Showing 2,690 complaints for PORSCHE
Incident date: Sep 21, 2013
I WAS DRIVING AT MILLER MOTORSPORTS IN TOOELE UTAH IN DRIVERS EDUCATION EVENT WHEN MY ENGINE TEMPERATURE GAUGE STARTED TO INCREASE FROM 180 DEGREES UP PAST 200 DEGREES. AS THE TEMPERATURE GAUGE WENT TO 250 DEGREES, A COOLANT FAILURE LIGHT CAME ON. I PULLED OFF THE TRACK AND SHUT DOWN THE CAR WITHIN 2 MINUTES OF THE FAILURE LIGHT AND I HAD TO BE TOWED OFF THE MILLER MOTORSPORTS TRACK. I HAD LOST A
... LL OF MY COOLANT FROM THE CAR. THE NEXT MORNING (SUNDAY) I TOOK A RENTAL CAR BACK TO MILLER MOTORSPORTS ALONG WITH 9 GALLONS OF DISTILLED WATER. I POURED 2 GALLONS OF DISTILLED WATER INTO THE CAR, AND THEN STARTED IT. ABOUT SEVEN MINUTES LATER, WATER STARTED SPURTING FROM AN ALUMINUM COOLANT LINE ATTACHMENT THAT HAD COME UNGLUED. THIS ALUMINUM ATTACHMENT WAS IN A PLACE ON THE TOP OF THE ENGINE THAT WAS READILY DETERMINABLE AS THE WATER WAS SHOOTING STRAIGHT UP FROM WHERE THE FITTING HAD COME UNGLUED AND SLIPPED OFF. I DO NOT CURRENTLY KNOW WHETHER I GOT THE CAR STOPPED IN TIME FOR THE ENGINE TO BE OK. I AM AFRAID TO DRIVE IT BEFORE I GET ALL OF THE ALUMINUM FITTINGS REGLUED OR WELDED. BECAUSE THIS HAPPENED ON THE TOP OF THE ENGINE, THE COOLANT DID NOT CREATE A SITUATION THAT WAS A SAFETY RISK TO ME, BUT IF IT HAD BEEN A DIFFERENT ALUMINUM COOLANT ATTACHMENT THAT LET LOOSE, I COULD HAVE CRASHED AT 115 MPH DUE TO COOLANT ON THE TIRES OR SOMEONE BEHIND ME COULD HAVE CRASHED. THE MILLER MOTORSPORT PERSONNEL SAID THEY NOTICED A PLUME OF STEAM AT THE END OF THE FRONT STRAIGHT. AT THE END OF THE FRONT STRAIGHT, I HAD SLOWED TO 115 MPH. I AM THE ORIGINAL PURCHASER OF THIS CAR AND DID NOT THINK I WAS AT RISK FOR THIS TYPE OF SAFETY ISSUE ON A CAR THAT IS NOT DRIVEN IN STOP AND GO TRAFFIC. IT ALSO ONLY HAS A LITTLE OVER 28,000 MILES. *LN UPDATED 1/8/2013 *JSRead more
Incident date: Sep 21, 2013
I WAS DRIVING AT MILLER MOTORSPORTS IN TOOELE UTAH IN DRIVERS EDUCATION EVENT WHEN MY ENGINE TEMPERATURE GAUGE STARTED TO INCREASE FROM 180 DEGREES UP PAST 200 DEGREES. AS THE TEMPERATURE GAUGE WENT TO 250 DEGREES, A COOLANT FAILURE LIGHT CAME ON. I PULLED OFF THE TRACK AND SHUT DOWN THE CAR WITHIN 2 MINUTES OF THE FAILURE LIGHT AND I HAD TO BE TOWED OFF THE MILLER MOTORSPORTS TRACK. I HAD LOST A
... LL OF MY COOLANT FROM THE CAR. THE NEXT MORNING (SUNDAY) I TOOK A RENTAL CAR BACK TO MILLER MOTORSPORTS ALONG WITH 9 GALLONS OF DISTILLED WATER. I POURED 2 GALLONS OF DISTILLED WATER INTO THE CAR, AND THEN STARTED IT. ABOUT SEVEN MINUTES LATER, WATER STARTED SPURTING FROM AN ALUMINUM COOLANT LINE ATTACHMENT THAT HAD COME UNGLUED. THIS ALUMINUM ATTACHMENT WAS IN A PLACE ON THE TOP OF THE ENGINE THAT WAS READILY DETERMINABLE AS THE WATER WAS SHOOTING STRAIGHT UP FROM WHERE THE FITTING HAD COME UNGLUED AND SLIPPED OFF. I DO NOT CURRENTLY KNOW WHETHER I GOT THE CAR STOPPED IN TIME FOR THE ENGINE TO BE OK. I AM AFRAID TO DRIVE IT BEFORE I GET ALL OF THE ALUMINUM FITTINGS REGLUED OR WELDED. BECAUSE THIS HAPPENED ON THE TOP OF THE ENGINE, THE COOLANT DID NOT CREATE A SITUATION THAT WAS A SAFETY RISK TO ME, BUT IF IT HAD BEEN A DIFFERENT ALUMINUM COOLANT ATTACHMENT THAT LET LOOSE, I COULD HAVE CRASHED AT 115 MPH DUE TO COOLANT ON THE TIRES OR SOMEONE BEHIND ME COULD HAVE CRASHED. THE MILLER MOTORSPORT PERSONNEL SAID THEY NOTICED A PLUME OF STEAM AT THE END OF THE FRONT STRAIGHT. AT THE END OF THE FRONT STRAIGHT, I HAD SLOWED TO 115 MPH. I AM THE ORIGINAL PURCHASER OF THIS CAR AND DID NOT THINK I WAS AT RISK FOR THIS TYPE OF SAFETY ISSUE ON A CAR THAT IS NOT DRIVEN IN STOP AND GO TRAFFIC. IT ALSO ONLY HAS A LITTLE OVER 28,000 MILES. *LN UPDATED 1/8/2013 *JSRead more
Incident date: Sep 13, 2013
COOLANT HOSE COUPLING CAME LOSE WHILE DRIVING THE VEHICLE AT SPEED, RESULTING IN LOSS OF ALL ENGINE COOLANT. COOLANT SPILLED RESULTED IN TEMPORARY REDUCTION OF VEHICLE TRACTION, FORTUNATELY WITHOUT INCIDENT. ENGINE DAMAGE DUE TO POSSIBLE OVERHEATING IS UNDER INVESTIGATION. *TR
Incident date: Sep 13, 2013
COOLANT HOSE COUPLING CAME LOSE WHILE DRIVING THE VEHICLE AT SPEED, RESULTING IN LOSS OF ALL ENGINE COOLANT. COOLANT SPILLED RESULTED IN TEMPORARY REDUCTION OF VEHICLE TRACTION, FORTUNATELY WITHOUT INCIDENT. ENGINE DAMAGE DUE TO POSSIBLE OVERHEATING IS UNDER INVESTIGATION. *TR
Incident date: Sep 13, 2013
COOLANT HOSE COUPLING CAME LOSE WHILE DRIVING THE VEHICLE AT SPEED, RESULTING IN LOSS OF ALL ENGINE COOLANT. COOLANT SPILLED RESULTED IN TEMPORARY REDUCTION OF VEHICLE TRACTION, FORTUNATELY WITHOUT INCIDENT. ENGINE DAMAGE DUE TO POSSIBLE OVERHEATING IS UNDER INVESTIGATION. *TR
Incident date: Aug 30, 2013
THE EPOXY HOLDING AN ALUMINUM ELBOW THAT CONNECTS A COOLANT HOSE TO THE WATER PUMP (I BELIEVE) LET GO, THE ELBOW WORKED ITS WAY LOOSE FROM THE PUMP AND EMPTIED THE COOLANT FROM THE SYSTEM OUT ONTO THE ROAD SURFACE. I BECAME AWARE OF THE PROBLEM WHEN I NOTICED THAT THE ENGINE TEMPERATURE NEEDLE HAD PEGGED AT THE HIGH END OF THE GAUGE RANGE, AFTER WHICH THE ENGINE TEMPERATURE WARNING LIGHT CAME ON.
... PRIOR THERETO, THE ENGINE TEMPERATURE GAUGE HAD BEEN READING AT NORMAL LEVELS AND RESPONDING NORMALLY. I WAS ABLE TO STOP WITHOUT AN ACCIDENT, BUT I NOTICED AFTER STOPPING THAT THE RIGHT REAR TIRE AND WHEEL WELL WERE WET AND SLIPPERY WITH COOLANT.Read more
Incident date: Sep 4, 2013
DRIVING ON FREEWAY AT ABOUT 70 MPH AND INTERMEDIATE SHAFT FAILED. CREATED DANGEROUS SITUATION AS ENGINE STARTED BILLOWING SMOKE, OBSCURING TRAFFIC CAUSING MANY CARS TO SWERVE DANGEROUSLY AND HAD STOP ABRUPTLY. CAR TOWED TO REPAIR SHOP EMPIRE AUTOHAUS, INC. WHERE PROBLEM WAS DIAGNOSED. OWNED CAR FOR THREE YEARS WITH ZERO PROBLEMS AND REGULAR SERVICE. LEARNED THAT MANY PORSCHE AUTOMOBILES WITH T
... HE M96 ENGINE (UP TO 25%) WITH LESS THAN 90,000 MILES HAVE HAD SAME PROBLEM AND HAS YET TO BE ADDRESSED BY MANUFACTURER. *JBRead more
Incident date: Sep 4, 2013
DRIVING ON FREEWAY AT ABOUT 70 MPH AND INTERMEDIATE SHAFT FAILED. CREATED DANGEROUS SITUATION AS ENGINE STARTED BILLOWING SMOKE, OBSCURING TRAFFIC CAUSING MANY CARS TO SWERVE DANGEROUSLY AND HAD STOP ABRUPTLY. CAR TOWED TO REPAIR SHOP EMPIRE AUTOHAUS, INC. WHERE PROBLEM WAS DIAGNOSED. OWNED CAR FOR THREE YEARS WITH ZERO PROBLEMS AND REGULAR SERVICE. LEARNED THAT MANY PORSCHE AUTOMOBILES WITH T
... HE M96 ENGINE (UP TO 25%) WITH LESS THAN 90,000 MILES HAVE HAD SAME PROBLEM AND HAS YET TO BE ADDRESSED BY MANUFACTURER. *JBRead more
Incident date: Sep 4, 2013
DRIVING ON FREEWAY AT ABOUT 70 MPH AND INTERMEDIATE SHAFT FAILED. CREATED DANGEROUS SITUATION AS ENGINE STARTED BILLOWING SMOKE, OBSCURING TRAFFIC CAUSING MANY CARS TO SWERVE DANGEROUSLY AND HAD STOP ABRUPTLY. CAR TOWED TO REPAIR SHOP EMPIRE AUTOHAUS, INC. WHERE PROBLEM WAS DIAGNOSED. OWNED CAR FOR THREE YEARS WITH ZERO PROBLEMS AND REGULAR SERVICE. LEARNED THAT MANY PORSCHE AUTOMOBILES WITH T
... HE M96 ENGINE (UP TO 25%) WITH LESS THAN 90,000 MILES HAVE HAD SAME PROBLEM AND HAS YET TO BE ADDRESSED BY MANUFACTURER. *JBRead more
Incident date: Jun 15, 2012
TL* THE CONTACT OWNS A 2012 PORSCHE CAYENNE. THE CONTACT STATED THAT HE NOTICED AN ABNORMAL GLARE FROM THE WINDSHIELD WHILE ENTERING A RESIDENTIAL GARAGE. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 50.
Incident date: Aug 16, 2013
TL* THE CONTACT OWNS A 2011 PORSCHE CAYENNE S. THE CONTACT STATED THAT WHEN HE STARTED THE VEHICLE, THE ENGINE AND STABILITY WARNING LIGHTS ILLUMINATED AS THE VEHICLE BEGAN TO SHAKE VIOLENTLY. THE DEALER WAS NOTIFIED OF THE FAILURE BUT STATED THAT THEY HAD NO AVAILABILITY TO REPAIR THE VEHICLE. THE FAILURE CEASED FOUR DAYS LATER BUT SOON RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. TH
... E VEHICLE HAD NOT BEEN REPAIRED. THE VIN WAS UNAVAILABLE. THE FAILURE AND CURRENT MILEAGE WAS 20,000. THE VIN WAS NOT AVAILABLE. UPDATED 09/17/13*LJ THE CONSUMER STATED PORSCHE IS MAKING THE NECESSARY REPAIRS. UPDATE 09/18/13Read more
Incident date: Aug 23, 2013
TL* THE CONTACT OWNS A 2004 PORSCHE CAYENNE S. THE CONTACT STATED THAT THE TREAD WALL SEPARATED ON ALL FOUR OF THE TIRES. THE TIRES WERE INSPECTED BUT WERE NOT DIAGNOSED. THE TIRES HAD NOT BEEN REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE APPROXIMATE VEHICLE FAILURE MILEAGE WAS 129,000. THE TIRE FAILURE MILEAGE WAS UNKNOWN. UPDATED 10/17/13*LJ THE CONSUMER PURCHASED THE TIRES FROM A
... TIRE RETAILER. THE TIRE SEPARATED ON THE SIDE WALL PREMATURELY.Read more
Incident date: May 29, 2013
MY CAR IS A 2002 PORSCHE GT2 (THE DROP DOWN MENU ABOVE DID NOT HAVE A 2002 TO SELECT). IT IS A STREET CAR BUT TO FULLY ENJOY IT I PARTICIPATE IN HIGH SPEED DRIVER EDUCATION EVENTS HELD ON RACETRACKS BUY THE PORSCHE AND BMW CLUBS. THE ENGINES IN THESE CARS ARE KNOWN TO HAVE CATASTROPHIC COOLANT LINE FITTING FAILURES. THESE FITTINGS ARE ADHERED TO THE MANIFOLDS AND THEY CAN COME LOOSE. WHEN THEY D
... O ALL THE COOLANT DUMPS OUT QUICKLY. AS ANTIFREEZE IS EXTREMELY SLIPPERY THIS CAN CAUSE A VERY DANGEROUS AND LIFE THREATENING SITUATION BOTH TO THE PORSCHE AND CARS BEHIND; THE CARS, DRIVERS AND OCCUPANTS THAT MAY DRIVE OVER THE COOLANT ARE AT RISK. I HAD ONE OF THE 7 COOLANT LINE FITTINGS IN THE CAR FAIL AT A HIGH PERFORMANCE DRIVING EDUCATION EVENT AT NEW HAMPSHIRE MOTOR SPEEDWAY WHILE BRAKING HARD FROM THE BACK STRAIGHTAWAY ENTERING TURN 3. I WAS SLOWING FROM A HIGH SPEED WHEN THE FITTING FAILED. MY REAR END WIGGLED WHEN THE TIRES HIT THE COOLANT BUT FORTUNATELY NEITHER I OR ANYONE ELSE ON THE TRACK HAD AN INCIDENT. THE TRACK WAS SHUT DOWN FOR 30 MINUTES WHILE THEY CLEANED UP THE SLIPPERY, DANGEROUS SURFACE. PORSCHE HAS KNOWN OF THIS PROBLEM FOR YEARS YET HAS NOT ISSUED A RECALL. THE PROPER REPAIR WHICH I HAD PERFORMED ENTAILS WELDING ALL THE FITTINGS AT A COST OF APPROXIMATELY $5000. THIS IS THE ONLY ACCEPTABLE SOLUTION, ONE PORSCHE SHOULD BE DOING PROACTIVELY AND SHOULD COVER THE COSTS FOR FOLKS LIKE ME, TO PREVENT POTENTIALLY FATAL ACCIDENTS. *TRRead more
Incident date: Jul 28, 2013
SUDDEN COOLANT LINE FITTING FAILURE. THE EPOXY FAILED AND A COOLANT FITTING COMPLETELY POPPED OUT OF THE ENGINE HOUSING NEAR THE ALTERNATOR. RESULTED IN RAPID COOLANT LOSS. CAR HAD TO BE TOWED/HAULED APPROX 140 MILES TO REPAIR FACILITY NEAR MY HOME. I HAVE NOT YET SEEN THE BILL FOR THIS SERVICE. I AM HAVING ALL COOLANT FITTINGS WELDED TO PREVENT THIS FROM HAPPENING TO ANY OF THE OTHER LINE
... S. WORK IS NOT YET COMPLETE BUT THE ESTIMATED BILL IS $3500+. *TRRead more
Incident date: Jul 26, 2013
TRAVELING IN A STRAIGHT LINE ON A DRY ROAD AT AROUND 65MPH, THE VEHICLE'S ENGINE EXPIRED IN A HUGE PLUME OF COOLANT/OIL. FLATBEDDED TO A PORSCHE DEALERSHIP, A TECHNICIAN USING A BOROSCOPE FOUND (ACCORDING TO THE DEALERSHIP) "SCORING TO #5 CYLINDER AND EVIDENCE THAT A VALVE HAD HIT THE TOP OF THE PISTON. THERE WAS ALSO A HUGE AMOUNT OF METAL DEBRIS IN THE OIL FILTER." THIS WAS A RESULT OF SOMETHING
... FAILING IN THE ENGINE, RATHER THAN THE CAUSE OF THE FAILURE. THE PORSCHE DEALERSHIP DID NOT CARE TO DETERMINE THE CAUSE OF THE FAILURE. I SUSPECT INTERMEDIATE MAIN SHAFT (IMS) FAILURE. ONE YEAR BEYOND CERTIFIED PRE-OWNED (CPO) WARRANTY AND $20K FOR A NEW ENGINE. *TRRead more
Incident date: Aug 16, 2008
WHILE DRIVING AT A DRIVERS EDUCATION EVENT AT WATKINS GLEN RACE TRACK, A COOLANT FITTING CAME APART AND OUT OF ITS HOUSING RELEASING ABOUT 3-4 GALLONS OF COOLANT ONTO THE TRACK. LUCKILY NO ACCIDENT OCCURRED. SINCE THE CAR WAS STILL UNDER WARRANTY PORSCHE AGREED TO COVER THE FAILURE UNDER GOOD WILL AND A NEW HOUSING (SAME DESIGN) WAS INSTALLED BY THE LOCAL PORSCHE DEALER. HOWEVER, IN OCTOBER, 2011
... WHILE DRIVING AT ANOTHER DRIVERS EDUCATION EVENT, THE SAME FITTING FAILED. THIS TIME 3 CARS FOLLOWING ME SLID OFF THE TRACK DUE TO THE COOLANT WITH ONE CRASHING INTO ANOTHER. ONE CAR WAS TOTALED AND THE OTHER SERIOUSLY DAMAGED. *TRRead more
Incident date: Jul 25, 2013
DRIVING AT A CONSTANT 50MPH AND HAD A VERY STRONG COOLANT SMELL COME THROUGH THE CABIN. PULLED OVER AND SAW COOLANT SLOWLY DRIPPING UNDER ENGINE. LET CAR COOL DOWN AND DROVE HOME. HAVE NOT DRIVEN CAR SINCE. SCHEDULED A APPOINTMENT WITH DEALER FOR 08/08/13. *TR
Incident date: Jul 31, 2013
DUE TO HIGHLIGHTED PROBLEMS WITH THE COOLING SYSTEM (NAMELY THE FITTINGS POPPING OFF) ON THE 2005 PORSCHE 911 GT3 IN VARIOUS FORUMS AND WEB SITES. I HAVE DECIDED TO PERFORM PREVENTATIVE MAINTENANCE AND TO ALLEVIATE SAFETY CONCERN WITH THE COOLING SYSTEM (FITTING AND HOSES) TO WELD THE COOLANT CUPLINGS. *TR
Incident date: Jul 25, 2013
A COOLANT LINE CAME LOOSE THEN I WAS DRIVING THE CAR. I WAS VERY LUCKY I DID NOT SPIN IN THE COOLANT, AND GET IN A SERIOUS ACCIDENT. THIS IS A VERY SERIOUS SAFETY ISSUE. THE LINES WERE ORIGINALLY "GLUED" IN FROM THE FACTORY. THIS WAS A POOR DESIGN AND IS A WEAKNESS OF THE CAR WHICH COULD HAVE BEEN CATASTROPHIC IN TERMS OF DESTROYING THE ENGINE, AND GETTING IN A SERIOUS ACCIDENT. IN ORDER TO P
... ROPERLY ADDRESS THE DESIGN ISSUE I WAS QUOTED OVER $3,000 TO RESOLVE THE ISSUE. THIS INVOLVES TAKING THE ENGINE OUT AND WELDING THE LINES. I BELIEVE PORSCHE SHOULD PAY FOR THE REPAIR. *TRRead more
Incident date: Jul 25, 2013
A COOLANT LINE CAME LOOSE THEN I WAS DRIVING THE CAR. I WAS VERY LUCKY I DID NOT SPIN IN THE COOLANT, AND GET IN A SERIOUS ACCIDENT. THIS IS A VERY SERIOUS SAFETY ISSUE. THE LINES WERE ORIGINALLY "GLUED" IN FROM THE FACTORY. THIS WAS A POOR DESIGN AND IS A WEAKNESS OF THE CAR WHICH COULD HAVE BEEN CATASTROPHIC IN TERMS OF DESTROYING THE ENGINE, AND GETTING IN A SERIOUS ACCIDENT. IN ORDER TO P
... ROPERLY ADDRESS THE DESIGN ISSUE I WAS QUOTED OVER $3,000 TO RESOLVE THE ISSUE. THIS INVOLVES TAKING THE ENGINE OUT AND WELDING THE LINES. I BELIEVE PORSCHE SHOULD PAY FOR THE REPAIR. *TRRead more
Incident date: Jul 27, 2013
SUMMARY: FAILURE OF COOLANT HOSES DURING NORMAL OPERATION OF VEHICLE, RESULTING IN IMMEDIATE FLUSHING OF ALL COOLANT ONTO ROAD SURFACE AND INTO ENGINE BAY. IMMEDIATE ENGINE SHUTDOWN REQUIRED TO PREVENT FURTHER DAMAGE. OBSERVED RISKS INCLUDE: PANIC SITUATION TO OPERATOR AND PASSENGERS OF VEHICLE; CATASTROPHIC ENGINE FAILURE DUE TO OVERHEATING AND CONSEQUENT ACCIDENT THREAT; LOSS OF TRACTION TO VEHI
... CLE AND SUBSEQUENT TRAFFIC DUE TO HIGH VOLUME OF COOLANT ON ROAD SURFACE; VAPOR TRAIL LIMITING VISIBILITY OF SUBSEQUENT TRAFFIC; ROADSIDE ACCIDENT HAZARD AFFECTING VEHICLE AND SUBSEQUENT TRAFFIC. DETAILS: SATURDAY, JULY 27, 2013, ~7:15PM ET, NASSAU COUNTY NY - WESTBOUND ON STATE ROUTE 24 - HEMPSTEAD TURNPIKE. DRIVING AT APPROXIMATELY 45MPH IN 3RD GEAR, VEHICLE OPERATOR NOTICED A THICK CLOUD OF VAPOR EMANATING FROM THE REAR OF THE VEHICLE, OVER THE ENGINE COMPARTMENT. OPERATOR BROUGHT VEHICLE TO A HALT IN THE MIDDLE OF THE ROAD, WHEREUPON THE ODOR OF BURNING COOLANT WAS DETECTED. HAVING BEEN FAMILIARIZED WITH REPORTS OF LIKE VEHICLES BEING AFFLICTED WITH THESE SYMPTOMS, OPERATOR IMMEDIATELY PLACED VEHICLE INTO REVERSE AND BACKED VEHICLE OFF OF ROUTE 24 AND ONTO A SIDE STREET, AND TURNED OFF VEHICLE BY REMOVING THE KEY. OPERATOR OBSERVED THE OUTSIDE TEMPERATURE TO BE APPROXIMATELY 75 DEGREES FAHRENHEIT, AND THE VEHICLE'S REPORTED (REMAINING) COOLANT TEMPERATURE TO BE APPROXIMATELY 190 DEGREES CENTIGRADE AT THE TIME OF THE INCIDENT. ALL OTHER VEHICLE SYSTEMS WERE FUNCTIONING PROPERLY AT THE TIME OF THE INCIDENT. VEHICLE HAS BEEN REGULARLY SERVICED AND ITS ENGINE, INTAKE, AND COOLING SYSTEMS ARE UNMODIFIED, FACTORY SPECIFICATION. OPERATOR HAS PHOTOGRAPHIC EVIDENCE OF THE EVENT AND WILL PROVIDE TO NHTSA AND RELATED PARTIES UPON LAWFUL REQUEST. *TRRead more
Incident date: Jun 27, 2013
WHILE DRIVING ON THE HIGHWAY A CATASTROPHIC FAILURE OCCURRED IN THE COOLANT SYSTEM. ONE OF THE ALUMINUM HOSE FITTINGS THAT IS EPOXIED INTO THE ALUMINUM HOUSING BROKE FREE CAUSING ENGINE COOLANT TO EMPTY OUT OF THE ENGINE ONTO THE HIGHWAY IN A MATTER OF SECONDS. THE RUBBER HOSE DID NOT FAIL AND IT WAS STILL CONNECTED TO ALUMINUM HOSE FITTING THAT BROKE AWAY FROM THE HOUSING. I PULLED THE CAR OFF
... THE FREEWAY IMMEDIATELY TO PREVENT FURTHER DAMAGE TO THE CAR. FURTHER INSPECTION AT THE DEALER SERVICE CENTER SHOWED THERE WAS VERY LITTLE TO NO COOLANT LEFT IN THE ENTIRE SYSTEM. *TRRead more
Incident date: Mar 16, 2013
I WAS DRIVING MY CAR ON I-79(3 LANE HIGHWAY) AT 70 MPH WHEN I NOTICED A LARGE CLOUD OF SMOKE/STEAM FROM THE REAR OF MY CAR. I THEN NOTICED OTHER CARS PULLING OFF TO THE SIDE TO GET AWAY FROM ALL THE COOLANT SPRAYING FROM MY CAR. I PULLED OFF TO THE SIDE OF THE ROAD AND CALLED FOR A TOW TRUCK. OUNCE I WAS ABLE TO GET PORSCHE DEALER TO LOOK AT THE ISSUE, IT WAS INDICATED THAT MY COOLANT FITTINGS FAI
... LED AND SEPARATED FROM THE ENGINE(KNOW ISSUE). *TRRead more
Incident date: Sep 22, 2012
PULLING AWAY FROM A GREEN LIGHT IN TRAFFIC, THE ENGINE STARTED TO UPSHIFT INTO A HIGHER GEAR MUCH SOONER THAN NORMAL AND THE CAR FELT DOWN ON POWER. THE ENGINE SOUNDED AS THOUGH IT WAS RUNNING ON FEWER THAN NORMAL CYLINDERS. I STOPPED THE VEHICLE IMMEDIATELY & HAD IT TOWED TO A PORSCHE SPECIALIST. THEY TOLD ME IT WAS AN IMS (INTERMEDIATE SHAFT) BEARING FAILURE AND THAT IS WAS A KNOWN PROBLEM
... WITH M96 AND M97 PORSCHE ENGINES. MINE BEING AN M96 ENGINE. *TRRead more
Incident date: Sep 22, 2012
PULLING AWAY FROM A GREEN LIGHT IN TRAFFIC, THE ENGINE STARTED TO UPSHIFT INTO A HIGHER GEAR MUCH SOONER THAN NORMAL AND THE CAR FELT DOWN ON POWER. THE ENGINE SOUNDED AS THOUGH IT WAS RUNNING ON FEWER THAN NORMAL CYLINDERS. I STOPPED THE VEHICLE IMMEDIATELY & HAD IT TOWED TO A PORSCHE SPECIALIST. THEY TOLD ME IT WAS AN IMS (INTERMEDIATE SHAFT) BEARING FAILURE AND THAT IS WAS A KNOWN PROBLEM
... WITH M96 AND M97 PORSCHE ENGINES. MINE BEING AN M96 ENGINE. *TRRead more
Incident date: Feb 3, 2013
PRESS FIT GLUED COOLANT PIPE FITTING FAILED ? COOLANT COVERED ENGINE AND REAR TIRES. *TR
Incident date: Mar 27, 2013
TL* THE CONTACT OWNS A 2013 PORSCHE 911 CARRERA 4. THE CONTACT STATED THAT WHILE AT A TRAFFIC STOP, THE VEHICLE SURGED FORWARD WITHOUT WARNING. THE CONTACT MENTIONED THAT THE FAILURE RECURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS TAKEN TO A DEALER WHERE THE FAILURE WAS UNABLE TO BE REPLICATED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE
... MILEAGE WAS 500 AND THE CURRENT MILEAGE WAS 3,000. THE VIN WAS NOT AVAILABLE. *TRRead more
Incident date: Mar 15, 2013
TL* THE CONTACT OWNS A 2007 PORSCHE 911 TURBO. THE CONTACT STATED THAT WHILE PARKED, HE NOTICED A STRONG COOLANT ODOR. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC FOR DIAGNOSIS. THE MECHANIC STATED THAT THE COOLANT FITTINGS WOULD HAVE TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 22,700. *TR
Incident date: Apr 28, 2013
THE CAR DEVELOPED A COOLANT LEAK THAT WAS DISCOVERED WHEN I STOPPED THE CAR AND NOTICED FLUID LEAKING UNDER THE DRIVERS SIDE REAR TIRE. THE CAR WAS TAKEN IN TO PORSCHE AND THERE WAS A FAILED COOLANT LINE. *TR
Incident date: Oct 19, 2011
ON TWO SEPARATE OCCASIONS, THE COOLANT FITTINGS WHICH MOUNT IN THE CYLINDER HEAD POPPED OUT. THE FITTINGS ATTACH TO THE COOLANT HOSES. IN BOTH CASES THE EPOXY THAT HELD THE FITTINGS IN HAD FAILED. EACH TIME I WAS DRIVING AND COOLANT SPEWED ALL OVER THE INSIDE OF THE ENGINE BAY AND THEN SUBSEQUENTLY ONTO THE ROAD AS I WAS DRIVING. THE FIRST INCIDENT I WAS DRIVING ABOUT 50 MPH (10/19/11 - 52230 MILE
... S ON THE ODOMETER). WHEN THIS FIRST FITTING POPPED OUT, SINCE IT WAS BEHIND THE ALTERNATOR, DAMAGED IT REQUIRING REPLACEMENT OF THE ALTERNATOR. I HAD TO PAY FOR THE ALTERNATOR AND EPOXIED THAT FITTING OUT. THE SECOND FITTING FAILED ON JUNE 14, 2012 WITH 56384 MILES ON THE ODOMETER. THIS TIME IT WAS IN A LOCATION THAT REQUIRED REMOVAL OF THE ENGINE. THE CIRCUMSTANCES WERE SIMILAR TO THE FIRST, AROUND 50 MPH AND COOLANT DUMPING OVER ALL OVER THE GROUND. SINCE THIS HAPPENED A SECOND TIME, THE SHOP I TOOK THE CAR TO REMOVED ALL 8 OF THE COOLANT FITTINGS IN THE ENGINE, REMOVED THE EPOXY, AND THEN WELDED THEM INTO PLACE. AFTER TWO OF THE FITTINGS POPPED OUT, I WAS NOT GOING TO TAKE ANY CHANCES OF ANOTHER FITTING POPPING OUT AND BEING LEFT STRANDED YET AGAIN. *TRRead more
Incident date: Jan 28, 2012
WHILE DRIVING THE CAR ON TRACK, A COOLANT FITTING BROKE LOOSE AND DUMPED ALL THE ANTIFREEZE DOWN ONTO THE TRACK SURFACE. A VEHICLE ON TRACK BEHIND ME RAN OVER THE ANTIFREEZE, LOST CONTROL AND SKIDDED OFF THE TRACK. THE DRIVER OF THE OTHER CAR WASN'T INJURED AND THERE DIDN'T APPEAR TO BE MUCH DAMAGE TO HIS CAR, EXCEPT PERHAPS SOME SCUFFING OF THE PAINT ON HIS FRONT BUMPER. THE FITTING THAT CAME
... LOOSE IS ONE OF 8 FITTINGS THAT PORSCHE GLUED INTO PLACE WHEN THEY ORIGINALLY BUILT THE ENGINE OF MY 04 GT3. WHEN THE GLUE GETS OLD IT LETS GO, AND THAT'S WHAT HAPPENED TO ME. I HAD TO FLAT BED THE CAR FROM THE TRACK TO A REPAIR SHOP, PAY THEM TO DROP THE ENGINE, COMPLETELY DISASSEMBLE ALL THE COOLANT MANIFOLDS THAT USE THESE GLUED-IN FITTINGS, BRING THE MANIFOLDS TO A WELDING SHOP, HAVE THE WELDING SHOP WELD ALL THE FITTINGS INTO PLACE, AND THEN HAVE MY REPAIR SHOP REASSEMBLE THE ENTIRE ENGINE AND RE-INSTALL IN THE CAR. THIS RESULTED IN A CONSIDERABLE EXPENSE, AND THE LOSS OF USE OF MY CAR FOR A COUPLE OF MONTHS WHILE THIS WORK WAS BEING PERFORMED, WAITING ON PARTS TO ARRIVE, ETC. I HAVE PICTURES OF THE FITTINGS THAT HAD TO BE WELDED, WHILE MY ENGINE WAS STILL IN PIECES DURING THE REPAIR PROCESS. *TRRead more
Crash
Incident date: Jun 30, 2013
WAS DRIVING AND MASSIVE AMOUNTS OF ANTIFREEZE LEAKED OUT OF THE BACK ONTO THE ROAD AND ON MY TIRES. ENGINE THEN STARTED TO SMOKE AND OVERHEAT. COULD HAVE BEEN VERY DANGEROUS. OVERFLOW RESERVOIR CAP WAS SCREWED ON TIGHTLY SO THAT WAS NOT THE ISSUE. I READ THAT THERE WERE SOME ISSUES WITH THE 2001-07 PORSCHE 911. MY ENGINE WAS REPLACED IN 2003 SO PERHAPS IT WAS RETROFITTED WITH THE PROBLEM PARTS. I
... T WILL BE AT THE RAY CATENA PORSCHE DEALERSHIP IN EDISON NJ TOMORROW FOR REPAIRS. *TRRead more
Incident date: Jun 8, 2013
ALUMINUM COOLANT PIPE, THAT IS GLUED INTO WATER PUMP MANIFOLD, CAME LOOSE CAUSING MASSIVE LOSS OF COOLANT ALL OVER THE ROAD CAUSING SLIPPERY CONDITIONS FOR OTHER DRIVERS. *TR
Incident date: Jun 26, 2013
I RENTED A 2013 PORSCHE BOXTER CONV. THEY DROPPED IT OFF TO ME AT STORE, DUE TO MY CAR BEING TOWED AWAY FROM BEING HIT. WAS QUICKLY SHOWN THE OUTSIDE TO VERIFY NO BODY OR WHEEL DAMAGE' FEW DAYS LATER, DRIVING RENTAL, I PULL UP BEHIND A PICK UP TRUCK ON THE COLDWATER CYN IN LOS ANGELES, (ONE WAY, EACH DIRECTION} TRAFFIC CAME TO A STANDSTILL, AND THEN MY ENGINE SHUT OFF, TACHOMETER WENT TO ZERO
... . ODD, AND AS I WAS REACHING FOR KEY TO RESTART, I GENTLY PUT MY FOOT ON THE ACCELERATOR, AND WOW, CAR COMES ALIVE AND LURCHES INTO TRUCK IN FRONT OF ME. NOW DAMAGE TO CAR CAN BE REPAIRED, BUT IF I HAD BEEN AT A CROSSWALK WHEN THIS HAPPENED, I COULD HAVE KILLED OR SERIOUSLY INJURED PEDESTRIAN. \ DEALER LATER TELLS ME CAR HAS OPTION OF AUTO STOP.\ SHOULD BE REQUIRED OF RENTAL CAR COMPANIES TO INFORM RENTER OF THIS FEATURE SO AS NOT TO HAVE ACCIDENTS. *TRRead more
Crash
Incident date: Jun 26, 2013
I RENTED A 2013 PORSCHE BOXTER CONV. THEY DROPPED IT OFF TO ME AT STORE, DUE TO MY CAR BEING TOWED AWAY FROM BEING HIT. WAS QUICKLY SHOWN THE OUTSIDE TO VERIFY NO BODY OR WHEEL DAMAGE' FEW DAYS LATER, DRIVING RENTAL, I PULL UP BEHIND A PICK UP TRUCK ON THE COLDWATER CYN IN LOS ANGELES, (ONE WAY, EACH DIRECTION} TRAFFIC CAME TO A STANDSTILL, AND THEN MY ENGINE SHUT OFF, TACHOMETER WENT TO ZERO
... . ODD, AND AS I WAS REACHING FOR KEY TO RESTART, I GENTLY PUT MY FOOT ON THE ACCELERATOR, AND WOW, CAR COMES ALIVE AND LURCHES INTO TRUCK IN FRONT OF ME. NOW DAMAGE TO CAR CAN BE REPAIRED, BUT IF I HAD BEEN AT A CROSSWALK WHEN THIS HAPPENED, I COULD HAVE KILLED OR SERIOUSLY INJURED PEDESTRIAN. \ DEALER LATER TELLS ME CAR HAS OPTION OF AUTO STOP.\ SHOULD BE REQUIRED OF RENTAL CAR COMPANIES TO INFORM RENTER OF THIS FEATURE SO AS NOT TO HAVE ACCIDENTS. *TRRead more
Crash
Incident date: Jun 26, 2013
I RENTED A 2013 PORSCHE BOXTER CONV. THEY DROPPED IT OFF TO ME AT STORE, DUE TO MY CAR BEING TOWED AWAY FROM BEING HIT. WAS QUICKLY SHOWN THE OUTSIDE TO VERIFY NO BODY OR WHEEL DAMAGE' FEW DAYS LATER, DRIVING RENTAL, I PULL UP BEHIND A PICK UP TRUCK ON THE COLDWATER CYN IN LOS ANGELES, (ONE WAY, EACH DIRECTION} TRAFFIC CAME TO A STANDSTILL, AND THEN MY ENGINE SHUT OFF, TACHOMETER WENT TO ZERO
... . ODD, AND AS I WAS REACHING FOR KEY TO RESTART, I GENTLY PUT MY FOOT ON THE ACCELERATOR, AND WOW, CAR COMES ALIVE AND LURCHES INTO TRUCK IN FRONT OF ME. NOW DAMAGE TO CAR CAN BE REPAIRED, BUT IF I HAD BEEN AT A CROSSWALK WHEN THIS HAPPENED, I COULD HAVE KILLED OR SERIOUSLY INJURED PEDESTRIAN. \ DEALER LATER TELLS ME CAR HAS OPTION OF AUTO STOP.\ SHOULD BE REQUIRED OF RENTAL CAR COMPANIES TO INFORM RENTER OF THIS FEATURE SO AS NOT TO HAVE ACCIDENTS. *TRRead more
Crash
Incident date: Jan 18, 2013
I WOULD LIKE TO REPORT THAT MY VEHICLE HAS SUFFERED A COMMON REPORTED INCIDENT RELATED TO THE COOLANT HOSES. THE VEHICLES COOLANT HOSES ARE LEAKING. IT APPEARS THEY ONLY HAD ADHESIVE AND ARE NOT THREADED CAUSING THEM TO LEAK. IT APPEARS VERY COMMON AND IS A HIGH RISK AS IT CAN RUPTURE DURING THE DRIVE. *TR
Incident date: Dec 10, 2011
I WAS DRIVING ON A SATURDAY NIGHT ON INTERSTATE 79 NORTHBOUND AT APPROXIMATELY MILE MARKER 3 BETWEEN MINK SHOALS AND ELKVIEW, WV. I HAD JUST PICKED UP A PIZZA AND I WAS HEADED HOME A FEW MILES FROM MY HOUSE. I WAS GOING UPHILL WHEN I HEARD A POP AND SAW A HUGE PLUME OF STEAM SHOOT OUT FROM BEHIND MY CAR. I THEN TAPPED THE BRAKES AND THE REAR RIGHT TIRE GOT A LITTLE LOOSE AS IT HAD ANTIFREEZE COOL
... ANT SPRAYING DIRECTLY ON IT. I MANAGED TO GET MY CAR HOME AS IT WAS QUICKLY STARTING TO GET HOT AND CLOSE TO OVERHEATING AS THERE WAS NO COOLANT LEFT. I GOOGLED "PORSCHE 911 COOLANT LINE FAILURE" AND QUICKLY LEARNED THAT MY ISSUE HAD HAPPENED TO MANY OTHERS.I LEARNED THAT FROM THE FACTORY PORSCHE GLUES/EPOXIES THE COOLANT FITTINGS INTO THE ENGINE BLOCK AND OVER TIME AND MANY HEAT CYCLES LATER THE GLUE/EPOXY FAILS AND THE COOLANT SPRAYS EVERYWHERE AND MANY TIMES DIRECTLY ON THE REAR TIRES. THIS CREATES AN UNSAFE ENVIRONMENT FOR THE DRIVER AND PASSENGER AND ANYONE IN THE IMMEDIATE VICINITY. I PERFORMED A QUICK FIX ON MY CAR AND PINNED THE FITTING BACK INTO THE BLOCK. I LATER LEARNED THAT THE ENTIRE ENGINE HAD TO BE DROPPED AND EACH OF THE 6 COOLANT LINES NEEDED TO BE WELDED TOGETHER TO TRULY PREVENT THIS FROM BEING A HAZARD. I PAID SEVERAL THOUSAND DOLLARS TO HAVE THE ENGINE DROPPED AND FIXED LIKE PORSCHE SHOULD HAVE DONE FROM THE FACTORY. THEY SHOULD HAVE ADDRESSED THE ISSUE AND OFFERED TO FIX THE FAILED COOLANT LINES UNDER A RECALL BUT TO MY KNOWLEDGE THIS HAS NOT BEEN DONE. PORSCHE CLAIMS NO FAULT OF THEIRS. MANY PERFORMANCE DRIVING EVENTS HAVE IDENTIFIED THE ISSUE AND WON'T LET YOU DRIVE YOUR CAR AT THEIR EVENT UNLESS THE ISSUE HAS BEEN PROPERLY ADDRESSED BY DROPPING THE ENGINE. WHEN YOU SPEND THAT MUCH MONEY ON A CAR OR ANY MONEY FOR THAT MANNER YOU EXPECT THE CAR MANUFACTURE TO DO EVERYTHING POSSIBLE TO KEEP YOUR SAFETY AND THE SAFETY OF OTHERS A HIGH PRIORITY. *TRRead more
Incident date: Dec 10, 2011
I WAS DRIVING ON A SATURDAY NIGHT ON INTERSTATE 79 NORTHBOUND AT APPROXIMATELY MILE MARKER 3 BETWEEN MINK SHOALS AND ELKVIEW, WV. I HAD JUST PICKED UP A PIZZA AND I WAS HEADED HOME A FEW MILES FROM MY HOUSE. I WAS GOING UPHILL WHEN I HEARD A POP AND SAW A HUGE PLUME OF STEAM SHOOT OUT FROM BEHIND MY CAR. I THEN TAPPED THE BRAKES AND THE REAR RIGHT TIRE GOT A LITTLE LOOSE AS IT HAD ANTIFREEZE COOL
... ANT SPRAYING DIRECTLY ON IT. I MANAGED TO GET MY CAR HOME AS IT WAS QUICKLY STARTING TO GET HOT AND CLOSE TO OVERHEATING AS THERE WAS NO COOLANT LEFT. I GOOGLED "PORSCHE 911 COOLANT LINE FAILURE" AND QUICKLY LEARNED THAT MY ISSUE HAD HAPPENED TO MANY OTHERS.I LEARNED THAT FROM THE FACTORY PORSCHE GLUES/EPOXIES THE COOLANT FITTINGS INTO THE ENGINE BLOCK AND OVER TIME AND MANY HEAT CYCLES LATER THE GLUE/EPOXY FAILS AND THE COOLANT SPRAYS EVERYWHERE AND MANY TIMES DIRECTLY ON THE REAR TIRES. THIS CREATES AN UNSAFE ENVIRONMENT FOR THE DRIVER AND PASSENGER AND ANYONE IN THE IMMEDIATE VICINITY. I PERFORMED A QUICK FIX ON MY CAR AND PINNED THE FITTING BACK INTO THE BLOCK. I LATER LEARNED THAT THE ENTIRE ENGINE HAD TO BE DROPPED AND EACH OF THE 6 COOLANT LINES NEEDED TO BE WELDED TOGETHER TO TRULY PREVENT THIS FROM BEING A HAZARD. I PAID SEVERAL THOUSAND DOLLARS TO HAVE THE ENGINE DROPPED AND FIXED LIKE PORSCHE SHOULD HAVE DONE FROM THE FACTORY. THEY SHOULD HAVE ADDRESSED THE ISSUE AND OFFERED TO FIX THE FAILED COOLANT LINES UNDER A RECALL BUT TO MY KNOWLEDGE THIS HAS NOT BEEN DONE. PORSCHE CLAIMS NO FAULT OF THEIRS. MANY PERFORMANCE DRIVING EVENTS HAVE IDENTIFIED THE ISSUE AND WON'T LET YOU DRIVE YOUR CAR AT THEIR EVENT UNLESS THE ISSUE HAS BEEN PROPERLY ADDRESSED BY DROPPING THE ENGINE. WHEN YOU SPEND THAT MUCH MONEY ON A CAR OR ANY MONEY FOR THAT MANNER YOU EXPECT THE CAR MANUFACTURE TO DO EVERYTHING POSSIBLE TO KEEP YOUR SAFETY AND THE SAFETY OF OTHERS A HIGH PRIORITY. *TRRead more
Incident date: Jun 21, 2013
COOLANT PIPES LEAKING AFTER DRIVE. *TR
Incident date: Jun 14, 2013
I HAD THE 8 COOLANT FITTINGS, PRONE TO EPOXY FAILURES, SECURED TO HOUSINGS BY WELDING. COST FOR WELDING WAS $275. *TR
Incident date: Mar 15, 2011
THIS IS IN RESPONSE TO MY AWARENESS OF NHTSA PE13-009. I AM THE THIRD OWNER OF A 2004 PORSCHE GT3 THAT I USE PRIMARILY FOR TRACK DRIVING DAYS AND OCCASIONALLY FOR STREET USE. WHEN I PURCHASED THE CAR IN 2010, I WAS AWARE OF MANY REPORTS FROM OWNERS OF SIMILAR CARS THAT HAD EXPERIENCED SUDDEN COOLANT LOSS FROM ANY OF EIGHT GLUED-IN TUBE-LIKE ALUMINUM FITTINGS TO WHICH COOLANT HOSES ARE ATTACHED.
... THE REPORTS DESCRIBED THE CATASTROPHIC EFFECTS OF COOLANT LOSS, PRIMARILY ON THE TRACK, THAT IN SOME CASES RESULTED IN LOSS OF CONTROL TO THE AFFECTED CAR AND/OR LOSS OF CONTROL TO CARS FOLLOWING THAT CAR. A NUMBER OF CRASHES WERE REPORTED. THESE REPORTS ARE CONTAINED IN VARIOUS ONLINE FORUMS, INCLUDING RENNLIST.COM. BECAUSE I WAS CONCERNED ABOUT THE POSSIBILITY OF THIS FAILURE OCCURRING TO MY CAR, I PROPHYLACTICALLY HAD MY ENGINE REMOVED AND ALL EIGHT COOLANT PIPES WELDED INTO THE ALUMINUM MANIFOLDS THAT THEY HAD ORIGINALLY BEEN GLUED INTO. I DID THIS AT A COST OF $2500. I THINK IT WOULD BE PRUDENT FOR PORSCHE CARS NORTH AMERICA TO RECOGNIZE THE ISSUE CREATED BY THIS POOR DESIGN AND CORRECT IT BY RECALLING CARS THAT HAVE NOT BEEN REPAIRED, AND REIMBURSING OWNERS, LIKE ME, WHO TOOK IT UPON THEMSELVES TO CORRECT THE PROBLEM BEFORE THERE WERE ANY CONSEQUENCES. IT IS INTERESTING TO NOTE THAT VARIOUS SIMILAR-ENGINED FACTORY RACE CARS MADE BY PORSCHE DURING THAT ERA, INCLUDING THE 2001 GT3 RS THAT I OWN, USED A COMPLETELY DIFFERENT (AND MORE ROBUST) THREADED MEANS OF ATTACHING THESE COOLANT FITTINGS TO THE COOLANT MANIFOLD. *TRRead more
Incident date: Aug 17, 2012
I AM CONCERNED THAT THIS COOLANT HOSE ISSUE WILL EFFECT MY CAR AND CAUSE A SAFETY HAZARD. I FEEL THAT THERE SHOULD BE A RECALL FROM PORSCHE TO FIX THIS. I UNDERSTAND THAT THE ENGINE COOLANT HOSE IS GLUED ON USING EPOXY INSTEAD OF WELDED OR THREADED. ALSO, I DON'T WANT TO HAVE TO SHELL OUT $3.5K TO FIX THIS SHOULD IT FAIL BECAUSE MY WARRANTY HAS EXPIRED. IF THE ACTUAL ENGINE BLOWS AS A RESULT O
... F THIS FAILURE I AM LOOKING AT WELL OVER $35000 TO REPLACE THE ENGINE AND FIX THE PROBLEM. MY ENGINE COOLANT TEMPERATURE SENSOR HAS ALREADY FAILED AND WAS REPLACED ON 08/17/2012. *TRRead more
Incident date: Aug 17, 2012
I AM CONCERNED THAT THIS COOLANT HOSE ISSUE WILL EFFECT MY CAR AND CAUSE A SAFETY HAZARD. I FEEL THAT THERE SHOULD BE A RECALL FROM PORSCHE TO FIX THIS. I UNDERSTAND THAT THE ENGINE COOLANT HOSE IS GLUED ON USING EPOXY INSTEAD OF WELDED OR THREADED. ALSO, I DON'T WANT TO HAVE TO SHELL OUT $3.5K TO FIX THIS SHOULD IT FAIL BECAUSE MY WARRANTY HAS EXPIRED. IF THE ACTUAL ENGINE BLOWS AS A RESULT O
... F THIS FAILURE I AM LOOKING AT WELL OVER $35000 TO REPLACE THE ENGINE AND FIX THE PROBLEM. MY ENGINE COOLANT TEMPERATURE SENSOR HAS ALREADY FAILED AND WAS REPLACED ON 08/17/2012. *TRRead more
Incident date: Jul 16, 2011
COOLANT FITTING GLUED INTO THE BLOCK FAILED. THE GLUE FAILED AND THE ENGINE COOLANT BLEW ALL OVER THE ENGINE AND ONTO THE GROUND AFTER BRINGING THE CAR TO A STOP. *TR
Incident date: May 1, 2013
TL* THE CONTACT OWNS A 2007 PORSCHE 911 TURBO. THE CONTACT STATED THAT ANTIFREEZE LEAKED INTO THE ENGINE AND THE ENTIRE UNDER-CARRIAGE. THE VEHICLE HAD NEITHER BEEN DIAGNOSED NOR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE DEFECT. THE APPROXIMATE FAILURE MILEAGE WAS 46,000. ..UPDATED 08-07-13 *BF THE CONSUMER STATED THE LOSS OF ENGINE COOLANT WAS LEAKING ONTO THE REARS TIRES, CAUSING LOS
... S OF TRACTION.Read more
Incident date: May 1, 2013
TL* THE CONTACT OWNS A 2007 PORSCHE 911 TURBO. THE CONTACT STATED THAT ANTIFREEZE LEAKED INTO THE ENGINE AND THE ENTIRE UNDER-CARRIAGE. THE VEHICLE HAD NEITHER BEEN DIAGNOSED NOR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE DEFECT. THE APPROXIMATE FAILURE MILEAGE WAS 46,000. ..UPDATED 08-07-13 *BF THE CONSUMER STATED THE LOSS OF ENGINE COOLANT WAS LEAKING ONTO THE REARS TIRES, CAUSING LOS
... S OF TRACTION.Read more
Incident date: Jul 29, 2012
ENGINE COOLANT LEAKING AT UPPER COOLANT CONSOLE. EPOXY FAILED AT ALUMINUM COOLING HOSE AND COOLING CONSOLE CONNECTION POINT. AT A LATER DATE, REPEATED FAILURE OF COOLING HOSE CONNECTIONS AT RIGHT FRONT RADIATOR. *TR
Incident date: Aug 15, 2009
I PURCHASED MY 2004 PORSCHE GT3 IN MAY OF 2009. IT HAD JUST UNDER 20,000 MILES ON IT. IN AUGUST, 2010, I WAS DRIVING ON TRACK AT TEXAS MOTOR SPEEDWAY AND ONE OF THE COOLANT FITTINGS CAME LOOSE FROM THE ENGINE. THE EPOXY THAT HOLDS THE PRESS-FIT COUPLER TO ONE OF THE HEAT EXCHANGERS HAD LOST ITS ABILITY TO RETAIN THE FITTING AND CAME DISCONNECTED. ALL OF THE ENGINE COOLANT WAS LOST IN A SINGLE
... INSTANCE. [CATASTROPHIC COOLANT LOSS]. I HAD THAT FITTING REPLACED BY THE PORSCHE DEALER IN DALLAS UNDER AFTERMARKET WARRANTY. I CAN PROVIDE INFO REGARDING THE ON THIS AT YOUR REQUEST, AND I HAVE SOME PICTURES OF THE OFFENDING PART. I HAD A SECOND (AND SEPARATE) FITTING FAIL IN JANUARY 2011 AT 35,000 WHILE DRIVING ON TRACK AT MOTORSPORT RANCH HOUSTON. THEY SAME SYMPTOMS WERE FOUND - THE PRESS-FIT COUPLING HAD COME LOOSE RESULTING IN COMPLETE COOLANT LOSS. THIS WAS ALSO REPAIRED WITH A FACTORY REPLACEMENT PART UNDER AFTERMARKET WARRANTY AT THE PORSCHE DEALER IN HOUSTON. I BELIEVE THERE ARE 8 KNOWN PRESS-FIT COUPLERS ON THE GT1 ENGINE BLOCK IN THE 996 AND 997 MODEL GT AND TURBO CARS. EACH OF THESE IS KNOWN TO FAIL BASED ON THE PRESS-FIT COUPLER AND POOR DESIGN (USE OF EPOXY ON A HIGH PRESSURE COMPONENT). I UNDERSTAND THAT THIS IS A KNOWN PROBLEM ON PORSCHE GT/TURBO CARS AND HAS BEEN DISCUSSED ON THE INTERNET (E.G. RENNLIST) FOR MANY YEARS. 25% OF MINE HAVE FAILED, AND ALMOST EVERY OTHER GT DRIVER I KNOW HAS HAD AT LEAST ONE FAIL. *TRRead more
Incident date: Jun 5, 2013
COOLANT PIPE FAILURE. AFTER DRIVING BACK FROM THE AIRPORT AND PARKING, NOTICED HUGE COOLANT POOL FORM UNDER THE CAR. TOOK CAR TO SHOP AND THEY SCOPED THE COOLANT SYSTEM AND FOUND THE COOLANT PIPES HAVE STARTED TO SEPARATE. SHOP SAID THEY HAVE DONE MANY OF THESE REPAIRS, AND THAT MANY TRACKS WILL NOT LET 911 TURBOS ON THEM UNLESS THEY HAVE THESE WELDED BECAUSE OF THE HIGH NUMBER OF SEPARATIONS O
... F THESE PIPES. SEEMS LIKE THE EPOXY METHOD OF SECURING THESE IS NOT SUFFICIENT FOR THESE CARS. *TRRead more