCE A MON
... TH PROBLEM, THEN WEEKLY, NOW IT HAPPENS DAILY/HOURLY. IT STARTED AT APPROXIMATELY 40,000 MILES. THIS HAPPENS WHILE DRIVING ON CITY STREETS AND HIGHWAY, MOST OF THE TIME AT STOPS AND LOWER SPEEDS BUT DOES HAPPEN ON FREEWAY TOO.Read more
Incident date: Mar 12, 2019
SECOND TIME THIS HAPPENED...FIRST THEY SAID BATTERY...WHILE DRIVING, INDICATING WARNING LIGHTS ON DASH START BLINKING (ABS, CHECK ENGINE, TRACTION, AND OTHERS), THEN THE ENGINE GOES INTO LOW HEAR AND STAYS UNTIL THE VEHICLE IS TURNED OFF AND BACK ON. DURING THESE EPISODES THE SPEED ODOMETER IS ERRATIC. ALSO WHEN IN THIS STATE, THE REVERSE GEAR DOES NOT ENGAGE. WHEN THIS STARTED IT WAS A ONCE A MON
... TH PROBLEM, THEN WEEKLY, NOW IT HAPPENS DAILY/HOURLY. IT STARTED AT APPROXIMATELY 40,000 MILES. THIS HAPPENS WHILE DRIVING ON CITY STREETS AND HIGHWAY, MOST OF THE TIME AT STOPS AND LOWER SPEEDS BUT DOES HAPPEN ON FREEWAY TOO.Read more
Incident date: Feb 17, 2019
I TOOK MY CAR IN FOR J02 ENGINE VALVE SPRING SAFETY RECALL ON JAN 29TH, 2019 AT A TOYOTA DEALERSHIP. TOOK THEM A COUPLE DAYS, BUT WHEN THEY FINISHED, THEY SAID THE CAR WAS GOOD AS NEW AND I COULD DRIVE IT NORMALLY. 2 WEEKS OF DAILY COMMUTE TO WORK WITH NO ISSUES, THEN ON FEB 17, 2019, I WAS DRIVING UP HIGHWAY 1 FOR A COUPLE HOURS, AS I CAME AROUND A TURN, I WAS GOING ABOUT 25MPH, I TAPPED TH
... E BRAKE TO SLOW DOWN AS THE ROAD WAS SLOPING DOWNHILL WITH TWO HAIR PIN TURNS UP AHEAD. AS SOON AS I HIT THE BRAKE, I FELT THE REAR WHEELS GIVE WAY A LITTLE AND THE TRACTION CONTROL LIGHT BLINK (I WAS GOING 25MPH, NO REASON FOR TRACTION CONTROL TO ENGAGE). THOUGHT IT WAS A LITTLE WEIRD, SO I LET OFF THE BRAKE, COASTED DOWNHILL A LITTLE AND THEN TRIED TAPPING THE BRAKES AGAIN, THE SAME THING HAPPENED. THINKING MY BRAKES ARE HAVING ISSUES, I TRIED TO SLOW DOWN BY SHIFTING FROM 3RD TO 2ND GEAR (MANUAL TRANSMISSION). WHEN I ENGAGED 2ND GEAR, I HEARD A POP AND SAW THE HOOD OF MY CAR JUMP UP AS IF SOMETHING INSIDE HIT IT AND SAW A LITTLE BIT OF SMOKE. SINCE I JUST PASSED THE FIRST HAIRPIN TURN, I WAS LOOKING AHEAD TO SAFELY PARK MY VEHICLE TO THE SIDE, BUT I FELT MY FEET AND LEGS WERE BURNING HOT. WHEN I LOOKED DOWN, I SAW FLAMES COMING FROM THE DRIVER SIDE TIREWELL THROUGH THE WINDOW, IT WAS AT THIS POINT, I REMEMBERED I JUST FILLED UP A FULL TANK 20 MILES BACK, SO I USED THE BRAKES TO COMPLETELY STOP THE CAR IN THE MIDDLE OF THE HIGHWAY - DISREGARDING ANY WARNING LIGHTS AND EXITED THE CAR. THE FIRE EVENTUALLY SPREAD AND BURNED THE ENTIRE CAR DOWN. I HAD NO CELL RECEPTION WHERE I WAS AT, SO I WAITED BY THE CAR UNTILL THE POLICE AND FIRE SHOWED UP.Read more
Fire
Incident date: Jan 10, 2018
MY AIR BAGS IN MY SEATS DON'T WORK AT ALL. NEITHER DOES MY AIR BAG IN MY WHEEL. THE TIRES SHAKES WHEN I DRIVE PAST 60 AND THE RIMS ARE NOT SAFE. THIS SHOULD NOT HAPPEN TO MY CHILD WHAT IF SHE GETS IN A ACCIDENT. THE SEAT BELT DOES NOT BUCKLE AND SEAT WILL NOT GO BACK. 95000 MILES AND THIS IS REDICULIOUS.
Incident date: Mar 11, 2019
TAKATA RECALL, I RECEIVED THE LETTER FROM TOYOTA AIR BAGS RECALL FRO MY SCION XB 2014, I CALLED TOYOTA (410 AND BANDERA IN SAN ANTONIO TX ) AND REFUSE TO MAKE AN APPOINTMENT FOR ME
Incident date: Jan 10, 2018
MY AIR BAGS IN MY SEATS DON'T WORK AT ALL. NEITHER DOES MY AIR BAG IN MY WHEEL. THE TIRES SHAKES WHEN I DRIVE PAST 60 AND THE RIMS ARE NOT SAFE. THIS SHOULD NOT HAPPEN TO MY CHILD WHAT IF SHE GETS IN A ACCIDENT. THE SEAT BELT DOES NOT BUCKLE AND SEAT WILL NOT GO BACK. 95000 MILES AND THIS IS REDICULIOUS.
Incident date: Jan 10, 2018
MY AIR BAGS IN MY SEATS DON'T WORK AT ALL. NEITHER DOES MY AIR BAG IN MY WHEEL. THE TIRES SHAKES WHEN I DRIVE PAST 60 AND THE RIMS ARE NOT SAFE. THIS SHOULD NOT HAPPEN TO MY CHILD WHAT IF SHE GETS IN A ACCIDENT. THE SEAT BELT DOES NOT BUCKLE AND SEAT WILL NOT GO BACK. 95000 MILES AND THIS IS REDICULIOUS.
Incident date: Mar 9, 2019
DID NOT GET NOTIFIED OF THE RECALL FOR MY VEHICLE.