Showing 39,107 complaints for PONTIAC
Incident date: Apr 24, 2007
TUESDAY, 24 APR 2007 1500 HOURS AFTER WORKDAY ENDED, I-25 SOUTHBOUND AT COLORADO MILE MARKER 104 RIGHT LANE, WEATHER PARTLY CLOUDY WITH PARTLY WET ROADWAY, THE PONTIAC GRAND AM 2003 I WAS DRIVING AT 55 MPH STARTED FRONT DRIVE SHAKING. THE VEHICLE RAN OFF THE RIGHT SIDE OF THE HIGHWAY AND ROLLED ONE AND ONE-HALF TIMES IN THE BORROW DITCH. UPSIDE DOWN RESTRAINED BY THE SEAT BELT, I NOTICED THE P
... ONTIAC'S AIR BAGS HAD NOT DEPLOYED AND THE ENGINE WAS NOT RUNNING. AFTER UNBUCKLING THE SEATBELT, I, WITH A SCARRED FOREHEAD, CLIMBED THROUGH THE DRIVERS SIDE BROKEN OUT WINDOW AND EXITED THE VEHICLE. THE COLORADO STATE PATROL ARRIVED, INVESTIGATED , HAD THE VEHICLE TOWED TO THE SALVAGE YARD, AND SENT ME TO THE LOCAL HOSPITAL, AN OUTPATIENT FOR THE FOREHEAD SCAR. 3 JULY 2014 NHTSA RECALL 14V400 AND GM RECALL N140350 UNINTENDED KEY ROTATION FOR MY 1999-2005 PONTIAC GRAND AM. *TRRead more
Crash
Incident date: Apr 24, 2007
TUESDAY, 24 APR 2007 1500 HOURS AFTER WORKDAY ENDED, I-25 SOUTHBOUND AT COLORADO MILE MARKER 104 RIGHT LANE, WEATHER PARTLY CLOUDY WITH PARTLY WET ROADWAY, THE PONTIAC GRAND AM 2003 I WAS DRIVING AT 55 MPH STARTED FRONT DRIVE SHAKING. THE VEHICLE RAN OFF THE RIGHT SIDE OF THE HIGHWAY AND ROLLED ONE AND ONE-HALF TIMES IN THE BORROW DITCH. UPSIDE DOWN RESTRAINED BY THE SEAT BELT, I NOTICED THE P
... ONTIAC'S AIR BAGS HAD NOT DEPLOYED AND THE ENGINE WAS NOT RUNNING. AFTER UNBUCKLING THE SEATBELT, I, WITH A SCARRED FOREHEAD, CLIMBED THROUGH THE DRIVERS SIDE BROKEN OUT WINDOW AND EXITED THE VEHICLE. THE COLORADO STATE PATROL ARRIVED, INVESTIGATED , HAD THE VEHICLE TOWED TO THE SALVAGE YARD, AND SENT ME TO THE LOCAL HOSPITAL, AN OUTPATIENT FOR THE FOREHEAD SCAR. 3 JULY 2014 NHTSA RECALL 14V400 AND GM RECALL N140350 UNINTENDED KEY ROTATION FOR MY 1999-2005 PONTIAC GRAND AM. *TRRead more
Crash
Incident date: Aug 29, 2014
WHILE DRIVING THERE WAS A NOISE SIMILAR TO THAT OF WHICH YOU HEAR WHEN THE SEAT BELT ISN'T ENGAGED THEN THE DISPLAY ON THE RADIO READS "ENGINE POWER REDUCED" THEN IMMEDIATELY AFTER THAT IT READS "ENGINE POWER DISABLED" AND THEN THE CAR SHUTS ITSELF DOWN. I WAS ABLE TO COAST TO SAFETY WHERE I THEN TURNED THE IGNITION TO OFF. TRIED TO START IT AGAIN BUT THE CAR WAS COMPLETELY DEAD. I WAITED 10 MINUT
... ES AND THEN WAS ABLE TO START THE CAR AGAIN BUT IT DIDN'T START NORMAL IT KIND OF SPUTTERED AND THEN STARTED. I WAS THEN ABLE TO DRIVE HOME. A SECOND OCCURRENCE HAPPENED A DIFFERENT DAY WHEN I WAS PARKED. I STARTED THE CAR AND IT IMMEDIATELY MADE THE ABOVE MENTIONED NOISE, GAVE ME THE SAME 2 MESSAGES AND THEN SHUT ITSELF DOWN. I THEN COULD START IT AGAIN AFTER ABOUT 10 MINUTES. I WAS TOLD THIS WAS A THROTTLE BODY ISSUE BY A DEALER AND HAVE NOT YET HAD THIS PROBLEM RESOLVED. THIS IS A VERY DANGEROUS THING TO HAPPEN WHILE YOU ARE DRIVING ESPECIALLY IF YOU HAVE SMALL CHILDREN IN THE CAR. THIS SHOULD BE A RECALL IMMEDIATELY. *TRRead more
Incident date: Aug 29, 2014
WHILE DRIVING THERE WAS A NOISE SIMILAR TO THAT OF WHICH YOU HEAR WHEN THE SEAT BELT ISN'T ENGAGED THEN THE DISPLAY ON THE RADIO READS "ENGINE POWER REDUCED" THEN IMMEDIATELY AFTER THAT IT READS "ENGINE POWER DISABLED" AND THEN THE CAR SHUTS ITSELF DOWN. I WAS ABLE TO COAST TO SAFETY WHERE I THEN TURNED THE IGNITION TO OFF. TRIED TO START IT AGAIN BUT THE CAR WAS COMPLETELY DEAD. I WAITED 10 MINUT
... ES AND THEN WAS ABLE TO START THE CAR AGAIN BUT IT DIDN'T START NORMAL IT KIND OF SPUTTERED AND THEN STARTED. I WAS THEN ABLE TO DRIVE HOME. A SECOND OCCURRENCE HAPPENED A DIFFERENT DAY WHEN I WAS PARKED. I STARTED THE CAR AND IT IMMEDIATELY MADE THE ABOVE MENTIONED NOISE, GAVE ME THE SAME 2 MESSAGES AND THEN SHUT ITSELF DOWN. I THEN COULD START IT AGAIN AFTER ABOUT 10 MINUTES. I WAS TOLD THIS WAS A THROTTLE BODY ISSUE BY A DEALER AND HAVE NOT YET HAD THIS PROBLEM RESOLVED. THIS IS A VERY DANGEROUS THING TO HAPPEN WHILE YOU ARE DRIVING ESPECIALLY IF YOU HAVE SMALL CHILDREN IN THE CAR. THIS SHOULD BE A RECALL IMMEDIATELY. *TRRead more
Incident date: Aug 29, 2014
VEHICLE DISPLAY INDICATES SERVICE AIRBAGS. AIRBAG INDICATOR TURNS RED AS WELL TO INDICATE A AIRBAG PROBLEM. CAUSE OF ISSUE IS A BAD PASSENGER SEAT SENSOR. A COSTLY ITEM TO REPAIR. PROBLEM APPEARS TO BE VERY COMMON WITH PONTIAC SOLSTICE AND SATURN SKY CARS. OWNERS MANUAL SUGGEST THAT WHEN THE SERVICE AIR BAG FAULT IS INDICATED THAT THE AIRBAGS WILL NOT WORK. THIS IS CERTAINLY A SAFETY PROBLEM. SHOU
... LD SOMEONE HAVE A COLLISION BEFORE THEY CAN GET THIS FIXED GREATER INJURY COULD HAPPEN. SUGGEST THAT MANUFACTURER ADDRESS THE RELIABILITY ISSUE OF THESE SENSORS. *TRRead more
Incident date: Jul 15, 2014
TL* THE CONTACT OWNS A 2008 PONTIAC SOLSTICE. THE CONTACT STATED THAT WHILE DRIVING AT 50 MPH, THE VEHICLE DECREASED IN SPEED TO 15 MPH AND THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE ENGINE AND THE POWER TRAIN COMPUTER MODULE FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAIL
... URE MILEAGE WAS 35,000.Read more
Incident date: Jul 15, 2014
TL* THE CONTACT OWNS A 2008 PONTIAC SOLSTICE. THE CONTACT STATED THAT WHILE DRIVING AT 50 MPH, THE VEHICLE DECREASED IN SPEED TO 15 MPH AND THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE ENGINE AND THE POWER TRAIN COMPUTER MODULE FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAIL
... URE MILEAGE WAS 35,000.Read more
Incident date: Oct 1, 2013
I WAS PURCHASING THIS USED CAR FROM A DEALER. THEY REPLACED THE IGNITION ASSEMBLY 3 TIMES. THE CAR WOULD MYSTERIOUSLY SHUT OFF, THE IGNITION ASSEMBLY WOULD NOT ALLOW THE KEY TO BE REMOVED AND MULTIPLE TIMES THIS HAPPENED. I LOST ALLOT OF MONEY I PUT ON THE CAR AS IT BECAME OBVIOUS THEY COULD NOT FIX IT AND I HAD TO LET THEM TAKE IT BACK WITH NO REFUND TO ME.........THEY SAID AT THE DEALER THAT I
... WAS LUCKY THAT I DIDN'T HAVE A FIRE. *TRRead more
Incident date: Oct 1, 2013
I WAS PURCHASING THIS USED CAR FROM A DEALER. THEY REPLACED THE IGNITION ASSEMBLY 3 TIMES. THE CAR WOULD MYSTERIOUSLY SHUT OFF, THE IGNITION ASSEMBLY WOULD NOT ALLOW THE KEY TO BE REMOVED AND MULTIPLE TIMES THIS HAPPENED. I LOST ALLOT OF MONEY I PUT ON THE CAR AS IT BECAME OBVIOUS THEY COULD NOT FIX IT AND I HAD TO LET THEM TAKE IT BACK WITH NO REFUND TO ME.........THEY SAID AT THE DEALER THAT I
... WAS LUCKY THAT I DIDN'T HAVE A FIRE. *TRRead more
Incident date: Oct 1, 2013
I WAS PURCHASING THIS USED CAR FROM A DEALER. THEY REPLACED THE IGNITION ASSEMBLY 3 TIMES. THE CAR WOULD MYSTERIOUSLY SHUT OFF, THE IGNITION ASSEMBLY WOULD NOT ALLOW THE KEY TO BE REMOVED AND MULTIPLE TIMES THIS HAPPENED. I LOST ALLOT OF MONEY I PUT ON THE CAR AS IT BECAME OBVIOUS THEY COULD NOT FIX IT AND I HAD TO LET THEM TAKE IT BACK WITH NO REFUND TO ME.........THEY SAID AT THE DEALER THAT I
... WAS LUCKY THAT I DIDN'T HAVE A FIRE. *TRRead more
Incident date: Sep 1, 2014
SOMETIMES MY BLINKER WILL STOP WORKING. YOU CAN HEAR IT GOING BUT YOU WILL NOT SEE IT APPEAR ON THE DASH AND THE IT WILL START WORKING AGAIN AFTER A WHILE. ALSO THERE IS TIMES WHERE I'VE JUST USED THE BLINKER AND THEN IT WILL CONTINUE TO SOUND LIKE IT'S STILL BLINKING BUT IT'S NOT ON JUST THE SOUND OF THE BLINKER IS STILL GOING. I ALSO HAVE A PROBLEM WITH THE KEY TURNING AT ALL UNTIL I TURN THE W
... HEEL A BIT. *TRRead more
Incident date: Apr 1, 2013
TL* THE CONTACT OWNS A 2003 PONTIAC GRAND AM. THE CONTACT STATED UPON TAKING THE VEHICLE TO AN INDEPENDENT MECHANIC FOR ANOTHER SERVICE, THE MECHANIC INFORMED THE CONTACT THAT THE VEHICLE WAS LEAKING FUEL. THE CONTACT HAD NOTICED THAT THE "CHECK ENGINE" WARNING LIGHT WAS CONTINUOUSLY ILLUMINATED. THE CONTACT WAS THEN DRIVING APPROXIMATELY 35 MPH WHEN VEHICLE BEGAN TO SHUDDER. THE CONTACT THEN
... COASTED OVER TO AN EMERGENCY LANE AND THE ENGINE STALLED. THE ENGINE DID NOT RESTART AND WAS TOWED TO THE CONTACT'S RESIDENCE. THE VEHICLE HAD NOT BEEN TAKEN BACK TO A MECHANIC FOR DIAGNOSTIC TEST. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER :07E021000(FUEL SYSTEM, OTHER). THE APPROXIMATE FAILURE MILEAGE WAS 155,825.Read more
Incident date: Apr 1, 2013
TL* THE CONTACT OWNS A 2003 PONTIAC GRAND AM. THE CONTACT STATED UPON TAKING THE VEHICLE TO AN INDEPENDENT MECHANIC FOR ANOTHER SERVICE, THE MECHANIC INFORMED THE CONTACT THAT THE VEHICLE WAS LEAKING FUEL. THE CONTACT HAD NOTICED THAT THE "CHECK ENGINE" WARNING LIGHT WAS CONTINUOUSLY ILLUMINATED. THE CONTACT WAS THEN DRIVING APPROXIMATELY 35 MPH WHEN VEHICLE BEGAN TO SHUDDER. THE CONTACT THEN
... COASTED OVER TO AN EMERGENCY LANE AND THE ENGINE STALLED. THE ENGINE DID NOT RESTART AND WAS TOWED TO THE CONTACT'S RESIDENCE. THE VEHICLE HAD NOT BEEN TAKEN BACK TO A MECHANIC FOR DIAGNOSTIC TEST. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER :07E021000(FUEL SYSTEM, OTHER). THE APPROXIMATE FAILURE MILEAGE WAS 155,825.Read more
Incident date: Sep 5, 2014
TL* THE CONTACT OWNS A 2003 PONTIAC VIBE. THE CONTACT RECEIVED NHTSA CAMPAIGN NUMBER: 14V350000 (AIR BAGS) AND STATED THAT THE PART WAS NOT AVAILABLE. THE DEALER WAS UNCERTAIN OF WHEN THE PART WOULD BECOME AVAILABLE TO SERVICE THE VEHICLE UNDER THE RECALL REPAIR. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.... UPDATED 06-02-15 *BF THE CONSUMER STA
... TED THE ISSUE WAS RESOLVED. UPDATED 06/11/15*JBRead more
Incident date: Mar 15, 2011
TL* THE CONTACT OWNS A 2006 PONTIAC G6. THE CONTACT STATED THAT THE AIR BAG WARNING LIGHT INTERMITTENTLY ILLUMINATED. THE CONTACT ALSO STATED THAT THE FRONT PASSENGER SEAT HEATED INDEPENDENTLY. THE FAILURE OCCURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 75,000.
Incident date: Mar 15, 2011
TL* THE CONTACT OWNS A 2006 PONTIAC G6. THE CONTACT STATED THAT THE AIR BAG WARNING LIGHT INTERMITTENTLY ILLUMINATED. THE CONTACT ALSO STATED THAT THE FRONT PASSENGER SEAT HEATED INDEPENDENTLY. THE FAILURE OCCURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 75,000.
Incident date: Mar 23, 2011
TL* THE CONTACT OWNS A 2006 PONTIAC G6. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE BRAKE PEDAL WAS APPLIED AND THE STEERING COLUMN BEGAN TO VIBRATE. THE FAILURE OCCURRED ON MULTIPLE OCCASIONS. THE VEHICLE WAS TAKEN TO A DEALER WHERE IT WAS CONFIRMED THAT THE STEERING COLUMN FAILED. THE CONTACT STATED THAT THE PART WAS NOT AVAILABLE FOR THE RECALL REPAIR FOR NHTSA CAMPAIGN I
... D NUMBER: 14E044000 (STEERING). THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 85,000. .....UPDATED 10/15/15 *BF UPDATED 08/28/2017*CTRead more
Incident date: Mar 23, 2011
TL* THE CONTACT OWNS A 2006 PONTIAC G6. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE BRAKE PEDAL WAS APPLIED AND THE STEERING COLUMN BEGAN TO VIBRATE. THE FAILURE OCCURRED ON MULTIPLE OCCASIONS. THE VEHICLE WAS TAKEN TO A DEALER WHERE IT WAS CONFIRMED THAT THE STEERING COLUMN FAILED. THE CONTACT STATED THAT THE PART WAS NOT AVAILABLE FOR THE RECALL REPAIR FOR NHTSA CAMPAIGN I
... D NUMBER: 14E044000 (STEERING). THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 85,000. .....UPDATED 10/15/15 *BF UPDATED 08/28/2017*CTRead more
Incident date: Aug 20, 2014
TL* THE CONTACT OWNS A 2007 PONTIAC G6. THE CONTACT STATED THAT WHILE DRIVING AT LOW SPEEDS BETWEEN 1 AND 15 MPH A POPPING AND GRINDING TYPE NOISE WAS PRESENT WHEN TURNING THE STEERING WHEEL IN EITHER DIRECTION. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO REPLACED THE RACK AND PINION BUT THE NOISE CONTINUED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 22,000.
Incident date: Jul 1, 2014
I HAVE RECEIVED (2) RECALL NOTICES. 1 RECALL 13036 FOR BCM AND BAS SYSTEM FOR BRAKES AND 1 OTHER RECALL 14152 FOR TRANSMISSION SHIFT CABLE. FIRST CAME AT THE BEGINNING OF JULY/2014 AND THE OTHER THE MIDDLE OF JULY/2014. BOTH STATED THAT PARTS ARE NOT AVAILABLE AND IT HAS BEEN OVER 60 DAYS SINCE I RECEIVED THE NOTICES BUT THE RECALLS WERE ISSUED MAY 16, 2014. *TR
Incident date: Jul 1, 2014
I HAVE RECEIVED (2) RECALL NOTICES. 1 RECALL 13036 FOR BCM AND BAS SYSTEM FOR BRAKES AND 1 OTHER RECALL 14152 FOR TRANSMISSION SHIFT CABLE. FIRST CAME AT THE BEGINNING OF JULY/2014 AND THE OTHER THE MIDDLE OF JULY/2014. BOTH STATED THAT PARTS ARE NOT AVAILABLE AND IT HAS BEEN OVER 60 DAYS SINCE I RECEIVED THE NOTICES BUT THE RECALLS WERE ISSUED MAY 16, 2014. *TR
Incident date: Feb 25, 2014
TL* THE CONTACT OWNS A 2009 PONTIAC G6. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 55 MPH THE POWER STEERING SUDDENLY MALFUNCTIONED MAKING THE STEERING WHEEL VERY DIFFICULT FOR THE DRIVER TO TURN. THE CONTACT INDICATED THAT PRIOR TO THE MALFUNCTION OCCURRING A CHIMING NOISE WAS ACTIVATED INSIDE THE VEHICLE. AFTER TURNING THE ENGINE OFF AND BACK ON THE VEHICLE OPERATED AS NORMAL BEFORE THE
... FAILURE RECURRED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE FAILURE WAS CAUSED BY FAULTY WIRING INSIDE THE STEERING COLUMN. THE STEERING COLUMN WAS REPLACED AND THE FAILURE WAS REMEDIED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 87,000Read more
Incident date: Aug 31, 2014
TL* THE CONTACT OWNS A 2006 PONTIAC G6. THE CONTACT STATED THAT AFTER REFUELING, THE STEERING WHEEL STOPPED WORKING. THE CONTACT HAD TO SHUT OFF AND RESTART THE VEHICLE SEVERAL TIMES IN ORDER TO GET THE STEERING WHEEL OPERATING NORMALLY. THE VEHICLE WAS TAKEN TO THE DEALER. THE TECHNICIAN DIAGNOSED THAT THE POWER STEERING MOTOR AND COLUMN NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MA
... NUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VIN WAS UNAVAILABLE. THE APPROXIMATE FAILURE MILEAGE WAS 127,000.Read more
Incident date: Aug 27, 2002
I WAS DRIVING HOME IN THE AFTERNOON. I LOST CONTROL OF THE POWER STEERING. I TRIED TO MERGE OUT OF MY LANE SO I WOULD NOT IMPACT ANOTHER CAR. I HAD NO CONTROL OF THE STEERING AT ALL. I WAS UNABLE TO MERGE, I HIT THE BACK END OF A UTILITY TRUCK. *TR
Crash
Incident date: Aug 27, 2002
I WAS DRIVING HOME IN THE AFTERNOON. I LOST CONTROL OF THE POWER STEERING. I TRIED TO MERGE OUT OF MY LANE SO I WOULD NOT IMPACT ANOTHER CAR. I HAD NO CONTROL OF THE STEERING AT ALL. I WAS UNABLE TO MERGE, I HIT THE BACK END OF A UTILITY TRUCK. *TR
Crash
Incident date: Aug 22, 2012
DRIVERS SIDE LOCK INDICATOR BROKE OFF WITH NO UNUSUAL DAMAGE OR WEAR THAT WOULD.HAVE CAUSED! HAVE SEEN A LOT OF G6S LIKE THIS! *TR
Incident date: Aug 22, 2012
DRIVERS SIDE LOCK INDICATOR BROKE OFF WITH NO UNUSUAL DAMAGE OR WEAR THAT WOULD.HAVE CAUSED! HAVE SEEN A LOT OF G6S LIKE THIS! *TR
Incident date: Aug 22, 2012
DRIVERS SIDE LOCK INDICATOR BROKE OFF WITH NO UNUSUAL DAMAGE OR WEAR THAT WOULD.HAVE CAUSED! HAVE SEEN A LOT OF G6S LIKE THIS! *TR
Incident date: Sep 4, 2014
MY WIFE WEIGHS 105 POUNDS AND IS 5 FEET 5 INCHES TALL, SHE IS NOT HEAVY ENOUGH TO TURN ON THE PASSENGER AIR BAG. I WENT TO ROYAL BUICK DEALER IN TUCSON ARIZONA TO ASK IF THEY COULD MAKE AN ADJUSTMENT, THEY SAID NO THAT THE BAGS ARE NOT ARMED FOR ANYONE UNDER 100 POUNDS. I EXPLAINED TO THEM THAT SHE WEIGHS 105 AND THEY SAID THEY COULD NOT HELP ME, I ASKED IF THEY COULD TURN IT ON PERMANENTLY AND TH
... EY SAID THEY COULD NOT. SO, SHE RIDES IN THIS TWO PASSENGER SPORTS CAR, WE ARE SENIOR CITIZENS WITH NO SMALL CHILDREN EVER RIDING, AND SHE IS UNEASY BECAUSE SHE DOES NOT HAVE THE PROTECTION OF THE PASSENGER AIR BAG. I THINK EVEN 100 POUNDS IS TOO HIGH OF A REQUIREMENT, SHOULD BE DOWN TO 70-80 POUNDS. MY GRAND DAUGHTER RIDES WITH ME ALSO, SHE IS 12, 5 FEET 6 INCHES AND WEIGHS 85 POUNDS SO SHE HAS NO PROTECTION FROM THE AIR BAG EITHER. *TRRead more
Incident date: Aug 30, 2014
THE PLASTIC SUPPLY OR RETURN PORT ON THE FUEL PUMP MODULE CRACKED, WHICH CAUSED A FUEL LEAK. *TR
Incident date: Sep 4, 2014
STEERING GETS SO HARD, I AT 220LBS CAN BARELY STEER THE CAR GOING FORWARD OR REVERSE. MY DAUGHTER IS LEARNING ON THIS CAR FOR HER LICENSE BUT I AM NO LONGER LETTING HER DRIVE IT SINCE THE STEERING RANDOMLY GETS HARD AND THE ELECTRONIC STABILITY CONTROL AND ABS LIGHTS HAVE COME ON ALSO. IT ALSO SAYS IN THE INFORMATION SECTION TRACTION CONTROL SERVICE. SOMETHING NEEDS TO BE DONE FROM GM FOR THESE
... PROBLEMS BEFORE THEY KILL PEOPLE. *TRRead more
Incident date: Sep 4, 2014
STEERING GETS SO HARD, I AT 220LBS CAN BARELY STEER THE CAR GOING FORWARD OR REVERSE. MY DAUGHTER IS LEARNING ON THIS CAR FOR HER LICENSE BUT I AM NO LONGER LETTING HER DRIVE IT SINCE THE STEERING RANDOMLY GETS HARD AND THE ELECTRONIC STABILITY CONTROL AND ABS LIGHTS HAVE COME ON ALSO. IT ALSO SAYS IN THE INFORMATION SECTION TRACTION CONTROL SERVICE. SOMETHING NEEDS TO BE DONE FROM GM FOR THESE
... PROBLEMS BEFORE THEY KILL PEOPLE. *TRRead more
Incident date: Sep 4, 2014
I HAVE RECEIVED MULTIPLE "IMPORTANT SAFETY RECALL" LETTERS AND POST CARDS FROM GM AND PONTIAC URGING ME TO HAVE THE DEFECTIVE IGNITION & START SWITCH THAT WAS INSTALLED IN MY VEHICLE REPLACED. I RECEIVED LETTERS WHEN THEY FIRST ACKNOWLEDGED THE ISSUE, LETTERS SAYING THAT PARTS WOULD BE AVAILABLE SOON, LETTERS WHEN PARTS STARTED TO BECOME AVAILABLE, ETC. A MONTH AGO I CONTACTED MY LOCAL GM DEAL
... ERSHIP SO THEY COULD ORDER THE PARTS AS INSTRUCTED AND WAS TOLD I WOULD BE CONTACTED WHEN THEY ARRIVED. I WAS INFORMED LAST WEEK THAT THE PARTS HAD ARRIVED AND WAS GIVEN A 10AM SERVICE TIME FOR TODAY (9/4/14). I ARRIVED TO GET THE WORK DONE, SIGNED THE PAPER TO ALLOW THEM TO DO THE WORK, AND HAD A SEAT IN THE WAITING ROOM. APPROXIMATELY 50 MINUTES LATER I WAS APPROACHED AND INFORMED THAT GM WOULD NOT AUTHORIZE THE WORK TO BE DONE BECAUSE MY CAR HAS AN "ALTERED" TITLE (IT HAD SOME FRONT END DAMAGE 50,000 MILES AGO THAT WAS FIXED 100% WITH ORIGINAL GM PARTS). NO WHERE IN ANY OF THE NOTIFICATIONS THAT I RECEIVED DID IT MENTION THIS. I ASKED HOW THAT COULD BE CONSIDERING AS OF FEBRUARY OF THIS YEAR 13 DEATHS STEMMING FROM THIS FATAL DESIGN FLAW HAD ALREADY BEEN ADMITTED TO BY GM...I WAS TOLD IT WAS GM POLICY AND THERE WAS NOTHING THE DEALERSHIP COULD DO ABOUT. I ASKED WHAT FRONT END DAMAGE HAD TO DO WITH A FATAL DESIGN FLAW IN ANOTHER AREA OF THE CAR...I WAS TOLD IT WAS GM POLICY AND THERE WAS NOTHING THE DEALERSHIP COULD DO ABOUT. HOW IN THIS DAY CAN A COMPANY, THAT HAS ADMITTED THAT THEY HAVE INSTALLED A FAULTY PART IN NUMEROUS VEHICLES THAT HAS LEAD TO THE LOSS OF HUMAN LIFE, WIPE THEIR HANDS OF THE SITUATION BECAUSE A VEHICLE HAS AND "ALTERED" TITLE?? I HAVE BEEN WAITING TO SELL MY G5 FOR OVER A MONTH NOW, WANTING TO MAKE SURE THE NEXT OWNER WAS SAFE AND THE VEHICLE WAS IN THE BEST POSSIBLE SHAPE...BUT HOW DO I DO THAT NOW WHEN GM WILL NOT HONOR THEIR OWN RECALLS? *TRRead more
Incident date: Sep 22, 2011
DRIVERS SIDE SEAT LEATHER IS CRACKING/SPLITING, CAR HAS ALWAYS HAD PROPER CARE. *TR
Incident date: Sep 22, 2011
DRIVERS SIDE SEAT LEATHER IS CRACKING/SPLITING, CAR HAS ALWAYS HAD PROPER CARE. *TR
Incident date: Aug 16, 2011
FRONT DRIVERS SIDE FACTORY HEADLIGHT (LEFT SIDE) BECAME HAZED OVER WHEN CAR HAD LOW MILES AND HAD ALWAYS BEEN STORED INSIDE. CAR HAS ALWAYS BEEN KEPT VERY CLEAN! NOTICED MANY OTHER PONTIAC G6S' HAVING THE SAME EXACT ISSUE. *TR
Incident date: Aug 16, 2011
FRONT DRIVERS SIDE FACTORY HEADLIGHT (LEFT SIDE) BECAME HAZED OVER WHEN CAR HAD LOW MILES AND HAD ALWAYS BEEN STORED INSIDE. CAR HAS ALWAYS BEEN KEPT VERY CLEAN! NOTICED MANY OTHER PONTIAC G6S' HAVING THE SAME EXACT ISSUE. *TR
Incident date: Aug 16, 2011
FRONT DRIVERS SIDE FACTORY HEADLIGHT (LEFT SIDE) BECAME HAZED OVER WHEN CAR HAD LOW MILES AND HAD ALWAYS BEEN STORED INSIDE. CAR HAS ALWAYS BEEN KEPT VERY CLEAN! NOTICED MANY OTHER PONTIAC G6S' HAVING THE SAME EXACT ISSUE. *TR
Incident date: Sep 5, 2013
TL* THE CONTACT OWNS A 2007 PONTIAC G6 . THE CONTACT RECEIVED A NOTIFICATION FOR RECALL NHTSA CAMPAIGN NUMBER: 14V224000 (POWER TRAIN). HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER HAS BEEN MADE AWARE OF THE ISSUE. THE CONTACT HAS NOT EXPERIENCE A FAILURE.
Incident date: Sep 5, 2013
TL* THE CONTACT OWNS A 2007 PONTIAC G6. THE CONTACT RECEIVED A NOTIFICATION FOR RECALL NHTSA CAMPAIGN NUMBER: 14V252000 (ELECTRICAL SYSTEM, ELECTRONIC STABILITY CONTROL, EXTERIOR LIGHTING, SERVICE BRAKES, HYDRAULIC , VEHICLE SPEED CONTROL). HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MA
... NUFACTURER WAS MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.Read more
Incident date: Jun 1, 2013
UPON ACCELERATING AT SPEEDS ABOVE 50MPH, MY TRACTION CONTROL INDICATOR WILL COME ON, SOMETIMES SAYING TRACTION OFF, AND SOMETIMES SAYING TO SERVICE TRACTION. IT WILL SOMETIMES STAY ON AND MAKE MY CAR JERK AROUND A LOT WHILE IT'S SHIFTING GEARS. IF IT DOESN'T GO AWAY SHORTLY AFTER IT CAME ON, IT WILL GO AWAY ONCE I LEAVE MY CAR TURNED OFF FOR A WHILE. IT HAPPENS SO RANDOMLY, AND SOMETIMES WILL BE M
... ONTHS BETWEEN EPISODES, THAT WHEN I'VE TAKEN IT TO HAVE IT LOOKED AT, THEY CAN'T GET IT TO HAPPEN. *TRRead more
Incident date: Jun 1, 2013
UPON ACCELERATING AT SPEEDS ABOVE 50MPH, MY TRACTION CONTROL INDICATOR WILL COME ON, SOMETIMES SAYING TRACTION OFF, AND SOMETIMES SAYING TO SERVICE TRACTION. IT WILL SOMETIMES STAY ON AND MAKE MY CAR JERK AROUND A LOT WHILE IT'S SHIFTING GEARS. IF IT DOESN'T GO AWAY SHORTLY AFTER IT CAME ON, IT WILL GO AWAY ONCE I LEAVE MY CAR TURNED OFF FOR A WHILE. IT HAPPENS SO RANDOMLY, AND SOMETIMES WILL BE M
... ONTHS BETWEEN EPISODES, THAT WHEN I'VE TAKEN IT TO HAVE IT LOOKED AT, THEY CAN'T GET IT TO HAPPEN. *TRRead more
Incident date: Sep 1, 2014
LETTER FROM CONSTITUENT REGARDING HER PONTIAC G6 COUPE; SHE'S HAVING PROBLEMS SELLING HER VEHICLE DUE TO A RECALL ON THE VEHICLE; REQUEST THE ADVICE AS TO THE BEST COURSE OF ACTION THAT CAN BE TAKEN AGAINST GM FOR THE SWIFT RESOLUTION OF THIS MATTER. *SD
Incident date: May 16, 2014
WAS PARKED IN FRIENDS DRIVEWAY, EMERGENCY BRAKE ENGAGED. STARTED CAR AND DEPRESSED BRAKE AND RELEASED EMERGENCY BRAKE, THEN SHIFTED INTO REVERSE AND BACKED OUT OF DRIVEWAY. WHEN I SHIFTED FROM REVERSE TO DRIVE THE CAR DIED. I PUT IT IN PARK AND RESTARTED.. ENGINE WAS RUNNING VERY ROUGH, KEPT TRYING TO DIE, NO POWER STEERING, NO COOL AIR OR A/C.. SERVICE ESC MESSAGE ON DISPLAY AS WELL AS TRACTION
... CONTROL "OFF". CALLED ONSTAR FOR ONDEMAND DIAG. AND THEY SAID WAS MY EMERGENCY BRAKE AND TO SHUT OFF CAR AND THEN RESTART... DID THAT AND CAR RAN FINE.. FOR APPROX. A MONTH.. THEN HAPPENED AGAIN.. ON DEMAND DIAG COULD NOT GET A CODE.. NEITHER COULD DEALERSHIP. THIS CONTINUED INTERMITTENTLY UNTIL ABOUT 1 MONTH AGO.. @ 60,400 MILES (NOW OUT OF WARRANTY) TOOK CAR TO DEALERSHIP AND THEY WERE ABLE TO GET 2 CODES.. ONE SAYING ELECTRONIC STABILIZER AND OTHER SAYING THERMOSTAT HAS WENT OUT. (1 CONSISTENT THING WITH ALL THIS .. MY THERMOSTAT GAUGE WOULD BE FLATLINED NO MATTER IF CAR HAD BEEN DRIVEN RECENTLY OR NOT) UPON LEAVING THE DEALERSHIP PARKING LOT, JUST AS I WAS PULLING ONTO ROAD .THE "BUMPS"FROM THE TRANSITION CAUSED THE GAUGE TO START DISPLAYING AGAIN.. AND POWER STEERING, A/C AND COOL AIR RESUMED WORKING AS WELL... HAVE NOT HAD ANY MORE EPISODES FOR ABOUT A MONTH.. UNTIL 9/2 WHEN I GOT INTO MY CAR AND STARTED IT .. TEMP GAUGE NO WORK, NO A/C NO PWR STEERING.. REACHED DESTINATION AND CAR SAT APPROX 4 HRS.. THEN DROVE 4 MILES AND ENGINE LIGHT CAME ON AND HAS REMAINED ON. CHECKED FLUIDS .. ALL FINE.. BUT DID NOTICE ENGINE FAN STAYING ENGAGED CONTINUALLY WHILE DRIVING AND FOR A FEW SECONDS AFTER TURNING OFF CAR. *TRRead more
Incident date: May 16, 2014
WAS PARKED IN FRIENDS DRIVEWAY, EMERGENCY BRAKE ENGAGED. STARTED CAR AND DEPRESSED BRAKE AND RELEASED EMERGENCY BRAKE, THEN SHIFTED INTO REVERSE AND BACKED OUT OF DRIVEWAY. WHEN I SHIFTED FROM REVERSE TO DRIVE THE CAR DIED. I PUT IT IN PARK AND RESTARTED.. ENGINE WAS RUNNING VERY ROUGH, KEPT TRYING TO DIE, NO POWER STEERING, NO COOL AIR OR A/C.. SERVICE ESC MESSAGE ON DISPLAY AS WELL AS TRACTION
... CONTROL "OFF". CALLED ONSTAR FOR ONDEMAND DIAG. AND THEY SAID WAS MY EMERGENCY BRAKE AND TO SHUT OFF CAR AND THEN RESTART... DID THAT AND CAR RAN FINE.. FOR APPROX. A MONTH.. THEN HAPPENED AGAIN.. ON DEMAND DIAG COULD NOT GET A CODE.. NEITHER COULD DEALERSHIP. THIS CONTINUED INTERMITTENTLY UNTIL ABOUT 1 MONTH AGO.. @ 60,400 MILES (NOW OUT OF WARRANTY) TOOK CAR TO DEALERSHIP AND THEY WERE ABLE TO GET 2 CODES.. ONE SAYING ELECTRONIC STABILIZER AND OTHER SAYING THERMOSTAT HAS WENT OUT. (1 CONSISTENT THING WITH ALL THIS .. MY THERMOSTAT GAUGE WOULD BE FLATLINED NO MATTER IF CAR HAD BEEN DRIVEN RECENTLY OR NOT) UPON LEAVING THE DEALERSHIP PARKING LOT, JUST AS I WAS PULLING ONTO ROAD .THE "BUMPS"FROM THE TRANSITION CAUSED THE GAUGE TO START DISPLAYING AGAIN.. AND POWER STEERING, A/C AND COOL AIR RESUMED WORKING AS WELL... HAVE NOT HAD ANY MORE EPISODES FOR ABOUT A MONTH.. UNTIL 9/2 WHEN I GOT INTO MY CAR AND STARTED IT .. TEMP GAUGE NO WORK, NO A/C NO PWR STEERING.. REACHED DESTINATION AND CAR SAT APPROX 4 HRS.. THEN DROVE 4 MILES AND ENGINE LIGHT CAME ON AND HAS REMAINED ON. CHECKED FLUIDS .. ALL FINE.. BUT DID NOTICE ENGINE FAN STAYING ENGAGED CONTINUALLY WHILE DRIVING AND FOR A FEW SECONDS AFTER TURNING OFF CAR. *TRRead more
Incident date: May 16, 2014
WAS PARKED IN FRIENDS DRIVEWAY, EMERGENCY BRAKE ENGAGED. STARTED CAR AND DEPRESSED BRAKE AND RELEASED EMERGENCY BRAKE, THEN SHIFTED INTO REVERSE AND BACKED OUT OF DRIVEWAY. WHEN I SHIFTED FROM REVERSE TO DRIVE THE CAR DIED. I PUT IT IN PARK AND RESTARTED.. ENGINE WAS RUNNING VERY ROUGH, KEPT TRYING TO DIE, NO POWER STEERING, NO COOL AIR OR A/C.. SERVICE ESC MESSAGE ON DISPLAY AS WELL AS TRACTION
... CONTROL "OFF". CALLED ONSTAR FOR ONDEMAND DIAG. AND THEY SAID WAS MY EMERGENCY BRAKE AND TO SHUT OFF CAR AND THEN RESTART... DID THAT AND CAR RAN FINE.. FOR APPROX. A MONTH.. THEN HAPPENED AGAIN.. ON DEMAND DIAG COULD NOT GET A CODE.. NEITHER COULD DEALERSHIP. THIS CONTINUED INTERMITTENTLY UNTIL ABOUT 1 MONTH AGO.. @ 60,400 MILES (NOW OUT OF WARRANTY) TOOK CAR TO DEALERSHIP AND THEY WERE ABLE TO GET 2 CODES.. ONE SAYING ELECTRONIC STABILIZER AND OTHER SAYING THERMOSTAT HAS WENT OUT. (1 CONSISTENT THING WITH ALL THIS .. MY THERMOSTAT GAUGE WOULD BE FLATLINED NO MATTER IF CAR HAD BEEN DRIVEN RECENTLY OR NOT) UPON LEAVING THE DEALERSHIP PARKING LOT, JUST AS I WAS PULLING ONTO ROAD .THE "BUMPS"FROM THE TRANSITION CAUSED THE GAUGE TO START DISPLAYING AGAIN.. AND POWER STEERING, A/C AND COOL AIR RESUMED WORKING AS WELL... HAVE NOT HAD ANY MORE EPISODES FOR ABOUT A MONTH.. UNTIL 9/2 WHEN I GOT INTO MY CAR AND STARTED IT .. TEMP GAUGE NO WORK, NO A/C NO PWR STEERING.. REACHED DESTINATION AND CAR SAT APPROX 4 HRS.. THEN DROVE 4 MILES AND ENGINE LIGHT CAME ON AND HAS REMAINED ON. CHECKED FLUIDS .. ALL FINE.. BUT DID NOTICE ENGINE FAN STAYING ENGAGED CONTINUALLY WHILE DRIVING AND FOR A FEW SECONDS AFTER TURNING OFF CAR. *TRRead more
Incident date: Feb 8, 2008
TL* THE CONTACT OWNS A 2006 PONTIAC GRAND PRIX. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE HEADLIGHTS FAILED WITHOUT WARNING. THE HIGH BEAMS WORK INTERMITTENTLY AND COMPLETELY FAILED WHEN THE BLINKERS WERE ENGAGED. THE VEHICLE WAS TAKEN TO A DEALER WHERE THEY WERE UNABLE TO FIND A FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS UNKNOWN.
Incident date: Aug 9, 2014
PASSENGER AIRBAG SENSOR WENT BAD. LEAVES AIRBAG DISABLED WHETHER OR NOT THERE IS A PASSENGER IN THE SEAT. COULD BE VERY DANGEROUS AND GM REFUSES TO ACKNOWLEDGE RESPONSIBILITY FOR THIS VERY COMMON PROBLEM. *TR
Incident date: Mar 3, 2014
WHEN DRIVING AND ATTEMPTING TO SLOW DOWN, I AM ALMOST THROWN FROM MY VEHICLE BECAUSE IT FEELS LIKE THE WHEELS COMPLETELY STOPPED TURNING WHEN THE CAR IS DOWNSHIFTING. *TR
Incident date: Jul 3, 2014
EVERY TIME I LET MY CAR SIT FOR 2 HOURS OR MORE, I START IT UP AND THE BELT ON THE TENSIONER SQUEAK FOR 15 SECONDS. ALSO THE BATTERY LIGHT COMES ON AND THE RIM FLUCTUATE BETWEEN 1,000 AND 2,000. WHEN I DRIVE IT THE BATTERY LIGHT WILL CONTINUE TO STAY ON BUT EVERY TIME THE AIR BAG LIGHT TURNS ON AND I'M ACCELERATING THE ENGINE WILL NOT SHIFT, THE RPMS WILL REV UP TO RED LINE IF PUSHED THAT FAR, EVE
... NTUALLY THE LIGHT FOR AIRBAG AND BATTERY WILL SHUT OFF AND IT WILL SHIFT. SOMETIMES WHEN I HIT THE GAS PEDAL WHILE THIS IS DOING THIS AT NIGHT, MY DASHBOARD AS WELL AS RADIO LIGHTS WILL SHUT OFF UNTIL RPMS GO DOWN TO 2,000. *TRRead more