Showing 2,833 complaints for SCION
Incident date: Dec 12, 2014
THE HEAD GASKET FAILED ON MY 2006 SCION TC. WHILE FIXING THE GASKET AND REMOVING THE HEAD BOLTS, PIECES OF THE ALUMINUM THREADS FROM THE ENGINE BLOCK CAME OUT ATTACHED TO THE BOLTS. THE ALUMINUM THREADS WRAPPED AROUND THEN BLOTS 2, 3 AND SOMETIMES 4 TIMES. IT WAS CLEAR THAT THIS WAS THE PROBLEM AND WHY THE HEAD GASKET HAD FAILED. -- THIS IS A PROBLEM IN THE 2000-2010 TOYOTA CAMRY AND SCION TC
... ENGINES. -- THIS SEARCH OF THE INTERNET SHOW THE EXTENT AND THE NUMEROUS OMPLAINT RELATED TO THIS PROBLEM. HTTPS://WWW.GOOGLE.COM/#Q=SCION+TC+HEAD+BOLTS+STRIPPED -- THIS VIDEO SHOWING HOW TO FIX THE PROBLEM. HTTPS://YOUTU.BE/GXEOAW3QP6M -- A RECALL AND/OR REIMBURSMENT PROGRAM NEED TO BE SETUP FOR THESE AUTOMOBILES. *TRRead more
Incident date: Mar 12, 2015
HEADING IN TO WORK, HEAR KNOCKING. PULL OVER, NO WARNING LIGHTS. CHECK OIL, IT'S LOW. HAS NEVER BEEN LOW, NOR LEAKED ANY, AND IT IS A ONE-OWNER CAR. PUT A QUART IN, KEEP HEADING TO WORK, STILL, NO WARNING LIGHTS. FRONT OF LONG BLOCK EXPLODED FORWARD TOWARD THE RADIATOR. DIDN'T KNOW WHAT THE EXPLOSION WAS UNTIL WE HOOKED UP TO THE WRECKER. ALUMINUM PARTS AND A PISTON LAYING UNDER THE ENGINE. MO
... TOR WAS OUT OF OIL. NO WARNING LIGHT CAME ON, IT WENT STRAIGHT TO HOT, AND BLEW. MY HONDA WOULDN'T LET YOU TURN IT ON IF IT WAS LOW ON OIL OR ANTIFREEZE. I LIKED THAT. THIS PROBLEM HURTS. *TRRead more
Incident date: Mar 12, 2015
HEADING IN TO WORK, HEAR KNOCKING. PULL OVER, NO WARNING LIGHTS. CHECK OIL, IT'S LOW. HAS NEVER BEEN LOW, NOR LEAKED ANY, AND IT IS A ONE-OWNER CAR. PUT A QUART IN, KEEP HEADING TO WORK, STILL, NO WARNING LIGHTS. FRONT OF LONG BLOCK EXPLODED FORWARD TOWARD THE RADIATOR. DIDN'T KNOW WHAT THE EXPLOSION WAS UNTIL WE HOOKED UP TO THE WRECKER. ALUMINUM PARTS AND A PISTON LAYING UNDER THE ENGINE. MO
... TOR WAS OUT OF OIL. NO WARNING LIGHT CAME ON, IT WENT STRAIGHT TO HOT, AND BLEW. MY HONDA WOULDN'T LET YOU TURN IT ON IF IT WAS LOW ON OIL OR ANTIFREEZE. I LIKED THAT. THIS PROBLEM HURTS. *TRRead more
Incident date: Mar 6, 2015
THERE HAD BEEN A BIG SNOWSTORM THE DAY PRIOR. I WAS DRIVING IN THE MORNING IN VERY COLD TEMPERATURES. THE ROADS HAD BEEN PLOWED BUT THERE WAS STILL SLUSH ON THE HIGHWAYS. WHILE DRIVING ON THE HIGHWAY, MY BRAKES FAILED TO STOP THE VEHICLE EVEN THOUGH I WAS NOT DRIVING AT AN INCREDIBLY FAST SPEED. I WAS FORCED TO PULL OVER ONTO THE SIDE OF THE ROAD AND WAIT AN HOUR FOR THE TEMPERATURES TO WARM UP. S
... INCE THEN, I HAVE NOTICED THAT THE BRAKES HAVE A REPEATED TENDENCY TO NOT PROPERLY SLOW DOWN THE CAR IN COLD CONDITIONS (BOTH RAIN AND SNOW). THE SYMPTOMS OF THIS INCIDENT VERY CLOSELY MATCH THE TOYOTA RECALL THAT WAS INITIATED FOR OTHER VEHICLES MANUFACTURED IN 2008 THAT HAD BRAKE FAILURES WHILE DRIVING IN SNOW AND COLD CONDITIONS. I CALLED TOYOTA CORPORATE HEADQUARTERS ON THE DAY OF THE INCIDENT TO REPORT WHAT HAD HAPPENED BUT THEY INSISTED THERE WAS NO RECALL FOR MY VEHICLE. THEY ADVISED ME TO HAVE THE VEHICLE INSPECTED. ON 21 MARCH, I TOOK THE VEHICLE INTO AN AUTO SHOP FOR A BRAKE INSPECTION. I WAS TOLD THAT THE BRAKE PADS APPEAR NEW AND THERE ARE NO NOTICEABLE ISSUES WITH MY BRAKES. *TRRead more
Incident date: Feb 2, 2011
ELECTRIC DOOR LOCKS HAVE INCREASINGLY BECOME A PROBLEM. FIRST, THE FRONT PASSENGER SIDE STOPPED WORKING AND NOW HAS TO BE MANUALLY LOCKED AND UNLOCKED. THEN THE SAME HAPPENED TO THE PASSENGER SIDE REAR, WHICH HAS TO BE LOCKED AND UNLOCKED MANUALLY. FINALLY, THE DRIVER'S DOOR HAS ON THREE OCCASIONS, LOCKED ME IN, FORCING ME TO ROLL DOWN THE WINDOW AND USE MY KEY TO GET OUT OF THE VEHICLE. I'VE
... NEVER HAD ANYTHING LIKE THIS HAPPEN W/ ANY OF THE OTHER VEHICLES I'VE OWNED. *TRRead more
Incident date: Mar 11, 2015
TL* THE CONTACT OWNS A 2006 TOYOTA SCION TC. WHILE DRIVING APPROXIMATELY 70 MPH, THE SUN ROOF SUDDENLY EXPLODED CAUSING GLASS TO FALL ONTO THE HEAD OF THE DRIVER. NO INJURIES WERE REPORTED. THE CAUSE OF THE FAILURE WAS NOT DIAGNOSED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED AND THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 05V483000 (VISIBI
... LITY). THE FAILURE MILEAGE WAS 96,000.Read more
Incident date: Mar 16, 2015
LOST POWER STEERING WHILE MAKING A U-TURN. WAS ABLE TO GAIN CONTROL BY STEERING HARD ON THE STEERING WHEEL! ALMOST CRASHING ONTO ANOTHER CAR. FOUND OUT THAT THEY'RE ARE SO MANY COMPLAINTS IN REGARDS TO THIS MATTER ONLINE. SCION WOULD NOT RECALL, OR INVESTIGATE FURTHER. COST OF REPAIR, TOW, DIAGNOSTIC IS IN THE $1500+! *TR
Incident date: Feb 2, 2015
I PURCHASED THE SCION XB 2008 NEW AND HAVE HAD ALL OIL CHANGES AND RECOMMENDED SERVICE PERFORMED TIMELY. AT APPROX. 45,000 MILES (BUT AFTER THE 5 YEAR WARRANTY HAD EXPIRED, (I AM A LOW MILEAGE DRIVER) I NOTICED THAT IT HAD CONSUMED TWO QUARTS OF OIL WITHIN AROUND 1500 MILES AFTER THE OIL CHANGE (RECOMMENDED TO PERFORM EVERY 5000 MILES). I HAD AN OIL CHANGE AND TOOK A ROAD TRIP SO THAT I PUT MORE
... THAN A 1000 MILES ON IT IN ABOUT 10 DAYS, AND WHEN I WAS ON A STEEP INCLINE THE CHECK OIL LIGHT CAME ON. MY MECHANIC SAID IT WAS POSSIBLE THAT THE OIL HAD NOT BEEN FILLED PROPERLY AFTER THE CHANGE AND TOPPED IT OFF. IT WAS LOW AGAIN WHEN I HAD IT CHANGED AT THE 51,000 MARK; AFTER ABOUT 1,500 MILES IT NEEDED TWO QUARTS OF OIL WHICH WAS ADDED. AFTER ANOTHER 1,500 OR SO MILES IT NEEDED ANOTHER TWO QUARTS OF OIL, WHICH I ADDED. I CONTACTED TOYOTA, AND WITHOUT RECITING THE INITIAL RUNAROUND, THEY SET UP AN OIL CONSUMPTION TEST AFTER CONFIRMING IT WAS NOT LEAKING OIL. THE OIL CONSUMPTION TEST IS NOT COMPLETED - IT MAY NOT BE A TRUE REFLECTION OF OIL USAGE AS IT SEEMS TO BE WORSE WHEN DRIVEN A LONG DISTANCE AT ONE TIME WHICH WILL PROBABLY NOT HAPPEN DURING THIS 1,000 MILE CYCLE. I THEN GOT A NOTICE IN THE MAIL THAT THEY HAD A PROGRAM TO REIMBURSE OWNERS FOR THE PARTS (NOT THE LABOR) IF THEY BELIEVED THE VEHICLE MET CERTAIN (UNSPECIFIED) CRITERIA AFTER THE OWNERS HAD THE REPAIRS DONE FOR THE DEFECT WHICH, APPARENTLY, THEY ALREADY KNOW SPECIFICALLY EXISTS AND HOW TO FIX IT. THE NOTICE SAID THEY ARE MAKING AS MANY REPLACEMENT PARTS AS POSSIBLE BEFORE ENCOURAGING US TO GET OUR VEHICLES REPAIRED. MY NUMBERS ARE NOT EXACT BUT THE INFORMATION IS GENERALLY ACCURATE. PLEASE INVESTIGATE THIS AND HAVE A RECALL ISSUED. THANK YOU *TRRead more
Incident date: Feb 27, 2015
THE 1ST THING I NOTICED AFTER STARTING MY CAR AFTER WORK WAS THE HEATER WAS BLOWING COLD AIR, EVEN AFTER 4 MILES ON THE ROAD (2 LANE ROAD - 40 MPG). ABOUT 4 MILES FURTHER ON (FREEWAY - 60+ MPH), I NOTICED A THIN GREY CLOUD BEHIND ME, BUT THE EVENING MISTS WERE EVIDENT, SO I WASN'T SURE AT FIRST IF IT WAS COMING FROM MY CAR. I CHECKED THE TEMPERATURE GAUGE WHICH SHOWED FLAT COLD - UNUSUAL! I CHECKE
... D MY REARVIEW MIRROR AGAIN, MAYBE 200 YDS LATER, AND THERE WAS A PALER GREY CLOUD FOLLOWING ME. I CHECKED THE INSTRUMENT PANEL AGAIN AND THERE WERE NO WARNING LIGHTS SHOWING. ABOUT 200-500 YARDS FARTHER, THE VSC LIGHT CAME ON, THE TRACTION CONTROL LIGHT CAME ON AND ANOTHER LIGHT THAT IS NOT SHOWN IN THE OWNER'S MANUAL STARTED BLINKING: THE SYMBOL WAS A CAR WITH A RECYCLE ARROW INSIDE THE BODY. I TOOK IT TO MEAN THAT THE CONTROLS WERE ACKNOWLEDGING THE HEATER WASN'T WORKING (THE SYMBOL IS THE SAME AS "AIR INTAKE SELECTOR" ON THE HEATER/AIR CONDITIONER CONTROLS). I FELT THAT I STILL HAD GOOD CONTROL OVER THE STEERING; IT WAS A CLEAR EVENING AND THE ROAD WAS DRY, SO I FELT I COULD GET HOME SAFELY (2 MILES). THE CAR WAS RUNNING QUITE ROUGH WHEN I GOT HOME AND THERE WAS WHAT SEEMED TO BE STEAM COMING FROM THE FRONT QUADRANT ON THE PASSENGER SIDE. THE DEALER SAYS THE WATER PUMP FAILED, CAUSING THE ENGINE TO OVERHEAT, SO NOW THE ENGINE NEEDS TO BE REPLACED ($6800). WHY DID THE WARNING LIGHTS AND TEMPERATURE GAUGE NOT LET ME KNOW THE ENGINE WAS OVERHEATING????? OR WHY DID THE WATER PUMP SUDDENLY FAIL?? NO WARNING LIGHTS TO INDICATE FAILURE OF A CRITICAL PART!!!!!??!. (CAR HAS BEEN REGULARLY MAINTAINED, ALL RECOMMENDED SERVICE PERFORMED BY CERTIFIED MECHANICS). NO SIGN THAT THE WATER PUMP WAS LEAKING PRIOR TO THIS INCIDENT. *TRRead more
Incident date: Feb 27, 2015
THE 1ST THING I NOTICED AFTER STARTING MY CAR AFTER WORK WAS THE HEATER WAS BLOWING COLD AIR, EVEN AFTER 4 MILES ON THE ROAD (2 LANE ROAD - 40 MPG). ABOUT 4 MILES FURTHER ON (FREEWAY - 60+ MPH), I NOTICED A THIN GREY CLOUD BEHIND ME, BUT THE EVENING MISTS WERE EVIDENT, SO I WASN'T SURE AT FIRST IF IT WAS COMING FROM MY CAR. I CHECKED THE TEMPERATURE GAUGE WHICH SHOWED FLAT COLD - UNUSUAL! I CHECKE
... D MY REARVIEW MIRROR AGAIN, MAYBE 200 YDS LATER, AND THERE WAS A PALER GREY CLOUD FOLLOWING ME. I CHECKED THE INSTRUMENT PANEL AGAIN AND THERE WERE NO WARNING LIGHTS SHOWING. ABOUT 200-500 YARDS FARTHER, THE VSC LIGHT CAME ON, THE TRACTION CONTROL LIGHT CAME ON AND ANOTHER LIGHT THAT IS NOT SHOWN IN THE OWNER'S MANUAL STARTED BLINKING: THE SYMBOL WAS A CAR WITH A RECYCLE ARROW INSIDE THE BODY. I TOOK IT TO MEAN THAT THE CONTROLS WERE ACKNOWLEDGING THE HEATER WASN'T WORKING (THE SYMBOL IS THE SAME AS "AIR INTAKE SELECTOR" ON THE HEATER/AIR CONDITIONER CONTROLS). I FELT THAT I STILL HAD GOOD CONTROL OVER THE STEERING; IT WAS A CLEAR EVENING AND THE ROAD WAS DRY, SO I FELT I COULD GET HOME SAFELY (2 MILES). THE CAR WAS RUNNING QUITE ROUGH WHEN I GOT HOME AND THERE WAS WHAT SEEMED TO BE STEAM COMING FROM THE FRONT QUADRANT ON THE PASSENGER SIDE. THE DEALER SAYS THE WATER PUMP FAILED, CAUSING THE ENGINE TO OVERHEAT, SO NOW THE ENGINE NEEDS TO BE REPLACED ($6800). WHY DID THE WARNING LIGHTS AND TEMPERATURE GAUGE NOT LET ME KNOW THE ENGINE WAS OVERHEATING????? OR WHY DID THE WATER PUMP SUDDENLY FAIL?? NO WARNING LIGHTS TO INDICATE FAILURE OF A CRITICAL PART!!!!!??!. (CAR HAS BEEN REGULARLY MAINTAINED, ALL RECOMMENDED SERVICE PERFORMED BY CERTIFIED MECHANICS). NO SIGN THAT THE WATER PUMP WAS LEAKING PRIOR TO THIS INCIDENT. *TRRead more
Incident date: Mar 1, 2011
MY 2006 SCION TC REAR TRUNK HANDLE BROKE OFF. IT IS A COMMON PROBLEM. I HAD TAPE HOLDING IT ON FOR A YEAR OR SO, AND GLUED IT MYSELF. I DID NOT RECEIVE ANY RECALL NOTICE OTHERWISE I WOULD HAVE FIXED IT. IT IS NOT JUST THE HANDLE TO GET IN TO THE TRUNK. THIS IS A 18 INCH BY 6 INCH PIECE OF MY CAR HANGING BY A WIRE. I JUST CALLED SCION AND THEY SAID THAT IS WAS NOT A RECALL BUT A WARRANTY EXTEN
... SION THAT EXPIRED 7 YEARS FROM THE DATE OF CAR BEING SOLD OR MARCH 2014. HOPEFULLY IT STAYS ON AND DOESN'T FLY OFF ON THE FREEWAY AND CAUSE AN ACCIDENT, BECAUSE THEN WILL NOT BE ABLE TO HAVE ACCESS TO MY SPARE TIRE OR GET INTO MY TRUNK. THIS SHOULD BE A RECALL WITH NO EXPIRATION DATE. *TRRead more
Incident date: Oct 22, 2014
PURCHASE AN EXEDY STAGE 2 CLUTCH WITH LIGHT FLYWHEEL PART# 15953FW FOR A 2013 SCION FRS. ISSUE IS IT LOCK OUT OF GEAR IN FIRST AND REVERSE GEAR. YOU HAVE TO USED FORCE TO GET IT OUT OF 1ST AND REVERSE GEAR. ALSO HARD TO GET IT INTO 1ST AND REVERSE GEAR. THIS IS A PROBLEM WITH THIS CLUTCH FOR THIS VEHICLE AS MANY HAVE REPORTED THIS SIMILAR ISSUE IN FT86CLUB FORUM. THIS LOCKING AND HARD TO GET IN
... TO GEAR MAKES IT DANGEROUS TO DRIVE THE CAR WHEN YOUR IN TRAFFIC OR ON THE ROAD. IT OCCURS EVERY TIME I DRIVE MY CAR REGARDLESS IN THE CITY OR FREEWAY. NOTHING WAS DONE AS I HAVE CONTACT THE MANUFACTURE FOR A REPLACEMENT PART# 19599. THEY WANTED ME TO SEND THE OLD ONE TO THEM FOR INSPECTION WHILE I HAVE NO REPLACEMENT TO PUT IN MY CAR SO I CAN'T DRIVE MY CAR. THIS IS REALLY A DEFECTED PART AND SHOULD BE RECALLED AS MANY ARE HAVING THE SAME ISSUE. *TRRead more
Incident date: Dec 17, 2014
EXCESSIVE OIL CONSUMPTION AFTER 1000. MILES OIL CONSUMPTION TEST AT CALDWELL TOYOTA DEALER. 2 1/2/ QUARTS DOWN. THEN WE WERE GIVEN A WARRANTY ENHANCEMENT NOTIFICATION FORM TO TAKE TO THE DEALER. THE DEALER SAID COME BACK AND WE WILL DO ANOTHER OIL CONSUMPTION TEST IN 1000 MILES. THIS HAS BEEN GOING ON SINCE SUMMER OF 2014. I HOPE THE CAR DOESN'T BURN UP. PLEASE ISSUE RECALL. THEY ARE GETTING
... AWAY WITH NOT FIXING THE PROBLEM THE FIRST TIME. THE NOTICE SAID ONCE THERE ARE ENOUGH PARTS THEN THEY WILL SEND OUT NOTICES TO FIX THE CARS. OK NOW!!! *TRRead more
Incident date: Jan 1, 2011
MY CAR CONSUMES ABOUT TWO QUARTS OF OIL PER 1000 MILES. MECHANICS HAVE TOLD ME THAT IT DOESN'T APPEAR TO BE LEAKING, IT COULD BE BEING BURNED THOUGH. I KEEP MY CAR RUNNING WITH FREQUENT OIL CHANGES AND GO THROUGH A GOOD AMOUNT OF OIL EVERY MONTH IN BETWEEN. MANY OTHER TC DRIVERS HAVE TOLD ME THEY HAVE THIS SAME ISSUE ALSO. *TR
Incident date: Feb 1, 2010
OUT OF NO WHERE; NO TREES, NO TRUCKS IN FRONT OF ME OR ANY OTHER VEHICLES, ON A CLEAR DAY, MY WINDSHIELD MADE A LOUD POP NOISE AND IT CRACKED FROM THE TOP PASSENGER SIDE EDGE TO THE CENTER OF THE WINDSHIELD. IT SLOWLY CREEPED ACROSS TO THE MID-LINE OF VISIBILITY ON THE DRIVER SIDE OVER THE NEXT 24 HRS. -- I WAS SURPRISED TO LEARN THIS IS A COMMON ISSUE WITH THIS YEAR AND MODEL! *JS
Incident date: Feb 14, 2015
VEHICLE'S REAR WHEEL SPEED SENSOR CONNECTORS GET CORRODED BY ROAD SALT, RESULTING IN FAILURE OF CAR'S COMPUTER TO REGISTER SPEED OF REAR WHEELS. THEREFORE, THE ANTI-LOCK BRAKING SYSTEM AND VEHICLE STABILITY CONTROL MAY NOT FUNCTION CORRECTLY IN SNOWY CONDITIONS. TOYOTA RELEASED A TECHNICAL SERVICE BULLETIN REGARDING THIS ISSUE AND CORRECTED THE DESIGN FLAW ON LATER SCION XB MODELS. (S-SB-004
... 0-09 JULY 6, 2009). *TRRead more
Incident date: Feb 14, 2015
VEHICLE'S REAR WHEEL SPEED SENSOR CONNECTORS GET CORRODED BY ROAD SALT, RESULTING IN FAILURE OF CAR'S COMPUTER TO REGISTER SPEED OF REAR WHEELS. THEREFORE, THE ANTI-LOCK BRAKING SYSTEM AND VEHICLE STABILITY CONTROL MAY NOT FUNCTION CORRECTLY IN SNOWY CONDITIONS. TOYOTA RELEASED A TECHNICAL SERVICE BULLETIN REGARDING THIS ISSUE AND CORRECTED THE DESIGN FLAW ON LATER SCION XB MODELS. (S-SB-004
... 0-09 JULY 6, 2009). *TRRead more
Incident date: Dec 25, 2014
1. INCIDENT THE DRIVER WAS DRIVING THE 2008 SCION XB ALONE ON EAST-BOUND I-80, APPROACHING CARQUINEZ BRIDGE, VALLEJO, WHEN THE VEHICLE STOPPED WORKING. THE DRIVING SPEED WAS ABOUT 70 MPH. TIME OF THE INCIDENT WAS AROUND 12:45 A.M. ON DECEMBER 25, 2014. HE WAS DRIVING ON THE 1ST LANE, AND TO THE BEST OF HIS KNOWLEDGE, THERE WAS ONLY ONE COMPACT CAR PASSING NEARBY, WHEN THE CAR STOPPED ALL OF A
... SUDDEN . HE TRIED TO REACH OUT FOR A TOW TRUCK WITHOUT SUCCESS, BUT LATER ON HE REMEMBERED HE WAS AN ASSOCIATE MEMBER OF A CLASSIC MEMBERSHIP CARD REGISTERED IN THE NAME OF HIS MOTHER. BUT HE DID NOT HAVE THE CARD ON HIM AT THAT TIME, BUT GAVE HIS NAME TO AAA TO PROVE HE IS AN ASSOCIATE MEMBER. FINALLY, THE AAA TOW TRUCK ARRIVED ON THE SCENE AROUND 1:45 A.M. HE TOWED IT TO HOME, AND DAYS LATER HAD IT TOWED TO A MECHANIC SHOP, EAST BAY AUTO LOCATED ON NORTH TEXAS STREET. THE MECHANIC DIAGNOSED THE PROBLEM AND SAID THE ENGINE GOT BROKEN AND THE CAR NEEDED REPLACEMENT OF THE ENGINE. 2. SCION SIDE ON FEB. 10, 2015, THE OWNER OF THE VEHICLE RECEIVED A LETTER OF WARRANTY ENHANCEMENT NOTIFICATION FROM SCION. THE OWNER DID NOT TAKE AN INITIATIVE TO CALL SCION BEFORE RECEIVING THIS NOTIFICATION. THE NEXT DAY, THE VEHICLE OWNER CALLED SCION AND FILED A CLAIM FOR ENGINE FAILURE DUE TO EXCESSIVE ENGINE OIL CONSUMPTION. CASE #[XXX]. THE CUSTOMER SERVICE REP AT SCION ARRANGED FOR TOYOTA DEALERSHIP IN VACAVILLE TO INSPECT AND DIAGNOSE SCION XB TO SEE IF THE ENGINE FAILURE WAS DUE TO EXCESSIVE ENGINE OIL CONSUMPTION. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Jul 16, 2014
AFTER ENGINE WORMS UP, LET THE ENGINE IDLE AND STAYS AT 600 RPM FOR A FEW SECONDS, JUMP TO 1100 RPM THEN DOWN TO 600 AND 400, ENGINE SHAKES UP LIKE IS GOING TO STALL AND CHECK ENGINE LIGHT AND VSC LIGHT COME ON. DEALER TOLD ME IS A CAMSHAFT GEAR DEFECT THAT WILL NOT CHANGE THE ANGLE FOR THE VARIABLE VALVE TIMING(VVT). OTHER PARTS NEEDED TO BE CHANGE ARE OIL CONTROL VALVE AND CAMSHAFT VVT SENSOR.
... TOYOTA MUST ISSUE A RECALL FOR THESE, MORE THAN 250 CASES WERE REPORTS ON FT86CLUB.COM. SAME EXACT PROBLEM IS SHOWN ON THE SUBARU BRZ BECAUSE IS THE EXACT SAME CAR. *TRRead more
Incident date: Jan 26, 2015
TL* THE CONTACT OWNS A 2008 TOYOTA SCION XD. THE CONTACT STATED THAT WHEN THE VEHICLE WAS STARTED, THE ABS WARNING LIGHT ILLUMINATED. THE FAILURE RECURRED ON SEVERAL OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 55,000.
Incident date: Feb 6, 2015
AFTER SEVERAL WEEKS OF SMELLING BURNT OIL IN THE CABIN, I DISCOVERED A SERIOUS OIL LEAK ON THE ENGINE. THE ENGINE HAS A BLOCK OFF PLATE ON THE RIGHT REAR CAMSHAFT AREA. IT IS A STAMPED STEEL PLATE HELD ON WITH THREE BOLTS AND SEALED WITH RTV. THE OIL WAS LEAKING AROUND THE BOTTOM BOLT AND DRIPPING ONTO THE EXHAUST PIPE. SCION DEALER WAS CONTACTED AND THEY TOLD ME THAT ALL THEY COULD DO WAS RE-
... APPLY THE SEALANT AND HOPE FOR THE BEST. THEY ALSO COMMENTED THAT IT WOULD FAIL AGAIN IN THE SAME PLACE BECAUSE OF THE DESIGN. I ORDERED AN AFTERMARKET COVER PLATE THAT INCORPORATES AN O RING INTO THE SEAL. THIS PLATE IS GUARANTEED NOT TO LEAK IF INSTALLED ACCORDING TO THE INSTRUCTIONS. WEB FORUMS INDICATE THAT THIS IS A VERY COMMON PROBLEM WITH MANUAL TRANSMISSION EQUIPPED FR-S. THE AUTOMATIC TRANSMISSION VERSION HAS A PUMP IN PLACE OF THE BLOCK OFF PLATE. THIS IS A POTENTIAL FIRE HAZARD AND OWNERS SHOULD NOT HAVE TO BUY AFTERMARKET PARTS TO CORRECT THE PROBLEM. SCION/TOYOTA (SUBARU) SHOULD DESIGN A PLATE THAT DOES NOT LEAK ONTO THE HOT EXHAUST PIPE. *JSRead more
Incident date: Feb 1, 2015
I HAD BEEN HEARING CLUNKING NOISE FROM RIGHT FRONT WHEEL FOR A FEW WEEKS, THAT SEEMED TO BE GETTING LOUDER OVER TIME. MOST PROMINENT DURING BRAKING OR HITTING POTHOLES. FATHER LOOKED AT WHEEL WHILE I BACKED OUT OF DRIVEWAY AND NOTICED WHEEL SHIFTING FORWARD/BACKWARD WITHIN THE WHEEL WELL ABOUT AN INCH WHEN STARTING AND STOPPING. TOOK VEHICLE TO LOCAL TIRE SHOP AND WAS TOLD BOLD ATTACHING LOWER CO
... NTROL ARM TO BODY HAD CORRODED AND BROKEN OFF. SUGGESTED I TAKE CAR TO DEALER FOR REPAIR, AND MENTIONED THERE WAS A TSB ISSUED FOR THIS PROBLEM THAT EXTENDED THE WARRANTY TO 7 YEARS/100,000 MILES. DEALER REPAIRED VEHICLE AT MY COST ($422), SINCE THE WARRANTY HAS EXPIRED (MILEAGE). I BELIEVE THIS PART SHOULD LAST THE LIFE OF THE VEHICLE. LUCKILY MY FATHER NOTICED THE WHEEL MOVEMENT OR THE WHEEL MAY HAVE COME OFF AT HIGHWAY SPEED. *JSRead more
Incident date: Feb 4, 2015
SALT AND SNOW CAUSES ERROR CODES C0210, REAR SPEED SENSOR RH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS USED ON ROADWAYS. SALT AND SNOW CAUSES ERROR CODES C0215, REAR SPEED SENSOR LH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS
... USED ON ROADWAYS. THIS IS A KNOW PROBLEM WITH 2008-2009 SCION XB, TOYOTA TSB S-SB-0040-09, JULY 6,2009 **THE CONNECTORS FOR THESE SENSORS ARE EXPOSED TO THE ENVIRONMENT, CAUSING NON DEPLOYMENT OF SAFETY DEVICES LEADING UP TO, AND DURING A CRASH** *TRRead more
Incident date: Feb 4, 2015
SALT AND SNOW CAUSES ERROR CODES C0210, REAR SPEED SENSOR RH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS USED ON ROADWAYS. SALT AND SNOW CAUSES ERROR CODES C0215, REAR SPEED SENSOR LH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS
... USED ON ROADWAYS. THIS IS A KNOW PROBLEM WITH 2008-2009 SCION XB, TOYOTA TSB S-SB-0040-09, JULY 6,2009 **THE CONNECTORS FOR THESE SENSORS ARE EXPOSED TO THE ENVIRONMENT, CAUSING NON DEPLOYMENT OF SAFETY DEVICES LEADING UP TO, AND DURING A CRASH** *TRRead more
Incident date: Feb 4, 2015
SALT AND SNOW CAUSES ERROR CODES C0210, REAR SPEED SENSOR RH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS USED ON ROADWAYS. SALT AND SNOW CAUSES ERROR CODES C0215, REAR SPEED SENSOR LH CIRCUIT TO MALFUNCTION AND SHUTS DOWN THE ABS, TRACTION CONTROL, AND AIR BAG DEPLOYMENT. ALL SAFETY DEVICES ARE OFF WHEN SALT IS
... USED ON ROADWAYS. THIS IS A KNOW PROBLEM WITH 2008-2009 SCION XB, TOYOTA TSB S-SB-0040-09, JULY 6,2009 **THE CONNECTORS FOR THESE SENSORS ARE EXPOSED TO THE ENVIRONMENT, CAUSING NON DEPLOYMENT OF SAFETY DEVICES LEADING UP TO, AND DURING A CRASH** *TRRead more
Incident date: Jan 31, 2015
TL* THE CONTACT OWNS A 2005 SCION XB. THE CONTACT STATED THAT THE REAR HATCHBACK HANDLE FRACTURED CAUSING THE OTHER FOUR DOOR LOCKS TO BECOME DISABLED. IN ADDITION, THERE WERE HOLES WHERE THE HATCHBACK HANDLE WAS FRACTURED AND THERE WAS A STRONG FUEL ODOR. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 9
... 4,120.Read more
Incident date: Feb 1, 2015
2006 SCION TC -BATTERY LIGHT ON -ENGINE TEMPERATURE INDICATOR NO WORKING -WHINING NOISE COMING FROM ENGINE TRY TO JUMPSTART MAKES THIS BURNING SMELL AND WONT START STARTED SEEING SMOKES FROM JUMPER CABLES SO TURN EVERYTHING OFF NOW IT'S TOTALLY DEAD. *TR
1 injured
Incident date: Feb 1, 2015
2006 SCION TC -BATTERY LIGHT ON -ENGINE TEMPERATURE INDICATOR NO WORKING -WHINING NOISE COMING FROM ENGINE TRY TO JUMPSTART MAKES THIS BURNING SMELL AND WONT START STARTED SEEING SMOKES FROM JUMPER CABLES SO TURN EVERYTHING OFF NOW IT'S TOTALLY DEAD. *TR
1 injured
Incident date: Jan 31, 2015
TL* THE CONTACT OWNS A 2005 SCION XB. THE CONTACT STATED THAT THE REAR HATCHBACK HANDLE FRACTURED CAUSING THE OTHER FOUR DOOR LOCKS TO BECOME DISABLED. IN ADDITION, THERE WERE HOLES WHERE THE HATCHBACK HANDLE WAS FRACTURED AND THERE WAS A STRONG FUEL ODOR. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 9
... 4,120.Read more
Incident date: Feb 27, 2009
THE ELECTRONIC DOOR LOCKS ON THE CAR WILL OFTEN OPEN ONLY HALFWAY, PREVENTING THE OCCUPANT FROM EXITING THE VEHICLE. BOTH FRONT DOORS ARE AFFECTED, BUT THE DRIVERS DOOR IS AFFECTED MORE OFTEN. IT IS DIFFICULT IF NOT IMPOSSIBLE TO UNLOCK THE DOOR MANUALLY WHEN THIS HAPPENS. REPEATING THE UNLOCK PROCESS SEVERAL TIMES IS THE ONLY WAY TO GET THE LOCK TO OPEN. THIS WAS TAKEN TO THE DEALER FOR REPAIR, B
... UT THEY TOLD US THAT THE LOCKS WERE WORKING FINE WHEN THEY HAD IT AND THAT THEY COULD NOT WORK ON IT UNLESS THEY SAW THE PROBLEM ACTUALLY OCCURRING. I KEEP A WINDOW HAMMER IN THE CAR NOW. *TRRead more
Incident date: Jan 20, 2015
TRAVELING NORTH ON I-75 IN INDEPENDENCE TWP, MI SOUTH OF ORTONVILLE RD AT 10:55AM IN A SNOW STORM, DRIVER USED THE PASSING LANE TO OVERTAKE A SLOW MOVING VEHICLE IN THE CENTER LANE. ACCELERATING TO 70MPH, DRIVER BEGAN TO MERGE BACK INTO CENTER LANE BUT ENCOUNTERED A HEAVY BUILDUP OF SLUSH BETWEEN LANES AND BEGAN TO LOOSE TRACTION. VEHICLE STARTED TO VEER TO THE RIGHT. DRIVER REMOVED FOOT FROM THE
... ACCELERATOR AND TURNED WHEEL SLIGHTLY TO THE LEFT TO CORRECT THE SKID BUT THE ELECTRONIC STABILITY CONTROL ENGAGED AND THE VEHICLE IMMEDIATELY ENTERED INTO A RAPID 360 DEGREE SPIN TO THE RIGHT. NO OTHER VEHICLE WAS STRUCK. DRIVER RECOVERED FROM THE SPIN MOMENTARILY AND CAR WAS FACING NORTHBOUND BETWEEN THE CENTER AND RIGHT LANES BUT STILL VEERING TO THE RIGHT. THE FRONT WHEELS CONTACTED DRY PAVEMENT WHILE THE REAR WHEELS WERE ON WET PAVEMENT CAUSING THE VEHICLE TO MAKE A SHARP RIGHT TURN HEAD ON INTO THE GUARD RAIL AT 60 MPH. THE GUARD RAIL GAVE WAY AND THE FRONT END OF THE VEHICLE SUSTAINED HEAVY DAMAGE. HOWEVER THE VEHICLE REBOUNDED AND REMAINED IN THE ROAD WAY, SLIDING SIDEWAYS AND EVENTUALLY SPINNING ANOTHER 270 DEGREES AFTER AGAIN STRIKING THE GUARD RAIL. THE INITIAL HIGH SPEED IMPACT WITH GUARD RAIL APPEARS TO HAVE IGNITED THE SODIUM AZIDE AS EVIDENCED BY A GUNPOWDER LIKE ODOR IN THE VEHICLE HOWEVER NO AIRBAGS DEPLOYED. ADDITIONALLY, THE SEATBELT WHILE PROPERLY FASTENED DID NOT RETRACT AND RESTRAIN THE DRIVER. THE SEATBELT EXTENDED ALL THE WAY OUT AND REMAINED IN THIS POSITION. THIS MADE IT DIFFICULT TO CONTROL THE VEHICLE AND CAUSED THE DRIVER TO IMPACT THE STEERING WHEEL WHEN THE GUARDRAIL WAS STRUCK. THIS RESULTED IN INJURY TO THE RIGHT SIDE OF THE RIB CAGE, WITH POSSIBLE HAIRLINE FRACTURES TO THE RIBS, TORN MUSCLES, AND BRUISING OF THE LIVER. DRIVER'S HEAD ALSO IMPACTED THE CEILING. UPON SECOND GUARDRAIL IMPACT, DRIVER'S LEFT ARM IMPACTED THE STEERING WHEEL. *TRRead more
Crash
1 injured
Incident date: Jan 20, 2015
TRAVELING NORTH ON I-75 IN INDEPENDENCE TWP, MI SOUTH OF ORTONVILLE RD AT 10:55AM IN A SNOW STORM, DRIVER USED THE PASSING LANE TO OVERTAKE A SLOW MOVING VEHICLE IN THE CENTER LANE. ACCELERATING TO 70MPH, DRIVER BEGAN TO MERGE BACK INTO CENTER LANE BUT ENCOUNTERED A HEAVY BUILDUP OF SLUSH BETWEEN LANES AND BEGAN TO LOOSE TRACTION. VEHICLE STARTED TO VEER TO THE RIGHT. DRIVER REMOVED FOOT FROM THE
... ACCELERATOR AND TURNED WHEEL SLIGHTLY TO THE LEFT TO CORRECT THE SKID BUT THE ELECTRONIC STABILITY CONTROL ENGAGED AND THE VEHICLE IMMEDIATELY ENTERED INTO A RAPID 360 DEGREE SPIN TO THE RIGHT. NO OTHER VEHICLE WAS STRUCK. DRIVER RECOVERED FROM THE SPIN MOMENTARILY AND CAR WAS FACING NORTHBOUND BETWEEN THE CENTER AND RIGHT LANES BUT STILL VEERING TO THE RIGHT. THE FRONT WHEELS CONTACTED DRY PAVEMENT WHILE THE REAR WHEELS WERE ON WET PAVEMENT CAUSING THE VEHICLE TO MAKE A SHARP RIGHT TURN HEAD ON INTO THE GUARD RAIL AT 60 MPH. THE GUARD RAIL GAVE WAY AND THE FRONT END OF THE VEHICLE SUSTAINED HEAVY DAMAGE. HOWEVER THE VEHICLE REBOUNDED AND REMAINED IN THE ROAD WAY, SLIDING SIDEWAYS AND EVENTUALLY SPINNING ANOTHER 270 DEGREES AFTER AGAIN STRIKING THE GUARD RAIL. THE INITIAL HIGH SPEED IMPACT WITH GUARD RAIL APPEARS TO HAVE IGNITED THE SODIUM AZIDE AS EVIDENCED BY A GUNPOWDER LIKE ODOR IN THE VEHICLE HOWEVER NO AIRBAGS DEPLOYED. ADDITIONALLY, THE SEATBELT WHILE PROPERLY FASTENED DID NOT RETRACT AND RESTRAIN THE DRIVER. THE SEATBELT EXTENDED ALL THE WAY OUT AND REMAINED IN THIS POSITION. THIS MADE IT DIFFICULT TO CONTROL THE VEHICLE AND CAUSED THE DRIVER TO IMPACT THE STEERING WHEEL WHEN THE GUARDRAIL WAS STRUCK. THIS RESULTED IN INJURY TO THE RIGHT SIDE OF THE RIB CAGE, WITH POSSIBLE HAIRLINE FRACTURES TO THE RIBS, TORN MUSCLES, AND BRUISING OF THE LIVER. DRIVER'S HEAD ALSO IMPACTED THE CEILING. UPON SECOND GUARDRAIL IMPACT, DRIVER'S LEFT ARM IMPACTED THE STEERING WHEEL. *TRRead more
Crash
1 injured
Incident date: Jan 20, 2015
TRAVELING NORTH ON I-75 IN INDEPENDENCE TWP, MI SOUTH OF ORTONVILLE RD AT 10:55AM IN A SNOW STORM, DRIVER USED THE PASSING LANE TO OVERTAKE A SLOW MOVING VEHICLE IN THE CENTER LANE. ACCELERATING TO 70MPH, DRIVER BEGAN TO MERGE BACK INTO CENTER LANE BUT ENCOUNTERED A HEAVY BUILDUP OF SLUSH BETWEEN LANES AND BEGAN TO LOOSE TRACTION. VEHICLE STARTED TO VEER TO THE RIGHT. DRIVER REMOVED FOOT FROM THE
... ACCELERATOR AND TURNED WHEEL SLIGHTLY TO THE LEFT TO CORRECT THE SKID BUT THE ELECTRONIC STABILITY CONTROL ENGAGED AND THE VEHICLE IMMEDIATELY ENTERED INTO A RAPID 360 DEGREE SPIN TO THE RIGHT. NO OTHER VEHICLE WAS STRUCK. DRIVER RECOVERED FROM THE SPIN MOMENTARILY AND CAR WAS FACING NORTHBOUND BETWEEN THE CENTER AND RIGHT LANES BUT STILL VEERING TO THE RIGHT. THE FRONT WHEELS CONTACTED DRY PAVEMENT WHILE THE REAR WHEELS WERE ON WET PAVEMENT CAUSING THE VEHICLE TO MAKE A SHARP RIGHT TURN HEAD ON INTO THE GUARD RAIL AT 60 MPH. THE GUARD RAIL GAVE WAY AND THE FRONT END OF THE VEHICLE SUSTAINED HEAVY DAMAGE. HOWEVER THE VEHICLE REBOUNDED AND REMAINED IN THE ROAD WAY, SLIDING SIDEWAYS AND EVENTUALLY SPINNING ANOTHER 270 DEGREES AFTER AGAIN STRIKING THE GUARD RAIL. THE INITIAL HIGH SPEED IMPACT WITH GUARD RAIL APPEARS TO HAVE IGNITED THE SODIUM AZIDE AS EVIDENCED BY A GUNPOWDER LIKE ODOR IN THE VEHICLE HOWEVER NO AIRBAGS DEPLOYED. ADDITIONALLY, THE SEATBELT WHILE PROPERLY FASTENED DID NOT RETRACT AND RESTRAIN THE DRIVER. THE SEATBELT EXTENDED ALL THE WAY OUT AND REMAINED IN THIS POSITION. THIS MADE IT DIFFICULT TO CONTROL THE VEHICLE AND CAUSED THE DRIVER TO IMPACT THE STEERING WHEEL WHEN THE GUARDRAIL WAS STRUCK. THIS RESULTED IN INJURY TO THE RIGHT SIDE OF THE RIB CAGE, WITH POSSIBLE HAIRLINE FRACTURES TO THE RIBS, TORN MUSCLES, AND BRUISING OF THE LIVER. DRIVER'S HEAD ALSO IMPACTED THE CEILING. UPON SECOND GUARDRAIL IMPACT, DRIVER'S LEFT ARM IMPACTED THE STEERING WHEEL. *TRRead more
Crash
1 injured
Incident date: Jan 26, 2015
I WAS DRIVING ABOUT 50 MPH AND I HEARD A VERY LOUD POPPING SOUND LIKE A GUNSHOT. I PULLED OVER AND SAW THAT MY SUNROOF GLASS HAD SHATTERED (SPONTANEOUSLY). *TR
Incident date: Jan 26, 2015
I WAS DRIVING ABOUT 50 MPH AND I HEARD A VERY LOUD POPPING SOUND LIKE A GUNSHOT. I PULLED OVER AND SAW THAT MY SUNROOF GLASS HAD SHATTERED (SPONTANEOUSLY). *TR
Incident date: Aug 9, 2014
I WAS ALONE, PREPARING TO GET ON THE TURNPIKE ACCESS ROAD WHEN A CAR/VAN HIT THE RIGHT FRONT PASSENGER SIDE OF MY CAR. DETAILS OF THE ACCIDENT WERE RECORDED MANY HOURS AFTER THE CRASH. I WAS NEVER ASKED TO PROVIDE DETAILS. MY CAR ROLLED OVER TWICE DOWN A STEEP-ANGLED BUT SHALLOW EMBANKMENT AND THEN RIGHTED ITSELF UPRIGHT. MY SEATBELT WAS FASTENED AND SNUGGED BUT AT NO TIME DID THE RETAINING FUN
... CTION ENGAGE.THE SEATBELT FUNCTIONED LIKE A BUNJI CORD. AND THE AIRBAGS (NEITHER FRONT AIRBAG) DEPLOYED UNTIL MANY MINUTES AFTER THE CRASH, AS I WAS SLIDING ACROSS THE FRONT SEAT AND CONSOLE AS I BEGAN TO EXIT THE PASSENGER SIDE. I WAS AND AM STILL INJURED, HAVE LOST MUCH USE OF MY LEFT WRIST AND HAND, SUFFERED A BLOW TO THE BACK OF MY HEAD WHICH TEMPORARILY LEFT ME DEAF. I STILL HAVE SEVERE CONTUSIONS OF THE LEFT AND RIGHT LEGS, AND ABDOMEN BOTH EXTERNALLY AND ON THE INSIDE OF THE ABDOMINAL WALL. *TRRead more
1 injured
Incident date: Aug 9, 2014
I WAS ALONE, PREPARING TO GET ON THE TURNPIKE ACCESS ROAD WHEN A CAR/VAN HIT THE RIGHT FRONT PASSENGER SIDE OF MY CAR. DETAILS OF THE ACCIDENT WERE RECORDED MANY HOURS AFTER THE CRASH. I WAS NEVER ASKED TO PROVIDE DETAILS. MY CAR ROLLED OVER TWICE DOWN A STEEP-ANGLED BUT SHALLOW EMBANKMENT AND THEN RIGHTED ITSELF UPRIGHT. MY SEATBELT WAS FASTENED AND SNUGGED BUT AT NO TIME DID THE RETAINING FUN
... CTION ENGAGE.THE SEATBELT FUNCTIONED LIKE A BUNJI CORD. AND THE AIRBAGS (NEITHER FRONT AIRBAG) DEPLOYED UNTIL MANY MINUTES AFTER THE CRASH, AS I WAS SLIDING ACROSS THE FRONT SEAT AND CONSOLE AS I BEGAN TO EXIT THE PASSENGER SIDE. I WAS AND AM STILL INJURED, HAVE LOST MUCH USE OF MY LEFT WRIST AND HAND, SUFFERED A BLOW TO THE BACK OF MY HEAD WHICH TEMPORARILY LEFT ME DEAF. I STILL HAVE SEVERE CONTUSIONS OF THE LEFT AND RIGHT LEGS, AND ABDOMEN BOTH EXTERNALLY AND ON THE INSIDE OF THE ABDOMINAL WALL. *TRRead more
1 injured
Incident date: Jan 1, 2015
ABS AND BRAKE LIGHTS INTERMITTENTLY COME AND STAY ON. MANUAL TRANSMISSION XD. ABS/BRAKE LIGHTS COME ON BOTH AT HIGHWAY AND CITY SPEEDS, STAY ON FOR HOURS, THEN GO OFF, THEN COME BACK ON FOR A FEW DAYS, THEN GO BACK OFF. SOMETIMES THE ABS/BRAKE LIGHTS COME ON WHEN I START THE CAR, THEN EVENTUALLY GO OFF, SOMETIMES THEY COME ON WHILE DRIVING AND GO OFF THE NEXT DAY OR SO. TEMPERATURES ARE COOL A
... ND WET (40 DEGREE F) OVER THE PAST FEW WEEKS. ABS DOES NOT ENGAGE WHILE DRIVING, BUT DOES NOT ENGAGE PROPERLY WHILE ABS/BRAKE LIGHTS ARE ON AND DURING BRAKING. WHEN ABS/BRAKE LIGHTS ARE OFF, ALL BRAKING IS NORMAL. BRAKES AND ASSEMBLIES ARE NOT WORN OUT, BRAKE FLUID LEVEL IS SPOT ON. *TRRead more
Incident date: Mar 20, 2014
THE BACK HATCH DOOR HANDLE LOOKS LIKE IT IS MELTED AND VERY STICKY. NEEDS TO BE REPLACED. ALSO WHEN I SHIFT INTO 3RD GEAR SOMETIMES I FEEL A LIGHT GRINDING. IT SEEMS TO ONLY HAPPEN WHEN MY CAR IS COLD AND DOES NOT HAPPEN AFTER MY CAR IS WARMED UP. I HOPE IT NOTHING WRONG WITH THE TRANSMISSION. I HAVE TAKEN IT TO A MECHANIC THEY SAID NOTHING IS WRONG, VERY STRANGE. *TR
Incident date: Mar 20, 2014
THE BACK HATCH DOOR HANDLE LOOKS LIKE IT IS MELTED AND VERY STICKY. NEEDS TO BE REPLACED. ALSO WHEN I SHIFT INTO 3RD GEAR SOMETIMES I FEEL A LIGHT GRINDING. IT SEEMS TO ONLY HAPPEN WHEN MY CAR IS COLD AND DOES NOT HAPPEN AFTER MY CAR IS WARMED UP. I HOPE IT NOTHING WRONG WITH THE TRANSMISSION. I HAVE TAKEN IT TO A MECHANIC THEY SAID NOTHING IS WRONG, VERY STRANGE. *TR
Incident date: Mar 20, 2014
THE BACK HATCH DOOR HANDLE LOOKS LIKE IT IS MELTED AND VERY STICKY. NEEDS TO BE REPLACED. ALSO WHEN I SHIFT INTO 3RD GEAR SOMETIMES I FEEL A LIGHT GRINDING. IT SEEMS TO ONLY HAPPEN WHEN MY CAR IS COLD AND DOES NOT HAPPEN AFTER MY CAR IS WARMED UP. I HOPE IT NOTHING WRONG WITH THE TRANSMISSION. I HAVE TAKEN IT TO A MECHANIC THEY SAID NOTHING IS WRONG, VERY STRANGE. *TR
Incident date: Dec 31, 2014
WHEN I TRIED TO ROLL THE PASSENGER WINDOW DOWN, A PLUME OF SMOKE CAME OUT OF THE MASTER CONTROL PANEL. AT FIRST, I THOUGHT I WAS IMAGINING IT, BUT THE BUTTON FROZE INTO PLACE. I TOOK MY SCION INTO A DEALERSHIP FOR 2 RECALL NOTICE REPAIRS (DRIVER'S SEAT RAILING AND INTAKE MANIFOLD ASSEMBLY) AND MENTIONED THE WINDOW CONTROL PANEL PROBLEM AND MY CONCERN AS TO WHETHER OR NOT THERE WAS A RISK OF A FI
... RE. THE SERVICE TECH SAID THAT MY CAR WAS NOT PART OF THE RECALL? I AM CONCERNED AS TO WHETHER OR NOT MY CAR IS GOING TO CATCH ON FIRE AND AM CURIOUS TO KNOW IF THIS HAS BEEN AN ONGOING PROBLEM WITH THE NEWER MODEL SCION XDS? *TRRead more
Incident date: Dec 31, 2014
WHEN I TRIED TO ROLL THE PASSENGER WINDOW DOWN, A PLUME OF SMOKE CAME OUT OF THE MASTER CONTROL PANEL. AT FIRST, I THOUGHT I WAS IMAGINING IT, BUT THE BUTTON FROZE INTO PLACE. I TOOK MY SCION INTO A DEALERSHIP FOR 2 RECALL NOTICE REPAIRS (DRIVER'S SEAT RAILING AND INTAKE MANIFOLD ASSEMBLY) AND MENTIONED THE WINDOW CONTROL PANEL PROBLEM AND MY CONCERN AS TO WHETHER OR NOT THERE WAS A RISK OF A FI
... RE. THE SERVICE TECH SAID THAT MY CAR WAS NOT PART OF THE RECALL? I AM CONCERNED AS TO WHETHER OR NOT MY CAR IS GOING TO CATCH ON FIRE AND AM CURIOUS TO KNOW IF THIS HAS BEEN AN ONGOING PROBLEM WITH THE NEWER MODEL SCION XDS? *TRRead more
Incident date: Nov 12, 2013
TO MUCH CONSUMPTION OF OIL. *TR
Incident date: Nov 12, 2013
TO MUCH CONSUMPTION OF OIL. *TR
Incident date: Nov 30, 2014
THE TEMPERATURE WAS ABOUT 50 DEGREES AND SUNNY I HAD JUST LEFT CHURCH SERVICES SO THE CAR HAD BEEN SITTING OUT IN THE PARKING LOT FOR ABOUT 4 HOURS. I WAS IN THE CAR DOING ABOUT 40 MPH AND I HEARD A POP-LIKE THAT OF A CHAMPAGNE BOTTLE- AND WHAT SOUNDED LIKE SAND ON THE FLOOR. I LOOKED AROUND TO MAKE SURE A BUG OR REPTILE HADN'T GOTTEN INTO MY CAR. I DIDN'T THINK ANYTHING ABOUT IT. THIS MORNING 12/
... 3/2014 TEMPERATURE AROUND 43 DEGREES AND NOTICED THAT MY GLASS WIND DEFLECTOR WHAT SHATTERED AROUND THE EDGES. I'VE NEVER HAD ANY ISSUES WITH THE CAR AND I LIVE IN A GATE COMMUNITY SO I DIDN'T THINK THAT IT WAS AN ACT OF VANDALISM. I SPENT 3 YEARS IN ALASKA AND I KNOW WHAT FROZEN GLASS COULD DO IF EXPOSED TO DIRECT EXTREME HEAT. THIS WAS NOT THE CASE. I AM LOOKING INTO GETTING IT REPLACED BUT JUDGING FROM THE FORUMS AND THIS SITE DOESN'T SEEM LIKE TOYOTA WILL COVER MY 2007 SCION TC WHICH I THINK IS A VERY DISHONORABLE THING TO DO. MANY TC OWNERS ARE HAVING A TIME WITH VEHICLES THAT HAVE INCURRED THIS ISSUE THAT THEY DIDN'T CAUSE AND COULDN'T PREVENT. *JSRead more
Incident date: Dec 28, 2014
TL* THE CONTACT OWNS A 2005 TOYOTA SCION TC. WHILE THE TRUNK WAS OPENED, IT FAILED TO REMAIN OPEN AND SLAMMED ONTO THE CONTACT'S BACK. THE CONTACT DID NOT REQUIRE MEDICAL ATTENTION. THE VEHICLE WAS DIAGNOSED WITH A HYDRAULIC LIFT FAILURE. THE SPECIFICS OF WHERE THE VEHICLE WAS DIAGNOSED WERE NOT AVAILABLE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VIN AND
... FAILURE MILEAGE WERE UNAVAILABLE. UPDATED 02/24/15*LJ UPDATED 9/12/2017*CNRead more
1 injured
Incident date: Dec 26, 2014
ELECTRONIC POWER STEERING FAILURE WHILE PARKED. WHEN I PARKED THE CAR MY STEERING WORKED. WHEN I STARTED MY CAR AND PRECEDED TO BACK UP, THE POWER STEERING LIGHT APPEARED AND IT WAS NEARLY IMPOSSIBLE TO TURN THE WHEEL. *TR
Incident date: Nov 3, 2014
TL* THE CONTACT OWNS A 2014 SCION XD. THE CONTACT STATED THAT WHILE PARKED, THE REAR OF THE VEHICLE CAUGHT FIRE. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE AND STATED THAT THERE WAS A WIRE SHORTAGE IN THE REAR PASSENGER SIDE LIGHT. A POLICE/FIRE REPORT WAS FILED AND THERE WERE NO INJURIES REPORTED. THE VEHICLE WAS DESTROYED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 999.
Fire
Incident date: Dec 19, 2014
WHILE CAR RUNNING ON THE LOCAL ROAD, APPROX. 40 MPH, REAR WINDOW FROM DRIVER SIDE ROLLED DOWN ITSELF AND A LOT OF SMOKE STARTED COMING OUT FROM POWER WINDOW MASTER SWITCH CONTROLS AND FROM DRIVER SIDE WINDOW, INSIDE. TWO OF FOUR SWITCHES FROM MASTER SWITCH CONTROL THEN MELTED AND PUSHED ALL THE WAY DOWN, SEEMS LIKE THE BOTTOM PART OF THOSE SWITCHES CAUGHT FIRES OR SOMETHING, HOWEVER, NO FIRE WAS V
... ISIBLE FROM THE EXTERIOR. WAS THEN PULLED TO THE BUSINESS PARKING LOT AND TURNED OFF THE ENGINE. THE SMOKE THEN SLOWLY STOPPED. CAR TOWED TO AND PARKED AT LOCAL TOYOTA/ SCION DEALER SIDE WAY, SERVICE CONSULTANT CHECKED MY VIN AND INFORMED THAT THERE WAS NO RECALL FOR THIS PARTICULAR VIN. (VISIBILITY: POWER WINDOW DEVICES AND CONTROLS RECALL DATE: 10/10/2012 DOES NOT INCLUDE THIS PARTICULAR VIN) WAS THEN CONTACTED SCION RECALL SAME DAY AND THEY STARTED A FIRE CASE FOR INVESTIGATION, 3 DAYS LATER CASE MANAGER LETTING ME KNOW THAT TO COMPLETE THEIR INVESTIGATION OF THE CAUSES COULD TAKE UP TO A MONTH? THEY WANTED TO HOLD MY CAR AT THE DEALER UNTIL INVESTIGATION IS COMPLETED, WITHOUT AN ESTIMATE OF COMPLETION DATE AND THEY OFFERED NO LOANER CAR OR RENTAL REIMBURSEMENT? WHY NHTSA CAMPAIGN NUMBER: 12V491000 -- AFFECTED -- TOYOTA SCION XD 2008-2009 -- THEN WHY THIS VIN WITH THE SAME DEFECTIVE WAS NOT PART OF THE RECALL? *TRRead more
Fire